Semantic search
Jump to navigation
Jump to search
Issue date | Title | Topic | |
---|---|---|---|
ML20210P605 | 28 July 1999 | Rev 1 to Engineering Calculation E4C-098, 4 Kv Switchgear Protective Relay Setting Calculation | |
ML20204H146 | 11 March 1999 | Rev 0 to C-NOME-CALC-0107, Seismic Qualification of Hot Leg Rtd,Hot Leg Pdt & Hot Leg Sampling Mnsa Hardware | |
ML20204H182 | 10 March 1999 | Rev 0 to C-PENG-CALC-021, Determination of Waterford 3 Hot Leg Seismic Response Spectra & Accelerations for Use in Analyses of Mnsas | Safe Shutdown Earthquake Operating Basis Earthquake |
ML20206R497 | 2 November 1998 | Calculation Change Notice CNN-3,Rev 3 to Calculation M-0050-017, BTP Rsb 5-1 Condensate Inventory | |
ML20195K436 | 13 October 1998 | Rev 0 to J-SPA-269, ESFAS Radiation Monitoring Single Failure Analysis | Pressure Boundary Leakage |
ML20198T133 | 24 September 1998 | Calculation Change Notice 1,Rev 00 to J-SAB-023, Dnb/Lpd/Log Power Trip Bypass | |
ML20206R292 | 4 August 1998 | Calculation Change Notice CCN-2 to Rev 2 to Calculation M-0050-0917, BTP Rsb 5-1 Condensate Inventory | Safe Shutdown Boric Acid Loop seal Packing leak Tornado Missile Anchor Darling Operating Basis Earthquake Design basis earthquake Earthquake |
ML20204H214 | 10 February 1998 | Rev 0 to S2-NOME-CALC-0085, Seismic Qualification of SG Pdt,Hot Leg Pdt & Hot Leg Sampling Mnsa Hardware | |
ML20249C800 | 5 February 1998 | Rev 1 to Calculation EC-M96-002, Carbon Dioxide Generator/ Oxygen Depletion in Cr | |
ML20204H171 | 3 February 1998 | Rev 0 to S-PENG-CALC-008, Nozzle Loads for Which SONGS Bottom Mounted Pzr Mnsa Was Qualified | |
ML20217J977 | 21 August 1997 | Rev 0 to N-0720-014, Control Room & Offsite Doses Should Cpis,Cris & Fhis Fail | Stroke time |
ML20141G703 | 5 July 1997 | Revision B to Required Submergence to Prevent Vortexing in Csp | |
ML20217J959 | 12 June 1997 | Rev 0 to J-SPA-289, ESFAS Radiation Monitor Software Common Mode Failure Evaluation | Pressure Boundary Leakage |
ML20148G645 | 7 May 1997 | Rev 1 to Minimum Pipe Submergence to Prevent Vortexing Calculation | Boric Acid |
ML20147G178 | 29 January 1997 | Water Hammer Analysis:Lpsi 'B' | |
ML20113C514 | 18 June 1996 | Operator Action Summary Data Sheet & Post-Initiator Human Error Probability Calculation Worksheet HRA Worksheet 1 | High Radiation Area |
ML20113C519 | 18 June 1996 | Operator Action Summary Data Sheet & Post-Initiator Human Error Probability Calculation Worksheet HRA Worksheet 5 | |
ML20115G357 | 8 June 1996 | Rev 4 to N-0480-003, Fuel Transfer Tube Shielding | |
ML20115G354 | 28 May 1996 | Rev 0 to M-DSC-330, Thermal Analysis of Spent Fuel Transfer Tube | |
ML20095G870 | 14 December 1995 | Relative Humidity at Charcoal Beds (E-418 & 419),no Heating | |
ML20095G873 | 14 December 1995 | Evaporation Time of Entrapped Air Moisture in E-419 | |
ML20148G637 | 1 December 1995 | Rev 0 to Minimum Pipe Submergence to Prevent Vortexing Calculation | |
ML20112D041 | 26 September 1995 | Containment Spray (CS) & Emergency Cooling Unit (Ecu) Actuation Times | Stroke time |
ML20086J690 | 25 June 1995 | Vol Control Tank to 77 to Charging Pump Suction | Boric Acid Nondestructive Examination |
ML20112D052 | 22 March 1995 | Containment P/T Analysis for Design Basis MSLB - Suppl B | |
ML20112D049 | 17 February 1995 | Containment P/T Analysis for Design Basis LOCA - Suppl a | Ultimate heat sink Stroke time Fuel cladding |
ML20129E830 | 6 February 1995 | Rev 2 to Evaluation of Spent Fuel Pool for W High Density Racks | |
ML20078D695 | 12 January 1995 | 4 Kv SWGR Protective Relay Setting Calculation | |
ML20112D038 | 27 October 1994 | Sys Dynamic Voltages During Design Basis Accident | |
ML20070A636 | 27 May 1994 | Rev 1 to Revised P-T Curves for 20EFPY,SONGS 2 & 3 | |
ML20129E820 | 2 May 1994 | Rev 2 to Evaluation of Spent Fuel Pool for Westinghouse High Density Racks | |
ML20078F576 | 14 March 1994 | Fuel Handling Accident Inside Containment CR & Offsite Doses | Stroke time |
ML20086K565 | 10 February 1994 | Calculation J-SEA-012, Ni Subchannel Amplifier,Analysis of Calibration Data | Grace period |
ML20086K557 | 8 February 1994 | Suppl A,Calculation Change Notice 1 to Rev 0 to J-SBA-001, Plant Protection Sys Bistable Drift | |
ML20086K541 | 3 November 1993 | Rps/Esfas Extended Test Interval Evaluation for 120 Days Staggered Testing at SONGS Units 2 & 3 | Probabilistic Risk Assessment Fuel cladding Power change |
ML20100Q623 | 12 October 1993 | SONGS 3 Primary Plant Makeup Storage Tank Upgrade | Hydrostatic Operating Basis Earthquake Finite Element Analysis Design basis earthquake Code Reconciliation Earthquake Weak link |
ML20100Q612 | 5 October 1993 | SONGS 2 Primary Plant Make-Up Storage Tank Upgrade | Hydrostatic Operating Basis Earthquake Finite Element Analysis Design basis earthquake Code Reconciliation B.5.b Mitigating Strategies Earthquake Weak link |
ML20086B466 | 20 August 1993 | Control Room Outside Air Intake Radiation Monitor Setpoint Calculation | |
ML20078D682 | 16 August 1993 | Sys Dynamic Voltages During Design Basis Accident | |
ML20078D689 | 16 August 1993 | Auxiliary Sys Voltage Regulation | |
ML20128H918 | 20 January 1993 | Rev 1 to M-73-116, Room Temp Response During Station Blackout | |
ML20086D191 | 8 November 1991 | Calculation M-DSC-250, Stress Evaluation of Unit 3 Reactor Coolant Pump Flywheel | Coast down |
ML20082T184 | 21 May 1990 | Rev 1 to Room Temp Response During Station Blackout | Emergency Lighting |
ML20062A311 | 9 May 1990 | Suppl B to Calculation DC-2836, Auxiliary Feedwater Flow Venturi Sizing | |
ML20082T180 | 17 August 1989 | Rev 0 to 125 Volt Battery DC Sys Sizing | |
ML20094F352 | 15 March 1988 | Calculation CENC-1805, Waterford Unit 3 Steam Generator Manways |