ML20085E953
ML20085E953 | |
Person / Time | |
---|---|
Site: | Browns Ferry, Oconee, 05000000 |
Issue date: | 07/04/1975 |
From: | James Smith DUKE POWER CO. |
To: | Moseley N NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML20085E950 | List: |
References | |
NUDOCS 8308170159 | |
Download: ML20085E953 (1) | |
Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20199F6501997-11-14014 November 1997
[Table view]Special Rept:On 971031,one High Range Primary Containment Radiation Monitor Declared Inoperable for More than Seven Days.Caused by Component/Equipment Failure Inside Drywell. Will Repair or Replace Detector or Associated Cable ML20148S3141997-06-30030 June 1997 Ro:On 970422,Oconee Unit 2 Was Shut Down Due to Leak in Rcs. Leak Was Caused by Crack in Pipe to safe-end Weld Connection at RCS Nozzle for HPI Sys A1 Injection Line.Unit 1 Was Shut Down to Inspect Hpis Injection Lines & Implement Ldst Mods ML20117A5981992-11-23023 November 1992 Special Rept:On 921119,ability of Control Battery Racks to Withstand Seismic Event Could Not Be Confirmed & Batteries Declared Inoperable.Batteries Expected to Be Restored in TS Required Time ML20207K9241988-10-0707 October 1988 RO 88-01:on 880725,during Inventory of Snm,Discrepancy Noted for Intermediate Range Monitor Detector Removed from Core Location C.Caused by Inadequage SNM Control & Accountability Practices Existing at Time of Installation & Shipment ML20236T0791987-11-25025 November 1987 Advises LER 269/87-09,re Degradation of More than One Functional Unit of Emergency Power Switching Logic for Units 2 & 3,in Preparation & Will Be Submitted by 871215. Incident Originally Discussed in Special Rept ML20235J4541987-07-0202 July 1987 Special Rept 87-01,Rev 1:on 870321,three Seismic Triggers Would Not Provide Required Control Room Annunciation Upon Receipt of Horizontal 0.1 G Seismic Acceleration.All Instruments Removed from Site Repaired.Instructions Revised ML20210J6671987-02-0303 February 1987 Special Rept:On 861113-14,1206 & 23,spurious Fire Alarms Annunciated in Control Room.On 870118,unit Shut Down Due to Problems W/Detectors.Cause Undetermined.Technicians Investigating Potential Problem W/Detectors BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified1986-11-12012 November 1986 Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released1986-11-10010 November 1986 Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released ML20215N4011986-10-20020 October 1986 Special Rept:On 860808,during Shutdown for Maint,Found Unidentified Wires in Environmentally Qualified Limitorque motor-operated Valves.Caused by Mfg Deficiency.Wires Replaced ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found1986-08-29029 August 1986 Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found ML20209C1871986-08-13013 August 1986 Special Rept:On 860707,fire Barrier Penetration Nonfunctional.Caused by Design Deficiency Due to Ineffective Communication Between Design Groups.Fire Watch Established. Notice Initiated Requiring Installation of Fire Wall ML20212D2221986-07-29029 July 1986 Special Rept:On 860606,determined That Inadequate Assurance Existed Re Use of Qualified Grease in All Limitorque Operators.Appropriate Programs Not Updated to Reflect Revs. Lubrication Records Reviewed ML20211K8211986-06-18018 June 1986 Special Rept:On 860521,valid Failure Occurred on Div 2 Diesel Generator During Performance of Tech Spec Surveillance 4.8.1.1.2.Caused by Failure of Jacket Water Thermostatic Control Valve to Open ML20238E4591986-06-17017 June 1986 Partially Withheld Security Event Rept:On 860612,withheld Discovery Made Re 860604 Moderate Loss of Security Effectiveness.Caused by Inadequate Post Orders & Training for Assignment.Assignments Will Be Specifically Addressed 05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised1986-04-14014 April 1986 Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised ML20210N5641986-04-14014 April 1986 Special Rept:On 860206,fire Wall Determined to Be Degraded. Caused by Personnel Failure to Recognize That Removing Small Amount of Pyrocrete Would Degrade Fire Wall.Fire Wall Repaired & Declared Fully Functional.Part 21 Related BECO-86-016, Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended1986-02-20020 February 1986 Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended BECO-85-220, Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured1985-12-0909 December 1985 Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured ML20137D6481985-11-22022 November 1985 Ro:On 851119,Keowee Hydro Unit 2 Inoperable Beyond Oconee Tech Spec Limit Due to Burned Out Laminated Copper Connection Between Two Coils.Caused by Cracked Brazement. Connector & Field Coils Will Be Replaced ML20135D7781985-08-21021 August 1985 Ro:On 850722,CRD Dc Breaker CB-1 Failed Trip Time Requirement During Channel C Reactor Protective Sys on-line Test.Cause of Failure Could Not Be Determined.Failed CB-1 Breaker Placed in Tripped Position ML20129G0441985-05-24024 May 1985 Ro:On 850425,batch of Powdex Resin from Powdex Cells 1A & 1D Transferred to Chemical Treatment Pond 2 Instead of Powdex Backwash Tank.Caused by Misalignment of Valve CTP-7.Valve Correctly Positioned ML20117N7501985-05-0808 May 1985 Advises That Rept Will Not Be Prepared for RO BFRO-50-296/85011 ML20108E5341985-02-14014 February 1985 Special Rept:On 850114,CRD Dc Breaker Failed Slow During Channel D Reactor Protective Sys on-line Test.Caused by Sticking Trip Latch Roller Bearings & Excessive Trip Latch Operating Torque.Breaker Front Frame Replaced ML20112D0771984-12-14014 December 1984 Special Rept:On 841109,many Fire Barriers Did Not Meet Surveillance Insp Acceptance Criteria & Declared Inoperable. Caused by Const/Installation Deficiency,Component Failure/ Malfunction & Some Unknown Causes.Firestops Repaired ML20099E0241984-10-24024 October 1984 Special Rept:On 840927,discovered That Contaminated Oil Shipped to Lee Steam Station for Disposal by Incineration. Caused by Misinterpretation of Regulations.Shipments of Contaminated Oil Halted ML20093F1911984-10-0808 October 1984 RO 269/83-16,revising 831107 Commitment Re Completion Date of 850101 to Relocate Hydrogen Purge Unit Connection Near Permanent Hookup Connections on Each Unit for Hydrogen Recombiner ML20093L5061984-10-0505 October 1984 Special Rept:On 840906,batch of Powdex Resin from Powder Cells 2D & 2E Transferred from Plant to Chemical Treatment Pond 1 Instead of to Powdex Backwash Tank.Caused by Misalignment of Valves of Chemical Treatment Ponds 5 & 6 ML20106B4791984-10-0303 October 1984 Special Rept:On 840928,power Circuit Breaker 22 Explosively Short Circuited,Causing Power Circuit Breaker 9 to Open, Isolating 230 Kv Overhead Line from Primary OL Power Source. Breaker Reclosed ML20096A1061984-08-22022 August 1984 Suppl to Rev 1 to RO-287/83-13:containment Isolation Valve 3CS-5 Declared Inoperable Due to Leakage Past Seat. Investigation Into Valve Failure Conducted & Diaphragm Replaced ML20094N8601984-07-27027 July 1984 RO 269/83-20 Re Trip Shaft & Bearing Assembly Portions of CRD Breaker Front Frame Assemblies.Nine of 17 GE Frames Defective.Util Awaiting Schedule for Delivery of New Frames ML20092A4291984-06-0606 June 1984 Special Rept:On 840419,during Fuel Reshuffling for Cycle 8, Fuel Assembly FA 0297 Became Stuck in Fuel Location E-10 During Insertion & Fuel Assembly FA 029Q Damaged.Caused by Inadequate Procedure Change ML20092A3841984-04-30030 April 1984 Updated RO-269/83-20 Submitted on 840111 Re Two CRD Breakers Experiencing Delay During Testing.Ge Will Ship CRD Breaker Front Frame Assemblies on 840514.Installation Will Be Complete on All Three Units by 840731 ML20084G4851984-04-18018 April 1984 Updated RO 269/83-17:seals at Conduit Connections Defective. Scotchcast 9 Epoxy Resin Will Be Utilized to Seal Conduit Connections,Dow Corning RTV 3145 Applied to Conduit Fittings & Conduit/Cable Seals Will Be Upgraded AECM-84-0204, Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored1984-04-0606 April 1984 Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored ML20086G5971984-01-0303 January 1984 Telecopy RO 50-259/83073:on 831231,reactor Water Sample Indicated Chloride Concentration of 525 Ppb.Steam Flow Greater than 100,000 Lbm/H.Caused by Possible Resin Intrusion.Investigation in Progress ML20083E1551983-12-15015 December 1983 Telecopy RO 50-296-83060:on 831214,nine of 13 two-stage Relief Valves Tested Initially Failed to Lift within Allowable Range.Cause Being Evaluated W/Manufacturer.Nine Valves Will Be Reset & Retested Prior to Installation ML20082V3411983-12-12012 December 1983 Telecopy RO 50-259/83068:on 831210,RHR Pump 1C Motor Sparked & Smoked.Motor Shut Down & Restarted,Then Tripped on Overcurrent.Pump Declared Inoperable.Caused by Winding Failure.Motor Will Be Replaced ML20083A4301983-12-0808 December 1983 Telecopy Ro:On 831207,linear Crack Indication Identified by NDE in Weld DSHS-3-2 of Head Spray Piping of RHR Sys. Apparently Caused by Intergranular Stress Corrosion Cracking.Insp Per IE Bulletin 83-02 Will Be Performed ML20082R7561983-12-0202 December 1983 Ro:On 831015-16,standby Bus 2 Deenergized to Verify Emergency Power Path & CT-3 Startup Transformer Locked Out. Caused by Failure of Two Insulators Causing Short to Ground. Info Supersedes 831101 Rept ML20082H5161983-11-21021 November 1983 Ro:Re Loss of Power on Both Standby Buses W/Both Units Out of Svc.Investigation Incomplete.Necessary Info Will Be Submitted by 831202 ML20198H3691983-11-14014 November 1983 Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg ML20082C6081983-11-14014 November 1983 Ro:On 831109,while Units Out of Svc for Planned Maint,Lee 6C Gas Turbine Tripped off-line,deenergizing Standby Buses & Placing Units in Degraded Mode Beyond Tech Spec Limit.Cause Undetermined.Next Rept by 831118 ML20082D0251983-11-14014 November 1983 Telecopy Ro:On 831110,HPCI Isolated Due to Failure of Exhaust Rupture Disc.Cause Unknown.Maint Request Issued to Replace Disc.Investigation Continuing ML20078P9651983-11-0202 November 1983 Ro:On 831028,while Unit Out of Svc,Lee 6C Gas Turbine Tripped & Deenergized Both 4,160-volt Standby Buses.Cause Unknown.Lee 5C Turbine Placed on-line to Sys Grid. Investigation Continuing ML20081K0951983-11-0101 November 1983 Ro:On 831015-16,w/Unit 1 Out of Svc,Standby Bus 2 Deenergized to Allow Operability Verification of Underground Emergency Power Path in Accordance W/Tech Specs.On 831015, CT-3 Underwent Lockout.Caused by Bad Insulators ML20078P8841983-10-31031 October 1983 Ro:On 831026,w/unit Out of Svc for Maint,Lee Steam Station Gas Turbine Tripped,Deenergizing Both Standby Buses.Cause Not Determined.Redundant Buses Available ML20081B2521983-10-17017 October 1983 Ro:On 831012,standby Buses Deenergized to Allow for Operability Performance Testing of Standby Bus Breakers Per Tech Specs.Testing Caused Degraded Mode Beyond Tech Spec Limit 1997-06-30 Category:TEXT-SAFETY REPORT MONTHYEARML18039A9041999-10-15015 October 1999
[Table view]LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML20206P1501999-01-0505 January 1999 LER 98-S03-00:on 981207,security Officer Discovered Uncontrolled Safeguards Info Drawing.Caused by Failure to Follow Established Procedures & Policies.Drawing Was Controlled by Site Security.With ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20198E6381998-12-17017 December 1998 LER 98-S02-00:on 981130,security Access Was Revoked Due to Falsification of Criminal Record.Individual Was Escorted from Protected Area & Unescorted Access Was Restricted. with ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr 1999-09-30 |
Text
.
.-). -- ..
0 0 4
/
5
-T816P EST JUL 4 75 AA048 DUPLICATE OF TELEPHONED EL4_Mg6 4503 AAB193(1819)(2-018244E185)PD 07/04/75 '1819 ~
ICS IPMMTZZ CSP 3 8038784984 TDMT PICKENS SC 75 07-W4 0619P EST PMS NORMAN MOSELY, DLh
'3 NRC REGION 2 230 PEACHTREE ST NORTHWEST ATLANTA GA 30303 3 AT APPROXIMATELY 0635 7/3/75 XE0 WEE UNIT TWO BECAME INOPERABLE BECAUSE OF GOVERNOR PROBLEMS THE UNIT IS OPERABLE MANUALLY BUT AUTO 3 START UP CAN NOT BE.DONE. A LEE GAS TURBINE COULD NOT BE TIED IN THROUGH A ISOLATED LINE TO SUPPLY AND BUY POWER SHUT DOWN WAS O INITIATE ON OPERATING OCONEE UNIT AT APPROXIMATELY 1845 7/4/75.
COMPLETION OF REPAIRS TO XE0 WEE UNIT IS EXPECTED PRIOR TO 2400 3 7/4/75. INVESTIG ATION INTO LEE UNIT FAILURE CONTINING j, 7 g /g 3 J ED SMITH OCONEE NUCLEAR STATION SENECA SC 29678 Y, d[W *"
[
NNNN ,
3 a=um.>
F 8 1 ,
e
l +- .
.. ~ .