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 Issue dateTitleTopic
PNO-III-94-006, on 940121,licensee Commenced Shutdown of Unit 2 to Repair Steam Leak That Was Discovered in Vicinity of SG 1.Leak Was Repaired 940125 & Plant Has Commenced Startup25 January 1994PNO-III-94-006:on 940121,licensee Commenced Shutdown of Unit 2 to Repair Steam Leak That Was Discovered in Vicinity of SG 1.Leak Was Repaired 940125 & Plant Has Commenced Startup
PNO-III-92-045, on 920908,unit Shut Down Due to High Generator Vibrations.Cause Undetermined.Licensee Will Remove & Inspect Generator Rotor9 September 1992PNO-III-92-045:on 920908,unit Shut Down Due to High Generator Vibrations.Cause Undetermined.Licensee Will Remove & Inspect Generator Rotor
PNO-III-90-049, on 900713,one Person Killed & Three Others Injured When Fatally Injured Worker Touched Live Contact in 4-kV Cabinet.Licensee Declared Unusual Event Under Emergency Plan & Subsequently Terminated13 July 1990PNO-III-90-049:on 900713,one Person Killed & Three Others Injured When Fatally Injured Worker Touched Live Contact in 4-kV Cabinet.Licensee Declared Unusual Event Under Emergency Plan & Subsequently Terminated
PNO-III-90-033, on 900524,licensee Declared Emergency Plan After 765KV Switchyard Breaker Opened Unexpectedly & Control Room Received Rept of Fire & Explosion.Caused by Burning Oil from Crosstie Breaker L.Unit 1 Reduced Power to 62%24 May 1990PNO-III-90-033:on 900524,licensee Declared Emergency Plan After 765KV Switchyard Breaker Opened Unexpectedly & Control Room Received Rept of Fire & Explosion.Caused by Burning Oil from Crosstie Breaker L.Unit 1 Reduced Power to 62%
PNO-III-87-113A, updates Util Evaluation of Defective & Incorrectly Installed Bolts in Facility Containment Access Area.Caused by Use of Improper Cutting & Welding Procedure. Evaluation Continuing3 September 1987PNO-III-87-113A:updates Util Evaluation of Defective & Incorrectly Installed Bolts in Facility Containment Access Area.Caused by Use of Improper Cutting & Welding Procedure. Evaluation Continuing
PNO-III-87-100, on 870723,unusual Event Declared When Contractor Employee Wearing Slightly Contaminated Clothing Taken to Local Hosp.When Clothing Removed,Surveys of Individual & Hosp Showed No Contamination24 July 1987PNO-III-87-100:on 870723,unusual Event Declared When Contractor Employee Wearing Slightly Contaminated Clothing Taken to Local Hosp.When Clothing Removed,Surveys of Individual & Hosp Showed No Contamination
PNO-III-87-098, on 870714,undervoltage on Reactor Coolant Pump Bus Occurred.Caused by Tripping of Unit from 80% Power Due to Voltage Variation.Licensee Decided to Shut Down Unit to Repair Minor Leaks in Reactor Cooling Sys15 July 1987PNO-III-87-098:on 870714,undervoltage on Reactor Coolant Pump Bus Occurred.Caused by Tripping of Unit from 80% Power Due to Voltage Variation.Licensee Decided to Shut Down Unit to Repair Minor Leaks in Reactor Cooling Sys
PNO-III-87-081, on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other Plants11 June 1987PNO-III-87-081:on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other PlantsEarthquake
PNO-III-87-032, on 870302,slow,steady Increase in Primary to Secondary Steam Generator Tube Leakage Monitored.On 870303, Leak Estimated at 0.2 Gpm & Unit Taken Out of Svc.Tube Will Be Repaired & Surveillance & Maint Program Implemented4 March 1987PNO-III-87-032:on 870302,slow,steady Increase in Primary to Secondary Steam Generator Tube Leakage Monitored.On 870303, Leak Estimated at 0.2 Gpm & Unit Taken Out of Svc.Tube Will Be Repaired & Surveillance & Maint Program Implemented
PNO-III-86-130, on 861105,during QA Audit of Contractor, Access Badges Removed Due to Inadequacies W/Screening Program.Employees Not Permitted to Return Until Screening Performed by Independent Organization6 November 1986PNO-III-86-130:on 861105,during QA Audit of Contractor, Access Badges Removed Due to Inadequacies W/Screening Program.Employees Not Permitted to Return Until Screening Performed by Independent Organization
PNO-III-86-096, on 860911,bomb Threat Received at Telephone Switchboard,Stating That Bomb Placed in Training Ctr.Ctr Evacuated & Facility Searched.No Bomb Found.Nrc Info Assessment Team Notified12 September 1986PNO-III-86-096:on 860911,bomb Threat Received at Telephone Switchboard,Stating That Bomb Placed in Training Ctr.Ctr Evacuated & Facility Searched.No Bomb Found.Nrc Info Assessment Team Notified
PNO-III-86-094, on 860910,federal Grand Jury in State of Mi Western District Indicted Util & Jg Del Percio W/Violations of NRC Fire Protection Requirements Occurring from Mar 1981 - Apr 198210 September 1986PNO-III-86-094:on 860910,federal Grand Jury in State of Mi Western District Indicted Util & Jg Del Percio W/Violations of NRC Fire Protection Requirements Occurring from Mar 1981 - Apr 1982
PNO-III-86-072, on 860722,reactor Tripped While Operating at 90% Power.Caused by Workman Error While Attempting to Calibr Stator Cooling Water Pressure Switches.Util Will Proceed to Cold Shutdown for Repairs & Perform Snubber Surveillances23 July 1986PNO-III-86-072:on 860722,reactor Tripped While Operating at 90% Power.Caused by Workman Error While Attempting to Calibr Stator Cooling Water Pressure Switches.Util Will Proceed to Cold Shutdown for Repairs & Perform Snubber Surveillances
PNO-III-86-050, on 860528,at 90% Power,Unit Tripped Following Main Turbine Trip on Overspeed.Caused by Small Leakage in Pressurizer Spray Valve & Letdown Valve.Failure of intermediate-range Detector Under Investigation28 May 1986PNO-III-86-050:on 860528,at 90% Power,Unit Tripped Following Main Turbine Trip on Overspeed.Caused by Small Leakage in Pressurizer Spray Valve & Letdown Valve.Failure of intermediate-range Detector Under Investigation
PNO-III-86-010, on 860201,auxiliary Transformer 2DC on Fire at Bushing Atop Unit.Caused by Trip from 80% Power Due to Main Electrical Fault on Transformer.Repairs & Bus Alignments Evaluated to Facilitate Restart3 February 1986PNO-III-86-010:on 860201,auxiliary Transformer 2DC on Fire at Bushing Atop Unit.Caused by Trip from 80% Power Due to Main Electrical Fault on Transformer.Repairs & Bus Alignments Evaluated to Facilitate Restart
PNO-III-85-099, on 851125,primary Coolant Sys Leaks Noted After Reactor Trip.Most Repairs Completed in Hot Standby. Remaining Leaks,In Two Safety Injection Check Valves & Gasket Flange for Coolant Pump,Scheduled for Cold Repair27 November 1985PNO-III-85-099:on 851125,primary Coolant Sys Leaks Noted After Reactor Trip.Most Repairs Completed in Hot Standby. Remaining Leaks,In Two Safety Injection Check Valves & Gasket Flange for Coolant Pump,Scheduled for Cold Repair
PNO-III-85-093C, on 851106,licensee Submitted Request for Restart Concurrence,Per 851030 Confirmatory Action Ltr.Insp & Testing of Reactor Trip Breakers Completed.Failed Breakers Shipped to Vendors for Testing & Evaluation7 November 1985PNO-III-85-093C:on 851106,licensee Submitted Request for Restart Concurrence,Per 851030 Confirmatory Action Ltr.Insp & Testing of Reactor Trip Breakers Completed.Failed Breakers Shipped to Vendors for Testing & Evaluation
PNO-III-85-093B, on 851029,reactor Trip Breaker & Associated Undervoltage Trip Actuating Device Failed.Breaker Mods Expected to Be Completed on 851105.Elements of Confirmatory Action Ltr Met Except for Cause of Device Failure4 November 1985PNO-III-85-093B:on 851029,reactor Trip Breaker & Associated Undervoltage Trip Actuating Device Failed.Breaker Mods Expected to Be Completed on 851105.Elements of Confirmatory Action Ltr Met Except for Cause of Device Failure
PNO-III-85-093, on 851029,reactor Tripped on Spurious Low Flow Signal in Primary Sys.Unit Will Remain Shut Down Until Licensee Investigation Completed & NRC Concurs W/Findings. Special Insp Team Dispatched.State of Mi Will Be Notified29 October 1985PNO-III-85-093:on 851029,reactor Tripped on Spurious Low Flow Signal in Primary Sys.Unit Will Remain Shut Down Until Licensee Investigation Completed & NRC Concurs W/Findings. Special Insp Team Dispatched.State of Mi Will Be Notified
PNO-III-85-059, on 850716,facility Shut Down to Investigate Increasing primary-to-secondary Sys Leakage in Two Steam Generators.Cause Not Stated.Eddy Current Testing Will Be Performed to Locate & Plug Leaking Tubes16 July 1985PNO-III-85-059:on 850716,facility Shut Down to Investigate Increasing primary-to-secondary Sys Leakage in Two Steam Generators.Cause Not Stated.Eddy Current Testing Will Be Performed to Locate & Plug Leaking Tubes
PNO-III-82-076A, on 820804,stuck Fuel Assembly Freed & Transferred W/O Incident to Spent Fuel Storage Pool.No Release of Radioactivity Evident.Assembly Placed in Normal Storage Location in Spent Fuel Storage5 August 1982PNO-III-82-076A:on 820804,stuck Fuel Assembly Freed & Transferred W/O Incident to Spent Fuel Storage Pool.No Release of Radioactivity Evident.Assembly Placed in Normal Storage Location in Spent Fuel Storage
PNO-III-82-076, on 820804,fuel Assembly Became Wedged in Device Used to Move Assemblies from Vertical to Horizontal Position for Movement Through Fuel Transfer Canal.Caused by Tilting Device in Horizontal Position Instead of Vertical4 August 1982PNO-III-82-076:on 820804,fuel Assembly Became Wedged in Device Used to Move Assemblies from Vertical to Horizontal Position for Movement Through Fuel Transfer Canal.Caused by Tilting Device in Horizontal Position Instead of VerticalFuel cladding
PNO-III-82-073, on 820731,unit Shut Down After Tube Leak Rate of 0.17 Gpm Determined in Steam Generator 2.Licensee Estimates Unit Will Be Down for Several Days for Testing & Leak Location Activities3 August 1982PNO-III-82-073:on 820731,unit Shut Down After Tube Leak Rate of 0.17 Gpm Determined in Steam Generator 2.Licensee Estimates Unit Will Be Down for Several Days for Testing & Leak Location Activities
ML20216J70713 November 1978PNO-78-192:on 781109,Unit 2 Shutdown for Scheduled Maint & Was in Cold Shutdown at Time of fire.Carbon-dioxide & Dry Chemical Fire Extinguishers,Water to Control & Finally Extinguish Fire.State of Mi Notified
ML20248L08313 March 1978PNO-78-044:on 780310,plant Achieved Initial Criticality.Rod Positions & Boron Concentration at Initial Criticality Were in Very Close Agreement W/Predicted Values.Unit 2 Currently in Low Power Physics Testing
ML20207G59118 November 1977PNO-77-205:on 771118,DC Cook Unit 1 Reactor Initiated Shutdown in Compliance with Order Issued by NRR to Imeco & Impco.Suspension of Power Operation of Facility Will Continue Until Qualified Connectors Installed
ML20126D19012 August 1977PNO-77-143:Pacific Pump Co Supplied Facilities W/Production Lot of 40 Pumps Mfg Using Shafts Made of Inferior Matl. Cause Unstated.All Utils W/Pumps Were Notified.Nrc Headquarters Notified on 770812
ML20151U70631 March 1977PNO-77-049:on 770330,allegation of Falsification of QC Records Occurred.Region III Personnel Have Appointment to Meet with Individual on 770407.Individual Unavailable Earlier,Due to Move of ResidenceNondestructive Examination
ML20249B90020 September 1976PNO-76-158:on 760917,util Informed Region III by Telephone That an Industrial Accident Has Resulted in Death by Asphyxiation of One Construction Worker & Hospitalization of Two Other WorkersFatality
ML20249B30611 May 1976PNO-76-085:on 760510,auxiliary Bldg Evacuated as Precautionary Measure for Approx 1 H Due to Leakage of Rc Water from Rc Filter Drain Valve.Region 3 Radiation Protection Specialist Conducting Routine Insp
ML20236W9494 December 1975PN-75-144:on 751204,oil in Oil Bath Air Cleaner for Diesel Generator Cd Was Accidentally Ignited.Plant Personnel Extinguished Fire Before Fire Department Arrived.No Injuries to Personnel & No Damage to Facility Resulted