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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20153A9941998-09-16016 September 1998 Safety Evaluation Denying Request to Remove Missile Shields from Plant Design ML20151U8821998-09-0808 September 1998 SER on Revised Emergency Action Levels for Gpu Nuclear,Inc, Three Mile Island Nuclear Plant Units 1 & 2 ML20237A8331998-08-12012 August 1998 Safety Evaluation Accepting USI A-46 Program Implementation at Plant,Unit 1 ML20217K4851998-04-24024 April 1998 Safety Evaluation Supporting Amend 207 to License DPR-50 ML20199G8371998-01-22022 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Three Mile Island Nuclear Station,Unit 1 ML20198K2281997-10-16016 October 1997 Safety Evaluation Supporting Amend 206 to License DPR-50 ML20211G8561997-10-0202 October 1997 Safety Evaluation Supporting Amend 204 to License DPR-50 ML20210Q9991997-08-28028 August 1997 Safety Evaluation Concluding That Since 25th Tendon Surveillance on Few Yrs Away,Adequacy of Remaining Prestressing Force Will Be Critical to Verify ML20217Q7341997-08-27027 August 1997 Safety Evaluation Supporting Amend 203 to License DPR-50 ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20149D2671997-07-11011 July 1997 SER Concluding That Exemption from Listed Fire Areas Should Be Granted & Exemption from Fire Area FH-FZ-5 Should Be Denied ML20138H6671996-12-19019 December 1996 Safety Evaluation Accepting Util IPE Submittal in Response to GL 88-20 ML20134D7811996-10-24024 October 1996 Safety Evaluation Supporting Amend 51 to License DPR-73 ML20128L6741996-10-11011 October 1996 Safety Evaluation Accepting Third ten-year Interval for Pump & Valve Inservice Testing Program for Facility ML20128K1981996-10-0808 October 1996 Safety Evaluation Supporting Amend 50 to License DPR-73 ML20094Q0301995-11-24024 November 1995 Safety Evaluation Supporting Amend 199 to License DPR-50 ML20092N2551995-10-0202 October 1995 Safety Evaluation Supporting Amend 197 to License DPR-50 ML20087G5771995-08-14014 August 1995 Safety Evaluation Supporting Amend 195 to License DPR-50 ML20086R7421995-07-24024 July 1995 Safety Evaluation Supporting Amend 194 to License DPR-50 ML20077C2901994-11-28028 November 1994 Safety Evaluation Supporting Amend 192 to License DPR-50 ML20071N3991994-08-0101 August 1994 Safety Evaluation Supporting Amend 191 to License DPR-50 ML20071K8921994-07-25025 July 1994 Safety Evaluation Supporting Amend 188 to License DPR-50 ML20071L2381994-07-25025 July 1994 Safety Evaluation Supporting Amend 189 to License DPR-50 ML20071K8741994-07-25025 July 1994 Safety Evaluation Supporting Amend 190 to License DPR-50 ML20070H2851994-07-14014 July 1994 Safety Evaluation Supporting Amend 187 to License DPR-50 ML20073S3941994-05-23023 May 1994 Safety Evaluation Supporting Amend 184 to License DPR-50 ML20059D1771993-12-28028 December 1993 Safety Evaluation Supporting Amend 48 to License DPR-73 ML20062M2481993-12-21021 December 1993 Safety Evaluation Supporting Amend 180 to License DPR-50 ML20062K1041993-12-0606 December 1993 Safety Evaluation Supporting Amend 47 to License DPR-73 ML20058F0311993-11-16016 November 1993 SE Informing That Changes to Pdms Requirements & Commitments List of 930115,does Not Constitute Unreviewed Safety Question,Nor Do They Involve Significant Hazard or an Environmental Impact ML20059K3001993-11-0808 November 1993 Safety Evaluation Supporting Amend 46 to License DPR-73 ML20057A8321993-09-10010 September 1993 Safety Evaluation Supporting Amend 178 to License DPR-50 ML20057A3641993-09-0101 September 1993 SER Denying Licensee 930216 & 0416 Requests for Relief from Certain Requirements of ISI Program ML20056F0171993-08-0505 August 1993 Safety Evaluation Accepting Proposed Changes to Pdms Requirements & Commitments List of 930115 ML20128P7321993-02-19019 February 1993 Safety Evaluation Supporting Amend 171 to License DPR-50 ML20128K0771993-02-11011 February 1993 Safety Evaluation Supporting Amend 169 to License DPR-50 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
05000289/LER-1998-009-01, :on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised1998-09-18018 September 1998
- on 980820,discovered Potential Loss of HPI During Postulated Loca.Caused by Misapplication or Interpretation of Design Inputs.Revised OL Was Implemented & Mut Pressure & Level Limits Analysis Revised
1999-09-30
[Table view] |
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UNITED STATES f;
j NUCLEAR REGULATORY COMMISSION y
WASmNGTON. D C 20555
%.a....f SAFETv EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.151 TO FACILITY OPERATING i.ICENSE NO. DPR-50 METROPOLITAN EDISON COMPANY JERSEY CENTPAL POWER & LIGHT COMPANY PENN5YLVANIA ELECTRIC COMPANY GPU NUCLEAR CORPORATION THREE MILE ISLAND NUCLEAR STATION. UNIT NO. 1 DOCKET NO. 50-289, INTRODUCTION
.GPU Nuclear Corporation (GPU' submitted Technical Specification Change Request (TSCR) No. 191 by letter dated June 13, 1989. The amendment requested by this TSCR would remove Section a.4.1.2.1, Scope of Testing, from the Technical Specifications (TS) anc relocate the listing of containment penetration components and valves requiring type "B" and "C" leak rate testing to the Updated Final Safety Analysis Report (USAR). The request also included changes to these lists resulting from modifications to the facility and reevaluation of 10 CFR 50, Appendix J requirements as well as various other editorial changes.
Finally, the TSCR requested removal, from the TS, of a periodic surveillance regarding the Penetration Pressurization System.
EVALUATION The operability of containment isolation valves and leak integrity of containment penetration components ensure that the containment atmosphere will be isolated from the outside environment in the event of a release of radioactive material to the containment atmosphere or pressurization of the containment.
To ensure operability and integrity of this hardware, Appendix J requires periodic leak testing of three different types: type A for overall containment integrated leakage, type 8 for various types of containment penetrations and type C for containment isolation valve leakage. Presently the specific components requiring type B and C leak tests are specifically listed in TS Section 4.4.1.2.5.
Each time the content of this list changes due to facility modifications or regulation interpretation a formal amendment to the facility operating license is required. GPU has proposed removal of the list from the TS and incorporating it in the USAR as Table 5.7-2 (type B testing) and Table 5.7-3 (type C testing).
Final draft copies of these tables were included with the TSCR.
8909110083 890831 E;DR ADOCK 05000289 F
PDC
i 3 s The Commission's Interim policy Statement on Technical Specification Improvements recognized the advantages of improved TS and endorsed the recommendations of the nuclear industry and the NRC staff for a program to develop improvements in TS. An important part of that program is the implementation of line-item improvements in TS. This change has been implemented in the TS for new licenses and is consistent with previous guidance provided by Generic Letter 84-13 on removing the list of snubbers from TS. Guidance to licensees regarding removal of this list from TS will be provided to all power reactor licensees in a future generic letter based on issuance of a similar amendment for Crystal River Unit 3 in May 1989. Relocation of the listing of components requiring Appendix J type B cnd C leak testing would allow future changes to be made without a license amendment. This would relieve both the NRC and the licensee of an administrative burden but would not change any requirements to perform Appendix J leak testing. Maintaining the table in the USAR would also ensure that the information is still available to the operators. Changes to the table would be controlled under 10 CFR 50.59 as a change to the facility. Therefore, adequate measures exist to control changes to the facility without having these components listed in the TS. Due to the proposed relocation of Section 4.4.1.2.5 from the TS to the USAR, references to the section would be deleted from TS 4.4.1.2.3.
The TSCR also discusses three changes to the local leak rate test listing itself. The first is moving containment purge valves AH-VIA/B/C/D from the type B list to the type C list. Type B test requirements apply to containment penetrations whose design incorporates resilient seals, airlock doors, and doors with resilient seals or gaskets.
In accordance with 10 CFR 50 Appendix J, the type C test is clearly specified to apply to valves such as AH-VIA/B/C/D that " provide a direct connection between the inside and outside atmospheres of the primary reactor containment under normal operations, such as purge and ventilation,... valves." Apparently, because the design of the purge valves incorporates the use of resilient seals, these valves were inappropriately included in the original TMI-1 Technical Specifications as type B components.
The purge valves were the only valves included in the list of type B components.
Special tests and inspections of the purge valves would continue to exceed the Appendix J test requirements for containment isolation valve type C tests.
Moving the purge valves from the list of valves requiring a type B test to the type C list could result in a change in purge valve test requirements in that it would no longer be required to test the valves prior to startup if opened following a type A or B test if the startup were to occur less than 92 days since the last test. The existing special tests of the purge valves each kS!E [ deSNcki$ k N e'0akve* h! b $g ab!O $n En N op$fa0$ N Iy* lbe"skaN agrees with this change. A resultant editorial change to TS 4.4.1.2.5.c is required to reflect the appropriate Appendix J section (III.D.3).
. x
}
e e The second change to the local leak rate test listing is deletion of valve LR-V10 from the type C list. LR-V10 has been included in the list of valves requiring a type C test ever since the original TMI-1 Technical Specifications was issued even though such a test is not needed in meeting the Local Leakage Rate test requirements of 10 CFR 50 Appendix J.
LR-V10 is a manual handwheel operated test connection valve between containment isolation valve LR-V49 and a containment isolation blind flange associated with containment penetration
- 417. LR-V10 has a blind flange installed at its outlet resulting in double manual isolation of the test connection. Therefore LR-V10 should be deleted from the list of vlaves requiring a type C test. The staff agrees with this change m The third change to the listing is addition of valves PP-V210, 211, 212 and 213 to the list of type C valves to be tested. During a recent modification, these globe valves were added to the facility to replace four check valves in the Penetration Pressurization System. The staff agrees with this change.
The TSCR also requested deletion of TS 4.4.1.2.5.e which provides for quarterly monitoring of the Penetration Pressurization System. The TSCR stated that this system is not required by Appendix J or any codes and that the TMI-1 safety analysis takes no credit for the active function of this system. The system, in fact, is disabled during the Appendix J type A containment integrated leak rate test. The staff notes, however, that this system interconnects with the instrument air system. The original purpose for the Penetration Pressurization System and related surveillance tests would have been to permit a reduced leak rate test program or justify exemptions from the 10 CFR 50 Appendix J.
- However, all containment penetrations with resilient seals, process system flanges, valves, and gaskets requiring periodic leak test per Appendix J are now tested using Type B or C tests with no credit or exemptions for the use of a fluid blocking system.
The apparent purpose of TS 4.4.1.2.5.e is to detect abnormal leakage in the Penetration Pressurization System. Since credit is not taken for this system the staff agrees that this surveillance serves no useful purpose. The staff reviewed the possible detrimental effects this system may have on the instrument air system should a major rupture occur in the system, thereby potentially causing depletion of instrument air. We concluded that the possibility of this occurrence is very remote in light of existing low pressure alarms, the ability to isolate the system and recent instrument air system enhancements under the Safety Performance Improvement Program. We therefore conclude that deletion of this TS is appropriate and has no detrimental effect on plant operation.
SUMMARY
The staff finds that the requested changes will maintain conservative limiting conditions for plant operation and adequate surveillance requirements. Thus, the staff finds the proposed changes to be acceptable.
L.7
_J*
. ENVIRONMENTAL CONSIDERATION
'The amendment changes a requirement with respect to installation or use of l
a facility component located within the restricted area as defined in 10 CFR Part 2, and also relates to changes in recordkeeping, reporting or administrative l'
procedures or requirements. We have determined that the amendment involves no significant increase in the amounts and no significant change in the types of any effluents that may be released off site, and that there is no significant increase in individual or cumulative occupational exposure. The staff has previously issued a proposed finding that this the amendment involves no significant hazards consideration, and there has been no public comment on such finding. Accordingly, the amendment meets the eli exclusion set forth in 10 CFR 51.22(c)(9) and (10)gibility criteria for categorical Pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be prepared in connection with the issuance of this amendment.
CONCLUSION We have concluded, based on the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance
-of this emendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor: Ronald L Hernan Dated:
August 31, 1989 i
m