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Issue date | Title | Topic | |
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ML20199F650 | 14 November 1997 | Special Rept:On 971031,one High Range Primary Containment Radiation Monitor Declared Inoperable for More than Seven Days.Caused by Component/Equipment Failure Inside Drywell. Will Repair or Replace Detector or Associated Cable | |
ML20207K924 | 7 October 1988 | RO 88-01:on 880725,during Inventory of Snm,Discrepancy Noted for Intermediate Range Monitor Detector Removed from Core Location C.Caused by Inadequage SNM Control & Accountability Practices Existing at Time of Installation & Shipment | |
ML20235J454 | 2 July 1987 | Special Rept 87-01,Rev 1:on 870321,three Seismic Triggers Would Not Provide Required Control Room Annunciation Upon Receipt of Horizontal 0.1 G Seismic Acceleration.All Instruments Removed from Site Repaired.Instructions Revised | |
ML20117N750 | 8 May 1985 | Advises That Rept Will Not Be Prepared for RO BFRO-50-296/85011 | |
ML20086G597 | 3 January 1984 | Telecopy RO 50-259/83073:on 831231,reactor Water Sample Indicated Chloride Concentration of 525 Ppb.Steam Flow Greater than 100,000 Lbm/H.Caused by Possible Resin Intrusion.Investigation in Progress | |
ML20083E155 | 15 December 1983 | Telecopy RO 50-296-83060:on 831214,nine of 13 two-stage Relief Valves Tested Initially Failed to Lift within Allowable Range.Cause Being Evaluated W/Manufacturer.Nine Valves Will Be Reset & Retested Prior to Installation | |
ML20082V341 | 12 December 1983 | Telecopy RO 50-259/83068:on 831210,RHR Pump 1C Motor Sparked & Smoked.Motor Shut Down & Restarted,Then Tripped on Overcurrent.Pump Declared Inoperable.Caused by Winding Failure.Motor Will Be Replaced | |
ML20083A430 | 8 December 1983 | Telecopy Ro:On 831207,linear Crack Indication Identified by NDE in Weld DSHS-3-2 of Head Spray Piping of RHR Sys. Apparently Caused by Intergranular Stress Corrosion Cracking.Insp Per IE Bulletin 83-02 Will Be Performed | |
ML20082D025 | 14 November 1983 | Telecopy Ro:On 831110,HPCI Isolated Due to Failure of Exhaust Rupture Disc.Cause Unknown.Maint Request Issued to Replace Disc.Investigation Continuing | |
ML20078M978 | 14 October 1983 | Telecopy Ro:On 831013,routine Analysis of 831007 Scram Revealed That 2-LT-85-45A Did Not Initiate Trip When SDIV Exceeded 50 Gallons.On 831014,testing of Transmitter Revealed Slow & Erratic Response to Measured Variable | |
ML20078H328 | 6 October 1983 | Telecopy RO 83061:on 831004,hydrogen-oxygen Analyzer Sample Pump B Determined Inoperable Following Notification from Metal Bellows Corp of Generic Deficiency.Pump Replaced W/ Upgraded Model in Stock on 831005 | |
ML20080L896 | 20 September 1983 | Telecopy Ro:On 830919,Surveillance 4.7.A.2.G3 Determined Leakage Rates Exceeded for MSIV Lines A,C & D.Caused by Leakage Past Main Valve Seat.Seating Surfaces Modified | |
ML20076J584 | 28 August 1983 | Telecopy Ro:On 830826,cracks Discovered on Core Spray Welds DCS-1-7 & DCS-1-8 & Reactor Water Cleanup Welds DSRWC-1-3 & DSRWC-1-2.Total Welds to Be Inspected Increased from 53 to 79.Updated Insp Results Encl | |
ML20076J745 | 25 August 1983 | Telecopy RO BFRO-50-259/83049 R9:on 830825,weld Crack Indications Discovered in Welds on Core Spray & Reactor Water Cleanup.Number of Welds to Be Inspected Increased from 53 to 79 | |
ML20076F335 | 23 August 1983 | Telecopy RO 50-259/83-49:on 830811,pipe Weld Cracking Indications Revealed by Addl Ultrasonic Insps.Possibly Caused by Corrosion.Addl Welds Inspected.Insp Repts to Be Submitted Periodically | |
ML20080D692 | 22 August 1983 | Telecopy RO 83049R7:on 830812,indications Discovered on Core Spray Welds DCS-1-7 & DCS-1-8 & Reactor Water Cleanup Welds DSRWC-1-3 & DSRWC-1-2.Addl 29 Welds Will Be Inspected.Insp Results Encl | |
ML20080E077 | 22 August 1983 | Telecopy Ro:On 830812,cracks Found on Welds DCS-1-7, DSRWC-1-3,DCS-1-8 & DSRWC-1-2.Cause Not Stated.Total Number of Welds to Be Inspected Increased from 53 to 79 | |
ML20080D572 | 18 August 1983 | Telecopy Ro:On 830812,weld Cracks Discovered in Core Spray & Reactor Water Cleanup Sys.Addl 29 Welds Will Be Inspected. Insp Results Encl | |
ML20076F691 | 17 August 1983 | Telecopy Ro:On 830812,indications Found on Pipe Welds for Core Spray & Reactor Water Cleanup.Addl 29 Welds Will Be Inspected Increasing Total Number of Welds to Be Inspected to 82 | |
ML20076F864 | 15 August 1983 | Telecopy Ro:On 830815,indications Identified on Welds DCS-1-7,DSRWC-1-3,DCS-1-8 & DSRWC-1-2.Weld Insp Results Encl | |
ML20076F521 | 15 August 1983 | Telecopy Ro:On 830812,core Spray Weld DCS-1-7 Had Intermittent Indication on Pipe Side of Weld Approx 41% Through Wall Depth.Reactor Water Cleanup Weld DSRWC-1-3 Had Two Indications Approx 5 Inches Long | |
ML20076F535 | 12 August 1983 | Telecopy Ro:On 830812,during Routine Surveillance Testing, Four of Four Turbine first-stage Permissive Switches Discovered Out of Tech Spec Limits.Caused by Setpoint Drift. Setpoints Reset | |
ML20077A034 | 12 July 1983 | Supplemental Ro:On 830604,13,14 & 15 Standby Gas Treatment Train B Declared Inoperable.Caused by Increased Damper Closure Since Measurements Made in May 1983.Dampers Returned to Preset Position | |
ML20077A279 | 6 July 1983 | Telecopy RO 50-259/83036:on 830705,seven two-stage Target Rock Relief Valves Tested at Wyle Labs for as-found Set Pressure Failed to Lift within Allowable Range.Caused Under Evaluation.Valves Will Be Reset & Retested | |
ML20071N446 | 24 May 1983 | Telecopy RO 50-286/8331:on 830520,reactor Low Pressure Switches PS-3-74B & PS-68-96,switch 2 Found Below Tech Spec Limits.Caused by Setpoint Drift.Setpoints Reset & Design Change Request DCR 1398 Initiated to Replace Switches | |
ML20071H580 | 18 May 1983 | Telecopy RO 50-259/83024:on 830517,design Review of Emergency Diesel Generator Room Ventilation Sys Capabilities Revealed Design Temp Limits of Some Electrical Components May Be Exceeded.Caused by Error in Heat Dissipation Data | |
ML20069M455 | 25 April 1983 | Telecopy RO 50-259/83021:on 830424,130 Fuel Bundles Unloaded from Core & Placed in High Density Fuel Storage Rack in Spent Fuel Storage Pool Not Tested for Boron Concentration. Caused by Inadequate Procedures | |
ML20069L336 | 20 April 1983 | Telecopy RO 50-296/83024:on 830419,review of Licensing Documents Revealed Lead Test Assemblies Could Reach Max of 18.8 Kw/Ft in Event of Rod Withdrawal Error.Caused by Error in Preparation & Review of GE Licensing Documents | |
ML20069K737 | 18 April 1983 | Telecopy RO 50-259/83020:on 830418,leakage Rate for Line a MSIV Found Above Tech Spec Limit.Caused by Leakage Past Main Valve Seat.Corrective Maint & long-term Mod Planned | |
ML20064N985 | 9 February 1983 | Telecopy Message of RO 50-260-8302:on 830208,pressure Switches PS-68-96,PS-3-74A & PS-3-74B Found Out of Tech Spec Limits During Performance of Surveillance Instruction 4.2.B-7.Caused by Setpoint Drift.Switches Recalibr | |
ML20064L256 | 8 February 1983 | Telecopy Ro:On 830207,reactor Low Water Level Switches Found Out of Tolerance.Caused by Instrument Drift.Switches Recalibr,Tested & Returned to Svc.Switches Will Be Replaced W/Analog Transmitter/Trip Unit Sys at Later Date | |
ML20064M146 | 7 February 1983 | Telecopy Message of RO 50-259/83006:on 830205,relief Valve PCV 1-22 Failed to Reseat Fully After Actuation to Control Reactor Pressure.Probably Caused by Excessive Leakage of Pilot Valve.Pilot Valve & Solenoid Actuator Replaced | |
ML20062K302 | 3 December 1980 | RO 50-259/8085:on 801123 Reservoir Water Temp Exceeded Max Allowable Temp.Caused by Influence of Colder Water Upstream.Load on Unit 3 Reduced in Four Stages to Shutdown & Water Flows Increased | |
ML20064K346 | 29 October 1980 | Ro:On 801029,HPCI Removed from Svc Due to Ground Occurring on Gland Seal Condensor Pump Motor.Cause Attributed to Moisture Found in Pump.Hpci Was Returned to Svc | |
ML20204B850 | 14 September 1978 | RO 50-259/7827:on 780913,recirculation Loop a Flow Decreased from 41,000 to 33,000 Cpm W/Corresponding Increase in Pump Delta F.Caused by Valve Stem Separating from Valve Disc | |
ML20084T913 | 21 September 1976 | Telecopy RO BFRO-50-259/7615:on 760921,HPCI & RCIC Failed Test.Reactor Shutdown Effected & Pressure Reduced to 100 Psi | |
ML20084T893 | 21 September 1976 | Telecopy RO BFRO-50-259/7617:on 760921,prescribed Rate of Reactor Coolant Change During Normal Heatup Exceeded When Averaged Over 1 H Period | |
ML20084U321 | 7 September 1976 | Telecopy RO BFRO-50-260/7610:on 760906,out-of-sequence Control Rod Withdrawn.Cause Not Stated | |
ML20084U269 | 28 July 1976 | Telecopied RO BFRO-50-296/762T:on 760728,during Surveillance Testing,Control Rod Accumulators Found Discharged W/O Control Rod Drive Electrically Disarmed.Cause Not Stated | |
ML20084U352 | 9 July 1976 | Telecopy RO BFRO-50-260/768T:on 760709,unit Scrammed Due to Loss of Neutron Monitoring Battery 2A.Cause Not Stated | |
ML20084U454 | 19 June 1976 | Telecopied RO BFRO-50-260/765T:on 760619,water Supply Valves 85-612 & 85-615 to Hydraulic Control Unit 30-32 Found Closed.No Cause Stated.Valves Opened | |
ML20085E953 | 4 July 1975 | Telecopy Message of Ro:On 750703,facility Became Inoperable Due to Governor Problems.Manual Operation Possible.Lee Gas Turbine Could Not Be Tied in Through Isolated Line to Supply & Buy Power.Investigation Continuing | |
ML20085F700 | 11 March 1975 | Telecopy RO BFAO-50-259/754T:on 750311,drywell Atmosphere Above Permissible Oxygen Concentration.Cause Not Stated | |
ML20085F790 | 27 February 1975 | Telecopy RO BFAO-50-259/753T:on 750226,pressure Relief Valve PCVI-4 Prematurely Lifted & Failed to Reseat Until Pressure Reached 480 Psig.Reactor in Cold Shutdown Condition for Valve Replacement.Cause Not Stated | |
ML20085G090 | 19 January 1975 | Telecopy Ro:On 750119,pressure Relief Valve PCV-1-4 Operated Several Times W/No Appreciable Blowdown.Unit in Cold Shutdown for Investigation & Possible Repair | |
ML20085G101 | 7 January 1975 | Telecopy RO BFAO-50-260/751T:on 750107,RCIC Failed to Operate Following Planned full-load Trip | |
ML20085G614 | 27 December 1974 | Telecopy RO BFAO-50-259/7461T:on 741227,proper Documentation Not Issued Prior to Installation of Dampening Pin for Main Steam Line high-flow Pressure Switch Snubbers.Cause Not Stated | |
ML20085G628 | 25 December 1974 | Telecopy Ro:On 741224,both Channels of Offgas Radiation Monitor Taken Out of Svc to Repair Leaking Flow Indicator. Cause Not Stated | |
ML20085G180 | 19 December 1974 | Telecopy RO BFAO-50-260/7436T:on 741218,drywell Air Sampling Monitor Failed.Cause Not Stated | |
ML20085G256 | 18 December 1974 | Telecopy RO BFAO-50-260/7435T:on 741218,RHR Valve 2-FCV-74-66 Closed During Routine Surveillance Testing & Could Not Be Opened.Cause Not Stated |