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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML20210M5901999-08-0505 August 1999 Rev 1 to License Change Application 247,dtd 990310,for Amend to License NPF-1,adding License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan. with Certificate of Svc ML20196L1311999-05-24024 May 1999 Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Operating Ownership of Pacificorp ML20207J3801999-03-10010 March 1999 Application for Amend to License NPF-1,adding License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan ML20198T1851999-01-0707 January 1999 Rev 3 to License Change Application 237 Re Spent Fuel Cask Loading in Fuel Bldg ML20198T1451999-01-0707 January 1999 Rev 3 to License Change Application 237 to License NPF-1, Inserting New License Condition to Authorize Loading of Spent Fuel & Other Matls Into Transtor Transfer & Storage Casks in Fuel Bldg ML20238E8261998-08-27027 August 1998 Application for Amend to License NPF-1,deleting Number of License Conditions & TS Requirements as Prerequisite to Implementing Requested Amend to Transfer of Nuclear Sf from Existing 10CFR50 Licensed Area to Proposed 10CFR72 ISFSI ML20199J5641998-01-29029 January 1998 Application for Amends to License NPF-1,deleting Security Plan Requirements of 10CFR50.54(p) & Part 73 for Trojan Plant After Spent Nuclear Fuel Is Moved to Proposed ISFSI Area ML20134C9781997-01-28028 January 1997 Application for Amend to License NPF-1,requesting to Clarify Controls That Will Be Used for Rev & Maint of Certified Fuel Handler Training Program ML20134A9531997-01-16016 January 1997 Application for Amend to License NPF-1,requesting Deletion of Paragaph 2.(C)(7) to Allow pre-operational Testing & Load Handling of Spent Fuel Transfer & Storage Casks in Trojan Fuel Bldg ML20134B7841997-01-16016 January 1997 License Change Application (Lca) 240 to License NPF-1.LCA Proposes to Delete Paragraph 2.(C)(7) to Allow Loading & Handling of Spent Fuel Casks in Trojan Fuel Bldg as Described in 10CFR72 License Application Submitted Mar 1996 ML20129E4751996-10-23023 October 1996 Application for Amend to License NPF-1,requesting Addition to Paragraph 2.(C)(8) to Allow Processing & Handling of Spent Fuel Pool Debris ML20059A5431993-10-21021 October 1993 Application for Amend to License NPF-1 to Modify Security License Condition for Clarity & Minimize Burden Associated W/Processing Application to Reflect Current Security Plan Rev ML20127P1691993-01-27027 January 1993 License Change Application 229 to License NPF-1,modifying OL to possession-only License to Allow Util to Possess SNM But Not Operate Nuclear reactor.Marked-up License NPF-1 Encl ML20127P2031993-01-27027 January 1993 License Change Application 230 to License NPF-1,revising Facility Staffing & Training Requirements in Light of Transition of Facility to Permanently Defueled Status ML20127M6361992-11-26026 November 1992 License Change Application 227 to License NPF-1,revising TS to Defer Unscheduled SG ISI Required by TS 4.4.5.3.c.1 Following primary-to-secondary Tube Leakage in Excess of TS Limits ML20141M1881992-03-27027 March 1992 Rev 1 to License Change Application 186 to License NPF-1, Changing TS 4.0.3 to Negatively State Failure to Perform Required Surveillances on Schedule Constitutes Noncompliance W/Operability Requirements of Lco,Per Generic Ltr 87-09 ML20059L6681990-09-21021 September 1990 Application for Amend to License NPF-1,consisting of License Change Application 203,Rev 1.Rev Reduces Scope of Previous Changes Re Tech Spec Table 3.6-1, Containment Isolation Valves ML20247C8771989-07-19019 July 1989 Application for Amend to License NPF-1 Consisting of License Change Application 179.Amend Changes Description of Turbine Steam Supply Valves in Tech Spec Table 3.6-1 from motor-operated to air-operated ML20246A7491989-06-30030 June 1989 Application for Amend to License NPF-1,consisting of License Change Application 182,reflecting Reorganization of Util Nuclear Div.Certificate of Svc & Description of Change Encl ML20244E6111989-06-12012 June 1989 Application for Amend to License NPF-1,changing Orifice Size of Steam Line Safety Valves Shown in Tech Spec Table 4.7-1, Steam Line Safety Valves Per Loop ML20235L9421989-02-10010 February 1989 Application for Amend to License NPF-1,consisting of License Change Application 174.Amend Revises Tech Specs to Allow Mods to Control Auxiliary Fuel Bldg Complex Resulting in Increase in Lateral Shear Forces of Any Story ML20235Q9101989-02-10010 February 1989 Application for Amend to License NPF-1,consisting of License Change Application 173,clarifying Surveillance Requirements for Containment Equipment Hatch ML20154D1681988-09-0909 September 1988 Application for Amend to License NPF-1,revising Tech Specs Re Setpoint for Pressurizer LPSI Ressure Safety Injection Necessary to Accommodate New Instrumentation ML20151T4991988-08-12012 August 1988 Application to Amend License NPF-1,consisting of License Change Application 169,revising Tech Specs Surveillance Requirements for ECCS Check Valves ML20151A0351988-07-0808 July 1988 Application for Amend to License NPF-1,incorporating Miscellaneous Editorial Corrections & Clarifications ML20148C2061988-03-18018 March 1988 Application for Amend to License NPF-1,consisting of License Change Application 162,Rev 2,revising Tech Specs Re Offsite & Facility Organization Charts ML20147E7291988-03-0101 March 1988 Application for Amend to License NPF-1,consisting of Rev 1 to License Change Application 124,revising Tech Specs Re Containment Isolation Valves ML20196J8861988-03-0101 March 1988 License Change Application 165 Requesting Amend to License NPF-1,modifying Tech Specs by Removing 3.5% U-235 Limit on Reactor Fuel Assemblies & Increase Enrichment Limit for New Fuel Storage Racks to 4.5% ML20149K1401988-02-17017 February 1988 Application for Amend to License NPF-1,consisting of License Change Application 163,revising Tech Specs to Add New Instruments for Monitoring Steam Generator Blowdown Sys Liquid Effluent Radioactivity & Flow Rate ML20149L6891988-02-15015 February 1988 Application for Amend to License NPF-1,consisting of Rev 1 to License Application 162,revising Offsite & Facility Organization Charts.Description of Requested Changes Encl ML20149H0921988-02-0404 February 1988 Application for Amend to License NPF-1,consisting of License Change Application 164.Amend Revises Operability & Surveillance Requirements & Bases for Component Cooling Water Sys ML20147D4431988-01-15015 January 1988 Application for Amend to License NPF-l Consisting of License Change Application 162,revising Offsite & Facility Organization Charts ML20195H8801987-12-24024 December 1987 Application for Amend to License NPF-1,consisting of License Change Application 151,removing Portions of Tech Specs Re Fire Protection & Relocating Them to Vol 1 to PGE-1012, Trojan Nuclear Plant Fire Protection Plan.. ML20237D6801987-12-18018 December 1987 Application for Amend to License NPF-1 Consisting of License Change Application 160,changing Tech Specs to Delete Requirement for Obtaining source-range Nuclear Instrument Detector Plateau Curves ML20237D6471987-12-16016 December 1987 Application for Amend to License NPF-1 Consisting of Rev 1 to License Change Application 154,to Correct Tech Specs Section 3/4.4.6.2 for Agreement W/Definition of Pressure Boundary Leakage ML20236W7391987-11-20020 November 1987 License Change Application 161 for Amend to License NPF-1, Revising Tech Specs to Include Effects of Nuclear Fuel Design Changes ML20236Q2191987-11-16016 November 1987 Application for Amend to License NPF-1,consisting of Rev 1 to License Change Application 142,resolving Control Room Habitability Issues by Changing Tech Spec Sections Re Chlorine Detection Sys & Control Emergency Ventilation Sys ML20236P4371987-11-13013 November 1987 Application for Amend to License NPF-1,consisting of License Change Application 153,revising Tech Specs to Extend Surveillance Time Period for Verifying Control Rod Insertability from 24 H to 7 Days ML20236N3821987-11-0909 November 1987 Application for Amend to License NPF-1,consisting of License Change Application 159,revising Tech Spec 3.9.9 to Resolve Inconsistencies within Tech Specs ML20236N5761987-08-0606 August 1987 Application for Amend to License NPF-1,consisting of License Change Application 154,correcting Tech Spec Section, Bases for Agreement W/Definition of Pressure Boundary Leakage ML20235W5301987-07-14014 July 1987 Application for Amend to License NPF-1,consisting of License Change Application 155 Re Solid Radwaste Sys ML20215K8131987-06-22022 June 1987 Application for Amend to License NPF-1,consisting of License Change Application 132,revising Operability Requirements for Reactor Trip Breakers & Surveillance Requirements for Manual Reactor Trip & Breakers ML20210B5801987-04-29029 April 1987 Application for Amend to License NPF-1,consisting of License Change Application 156,revising Tech Specs to Correct Typos & to Clarify Appropriate Process Used for Review & Approval of Temporary Changes to Procedures ML20209D0031987-04-20020 April 1987 Supplemental Application for Amend to License NPF-1, Incorporating License Change Application 152 Re Unneccessary Plugging of Steam Generator Tubes Which Increases Personnel Exposure & Reduces RCS Flow ML20212E2321987-02-26026 February 1987 Application for Amend to License NPF-1,consisting of Revised Pages for License Change Application 124 & License Change Application 135,adding Steamline Isolation Valves & Valve CV-8825 Back Onto Tech Spec Table 3.6-1 ML20211N9551987-02-20020 February 1987 Application to Amend License NPF-1,revising Steam Generator Tube Plugging Criteria in Tube Sheet Region.Fee Paid ML20211H3791987-02-11011 February 1987 License Change Application for Amend to License NPF-1, Increasing Setpoint Tolerance for Pressurizer & Main Steam Safety Valves from 1% to 2% ML20207Q5341987-01-20020 January 1987 Application to Amend License NPF-1,incorporating License Change Application 150 to Revise Surveillance Requirements for Safety Injection Sys Accumulator Isolation Valves. Description of Change Encl ML20207M5741987-01-0909 January 1987 Application for Amend to License NPF-1,consisting of Rev 1 to License Change Application 134,revising Min Contained Vol of Water Required in Condensate Storage Tank ML20215D2431986-12-12012 December 1986 Application for Amend to License NPF-1,consisting of License Change Application 127,separating Surveillance Requirement 4.7.3.1.c Into 4.7.3.1.c & 4.7.3.1.d & Listing Four Component Cooling Water Valves W/Modified Closure Signals 1999-08-05
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML20210M5901999-08-0505 August 1999 Rev 1 to License Change Application 247,dtd 990310,for Amend to License NPF-1,adding License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan. with Certificate of Svc ML20196L1311999-05-24024 May 1999 Application for Amend to License NPF-1 for Indirect Transfer of License,To Extent That Such Approval Required Solely to Reflect Change in Upstream Operating Ownership of Pacificorp ML20206H4411999-05-0505 May 1999 Amend 201 to License NPF-1,revising PDTSs by Deleting ISFSI Area,Changes Also Revise TSs by Revising Subsection 4.1.1 & Replacing Existing Figure 4.1-1 with New Figure 4.1-1 & Adding New Page to Figure 4.1-1 as Listed ML20206C9701999-04-23023 April 1999 Amend 200 to License NPF-1,changes License by Revising License Condition 2.C.(10), Loading of Fuel Into Casks in Fuel Building ML20206C9301999-04-23023 April 1999 Amend 199 to License NPF-1,changes License NPF-1 by Adding New License Condition Entitled, Loading of Fuel Into Casks in Fuel Building ML20207J3801999-03-10010 March 1999 Application for Amend to License NPF-1,adding License Condition Denoting NRC Approval of PGE-1078, Trojan Nuclear Plant License Termination Plan ML20198T1851999-01-0707 January 1999 Rev 3 to License Change Application 237 Re Spent Fuel Cask Loading in Fuel Bldg ML20198T1451999-01-0707 January 1999 Rev 3 to License Change Application 237 to License NPF-1, Inserting New License Condition to Authorize Loading of Spent Fuel & Other Matls Into Transtor Transfer & Storage Casks in Fuel Bldg ML20238E8261998-08-27027 August 1998 Application for Amend to License NPF-1,deleting Number of License Conditions & TS Requirements as Prerequisite to Implementing Requested Amend to Transfer of Nuclear Sf from Existing 10CFR50 Licensed Area to Proposed 10CFR72 ISFSI ML20199J5641998-01-29029 January 1998 Application for Amends to License NPF-1,deleting Security Plan Requirements of 10CFR50.54(p) & Part 73 for Trojan Plant After Spent Nuclear Fuel Is Moved to Proposed ISFSI Area ML20148K3491997-06-0909 June 1997 Amend 198 to License NPF-1,revising possession-only License to Add Sf Debris in Plant Fuel Bldg ML20148D2551997-05-23023 May 1997 Amend 197 to License NPF-1,revising Permanently Defueled TS to Delete Requirement for NRC Prior Approval of Changes to Certified Fuel Handler Training Program ML20141H3031997-05-19019 May 1997 Amend 196 to License NPF-1,revising License to Delete Prohibition on Moving Spent Fuel Assembly Shipping Cask Into Fuel Building ML20137K5521997-03-31031 March 1997 Application for Coc 9271,requesting Approval to Allow one- Time Shipment of Trojan Rv Package as Type B Exclusively for Radioactive Matl Transportation Package ML20134C9781997-01-28028 January 1997 Application for Amend to License NPF-1,requesting to Clarify Controls That Will Be Used for Rev & Maint of Certified Fuel Handler Training Program ML20134B7841997-01-16016 January 1997 License Change Application (Lca) 240 to License NPF-1.LCA Proposes to Delete Paragraph 2.(C)(7) to Allow Loading & Handling of Spent Fuel Casks in Trojan Fuel Bldg as Described in 10CFR72 License Application Submitted Mar 1996 ML20134B5761997-01-16016 January 1997 Application for Amend to License NPF-1,deleting Paragraph 2.(C)(7) to Allow Loading & Handling of Spent Fuel Casks & Insertion of New License Condition Authorizing Loading of Spent Fuel & Other Matls in Fuel Building ML20134A9531997-01-16016 January 1997 Application for Amend to License NPF-1,requesting Deletion of Paragaph 2.(C)(7) to Allow pre-operational Testing & Load Handling of Spent Fuel Transfer & Storage Casks in Trojan Fuel Bldg ML20134F1061996-10-31031 October 1996 Amend 195 to License NPF-1,revising Section 5.0,ACs,of Plant Permanently Defueled Tss,App A,To Reflect Organization Changes of Licensee,As They Apply to Oversight & Mgt of Plant ML20129E4751996-10-23023 October 1996 Application for Amend to License NPF-1,requesting Addition to Paragraph 2.(C)(8) to Allow Processing & Handling of Spent Fuel Pool Debris ML20058K1281993-12-0606 December 1993 Amend 193 to License NPF-1,relocating RETS to ODCM & PCP in Accordance W/Gl 89-01 & Changing Required Frequency for Submittal of Radioactive Effluent Release Rept from Semiannual to Annual ML20059A5431993-10-21021 October 1993 Application for Amend to License NPF-1 to Modify Security License Condition for Clarity & Minimize Burden Associated W/Processing Application to Reflect Current Security Plan Rev ML20057D0771993-09-22022 September 1993 Amend 192 to License NPF-1,relocating Portions of Plant TS Re Plant Fire Protection Program from TS to Topical Rept PGE-1012 ML20128K1001993-02-11011 February 1993 Corrected TS Page 3/4 3-49a to Amend 189 to License NPF-1, Reflecting Correct Spelling of Kziu in Items 4.c & 6.c ML20127P2031993-01-27027 January 1993 License Change Application 230 to License NPF-1,revising Facility Staffing & Training Requirements in Light of Transition of Facility to Permanently Defueled Status ML20127P1691993-01-27027 January 1993 License Change Application 229 to License NPF-1,modifying OL to possession-only License to Allow Util to Possess SNM But Not Operate Nuclear reactor.Marked-up License NPF-1 Encl ML20127P5741993-01-26026 January 1993 Amend 189 to License NPF-1,revising Plant TS 3/4.3.3.7, Fire Protection Instrumentation ML20125B8031992-12-0404 December 1992 Amend 188 to License NPF-1,deleting License Condition 2.C.(11) Re Fuel Assemblies ML20127M6361992-11-26026 November 1992 License Change Application 227 to License NPF-1,revising TS to Defer Unscheduled SG ISI Required by TS 4.4.5.3.c.1 Following primary-to-secondary Tube Leakage in Excess of TS Limits ML20141M1881992-03-27027 March 1992 Rev 1 to License Change Application 186 to License NPF-1, Changing TS 4.0.3 to Negatively State Failure to Perform Required Surveillances on Schedule Constitutes Noncompliance W/Operability Requirements of Lco,Per Generic Ltr 87-09 ML20059L6681990-09-21021 September 1990 Application for Amend to License NPF-1,consisting of License Change Application 203,Rev 1.Rev Reduces Scope of Previous Changes Re Tech Spec Table 3.6-1, Containment Isolation Valves ML20059C7901990-08-27027 August 1990 Amend 162 to License NPF-1,revising Tech Spec 3/4.6.1, Containment Integrity ML20058L4511990-08-0202 August 1990 Corrected Amend 161 to License NPF-1,revising Items 6.4.1 & 6.4.2 Re Administrative Controls ML20055C7511990-06-18018 June 1990 Amend 161 to License NPF-1,changing Qualification Requirements,As Specified in Tech Spec 6.3.1,that Must Be Met by Radiation Protection Manager ML20245H3661989-08-10010 August 1989 Corrected Page 3/4 7-18 to Amend 152 to License NPF-1 ML20247C8771989-07-19019 July 1989 Application for Amend to License NPF-1 Consisting of License Change Application 179.Amend Changes Description of Turbine Steam Supply Valves in Tech Spec Table 3.6-1 from motor-operated to air-operated ML20246A7491989-06-30030 June 1989 Application for Amend to License NPF-1,consisting of License Change Application 182,reflecting Reorganization of Util Nuclear Div.Certificate of Svc & Description of Change Encl ML20245E6491989-06-20020 June 1989 Amend 154 to License NPF-1,revising Tech Spec 5.7.2.2 to Allow Mods to control-auxiliary-fuel Bldg Complex ML20244E6111989-06-12012 June 1989 Application for Amend to License NPF-1,changing Orifice Size of Steam Line Safety Valves Shown in Tech Spec Table 4.7-1, Steam Line Safety Valves Per Loop ML20247M9211989-05-24024 May 1989 Amend 153 to License NPF-1,permitting Use of Upgraded Fuel Assemblies Which Incorporate Features of Westinghouse VANTAGE5 Fuel Assemblies & Allowing Extended Fuel Burnup to 60 Gwd/Mt & Higher Nuclear Peaking Factors ML20247H9521989-05-15015 May 1989 Amend 152 to License NPF-1,revising Tech Specs Re Chlorine Detection Sys & Control Room Emergency Ventilation Sys ML20246P5991989-05-12012 May 1989 Corrected Amend 58 to License NPF-1,consisting of Tech Spec Page 3/4 1-15 Re Borated Water Sources During Shutdown ML20247F1871989-03-17017 March 1989 Amend 151 to License NPF-1,revising Tech Specs by Deleting U-235 Fuel Enrichment Limit on Fuel Assemblies & Authorizing Storage & Use of New Fuel Assemblies W/Enrichment Up to 4.5 Weight Percent ML20236C4651989-03-15015 March 1989 Corrected Tech Spec Page 3/4 3-47 to Amend 93 to License NPF-1 ML20235T5291989-02-28028 February 1989 Amend 150 to License NPF-1,reflecting Merger of Pacific Power & Light & Utah Power & Light Companies to Form Pacificorp ML20235Q9101989-02-10010 February 1989 Application for Amend to License NPF-1,consisting of License Change Application 173,clarifying Surveillance Requirements for Containment Equipment Hatch ML20235L9421989-02-10010 February 1989 Application for Amend to License NPF-1,consisting of License Change Application 174.Amend Revises Tech Specs to Allow Mods to Control Auxiliary Fuel Bldg Complex Resulting in Increase in Lateral Shear Forces of Any Story ML20154D1681988-09-0909 September 1988 Application for Amend to License NPF-1,revising Tech Specs Re Setpoint for Pressurizer LPSI Ressure Safety Injection Necessary to Accommodate New Instrumentation ML20151X1121988-08-17017 August 1988 Corrected Page to Amend 142 of License NPF-1 Re Administrative Controls ML20151T4991988-08-12012 August 1988 Application to Amend License NPF-1,consisting of License Change Application 169,revising Tech Specs Surveillance Requirements for ECCS Check Valves 1999-08-05
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PORTLAND GENERAL ELECTRIC COMPANY EUGENE WATER & ELECTRIC BOARD AND PACIFIC POWER & LIGHT COMPANY Operating License NPF-1 Docket 50-344 License Change Application 161 This License Change Application requests modifications to Operating License NPF-1 for the Trojan Nuclear Plant to include the ef fects of nuclear fuel design changes.
PORTLAND GENERAL ELECTRIC COMPANY By C D. W. Cockfield Vice President Nuclear Subscribed and sworn to before me this 20th day of November 1987.
Y3daG V LuJ Notary [t2blico'fOregon My Commission Expires: /
J.hr..b&sk BETTY J. SIMICH kod20ao299 ADocM 05000072 ja044 NOTARY PUBLIC-OREGON P My commission Expires .IP.MIr.{g PDR {
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LCA 161 Page 1 of 7 j DESCRIPTION OF CHANCE A description of the,. proposed changes to the existing Trojan Technical Specifications (TTS)'is as follows. i i
Page Section Description of Change 2-2' 2.1 Safety Figure 2.1-1 is revised to change the four-loop Limits safety limit on the combination of thermal power, ;
pressurizer pressure and the highest operating loop T avg. This is due to reanalysis with a revised expression for the Enthalpy Rise Hot Channel Factor F{H. See the change description for TTS Page B 2-2, ;
below.
2-5, 2.2 Limiting Notes 3 and 4 are changed to revise the margin for 2-9 Safety the maximum trip points (Allowable Values) for i System Overtemperature and Overpower AT.
Settings In the overtemperature AT trip setpoint function:
2-7, - T' and T" are revised for consistency with 2-8 current analysis, 2-7 - The definition of ATo in Note 1 is corrected ,
by deleting the parenthetical phrase. Also, the K1 setpoint is revised from 1.32 to 1.28 for ,
consistency with the revised core limits. l l
2-8 - The ft (AI) function is modified for consistency with the revised axial offset limits, and 2-8 - A typographical error is corrected in Note 2.
B 2-2 Bases 2.1.1 Theenthalpyrisehotchannelfactor,F{He 18 l Reactor Core revised from 1.49 to 1.56.
B 2-6 Bases 2.2.1 The minimum limit of 1.73 for the Departure from Reactor Trip Nucleate Boiling Eatio (DNBR) is replaced by the System Instru- phrase "the safety analysis DNBR limit", such that mentation future analysis changes will not require a change Setpoints to the Technical Specification Bases.
3/4 2-5, 3.2.2 The constant values in the expressions for the 3/4 2-7 Heat Flux Hot limits on Fq(2) are revised to 2.50 and 5.00 for Channel Factor greater than, and less than or equal to 50 percent Fn(Z) power, respectively. The K(Z) function in Figure 3.2-2 is also revised, as established by a Loss-of-Coolant Accident (LOCA) reanalysis.
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o LCA 161 I Page 2 of:.7
~.g 3 Page Section Description'of Change 3/4 2-6a An error.is corrected in Paragraph 4.2.2.2.e.
3/4 2-8 -3.2.3,'4.2.3.2 Therevisedvalueof1.56isinsertedforF{H*
3/4 2-9 'RCS Flow Rate,
~ and FR-
'3/4 2-9a' 4.2.3.2 Therevisedvalueof1.56'isinsertedfor'F{H RCS Flow Rate- in the expression for the limit en F R- .i and F 3' B 3/4 2-1 3/4.2.1 The value for Fq(Z) is revised from 2.32 to
' Axial Flux: to 2.50.
Difference.
(AFD) a '
B 3/4 2-4, Bases 3/4.2.2 The revised value of 1.56 is inserted in'the-B 3/4 2-5 and 3/4.2.3: expressionfor.maximumF{H,andrevisedvalues Heat Flux Hot for DNBR margins are incorporated based on incorpo-Chanm.1 Factor, ration of a new rod bow penalty. Also, the 2.5 per-etc. cent DNBR penalty due to core bypass flow is encounted for in the new safety limit DNBR value.
B 3/4 2-6' Bases 3/4.2.5 The minimum limit of 1.73 for DNBR is replaced by DNB Parameters the phrase " greater than or equal to the safety analysis DNBR limit" such that future analysis changes will not require a change to the Technical Specification Bases.
B 3/4 4-1 Bases 3/4.4.1 The minimum limit of 1.73 for DNBR is replaced by Reactor Cool- the phrase "the safety analysis DNBR limit" such ant Loops and that future analysis changes will not require a Coolant change to the Technical Specification Bases.
Circulation B 3/4 5-2 3/4.5.5 A third basis is added to indicate that RWST minimum Refueling volume and' boron concentration must meet suberiti-Water Storage cality requirements for cold post-large break LOCA Tank (RWST) conditions.
5-4 5.3.1 This section is revised to provide for loading of j Fuel substitute rods for fuel rods as required for fuel l cf Assemblies reconstitution.
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1 LCA 161 Page 3 of 7 r
REASON FOR CHANGE These proposed changes to the Trojan Technical Specifications, Appendix A to Operating License NPF-1, are being made to provide for. improved operating economy. Portland General Electric Company desires to utilize an upgraded fuel design for future Trojan core loadings, beginning with-Cycle 11. Features of the upgraded fuel consist of fuel assemblies with y"
reconstitutable top nozzles, axial fuel blankets and the capability of achieving extended fuel burnups as well as satisfying higher nuclear peaking factors [F and F9 (Z)}. These features were previously reviewed (and approved) by the Nuclear Regulatory Commission (NRC) as Westinghouse Topical Report WCAP-10444-P-A, " Reference Core Report VANTAGE 5 Fuel Assembly",-September 1985. Analysis supporting the higher nuclear peaking factors is described in the enclosed Plant Safety Evaluation Report for the Trojan Nuclear Plant Fuel Upgrade.
The reconstitutable top nozzles incorporate a mechanical disconnect feature that facilitates removal of the top nozzle as required for fuel assembly repairs, if needed. The upgraded fuel assemblies also incorpo-rate fuel rods with long tapered end plugs to provide for easier replace-
. ment of individual fuel rods.
The axial fuel blanket consists of a nominal 6 inches of natural uranium oxide pellets at each end of the fuel pollet stack to reduce neutron .l leakage and improve uranium utilization. This core reactivity decrease is compensated by slightly increasing the enrichment of the remaining fuel.
The upgraded fuel design is capable of achieving a lead fuel rod average burnup of approximately 60,000 mwd /MTU. The basis for this extended burnup design was previously reviewed (and approved) by the NRC as Westinghouse Topical Report WCAP-10125-P-A, " Extended Burnup Evaluation of Westinghouse Fuel", December 1985.
Use of the upgraded fuel desig? in Trojan reload cores is optimized by the use of increased nuclear peaking f actors, Fh and FQ (z), to reduce burnable neutron absorber requirements, improve fuel economy, and increase nuclear design flexibility. Changes to the nuclear design bases provided in the Trojan Nuclear Plant Updated Final Safety Analysis Report (FSAR) are not required. Anticipated changes to the Trojan FSAR are presented in Section 5.0 (Accident Analysis) of the enclosed Plant Safety Evalua-tion Report for the Trojan Nuclear Plant Fuel Upgrade, f
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i LCA 161 page 4 of 7 SIGNIFICANT HAZARDS CONSIDERATION DETERMINATION The proposed revisions to the Trojan Technical Specifications do not involve a significant hazards consideration because operation of the Trojan Nuclear plant in accordance with these changes:
.(1) Would not involve a significant increase in.the probability or consequences of an accident previously evaluated. The changes to the nuclear fuel design, ie, the removable fuel assembly top nozzle and the axial fuel blanket, are not involved in accident initiation and have been analyzed and determined to have no adverse affect on the consequences of an accident. The changes to power peaking limits also have no effect on accident initiation. They could, '
however, have some effect on the consequences of an accident. The possible accident co'nsequence changes have been evaluated by reana-lyzing the Loss-of-Coolant Accident (LOCA) and the Departure from Nucleate Boiling Ratio (DMBR) margin. The results of these analyses demonstrate that the existing limits remain applicable, and there are no significant changes in the accident consequences due to the changes in the power peaking factor limits. I Changes to reactor trip setpoints for Overtemperature and Overpower AT were made to retain the DNBR protection provided by these trips and thus do not increase the probability or consequeneca of an acci-dent. Additional changes concern the fuel design description to allow substitution of non-fuel rods or vacancies in fuel assemblies to facilitate fuel assembly reconstitution. The details of such substitutions will be evaluated as part of the reload safety evaluation When specific changes are proposed.
(2) Would not create the possibility of a new or different kind of acci-dent from any previously evaluated. The changes do not affect com-ponents, systems or structures that have the capability of causing accidents. The power peaking factor changes affect normal operating limits that are routinely evaluated for reload cores. New or dif-ferent accident situations are not created by small changes in these limits.
It should be noted that some of the changes incorporated in the small break LOCA analysis, for example a revised methodology, higher assumed power level and reduced charging pump flow rate, have caused the limiting small break to shift from a pipe diameter of 4 inches to 3 inches. This is not a new or different kind of accident from those previously analyzed.
As previously noted, the fuel design changes, ie, the reconsti-tutable top nozzles and the axial fuel blanket, are not significant changes from the current fuel design. For the axial fuel blanket, L __ __ _ _ _.
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i LCA 161 Page 5 of 7 {
1 the possibility of interchanging enriched fuel and natural uranium ]
blanket fuel pellets is minimal because the pellets are different q lengths, and all fuel rods are gamma scanned as part of the produc- j tion process. In any event, the'results of such a misloading are bounded by the analysis described in Trojan Final Safety Analysis Report (FSAR) Section 15.4.7, " Inadvertent Loading and Operation of j a Fuel Assembly in an Improper Position".
(3) Would not involve a significant reduction in a margin of safety.
The DNBR accident analysis safety limits have been changed to 3 cccount for.the higher power peaking factors. These safety limits {
continue to meet the required design limits (with margin). The l changes to the Overpower and Overtemperature AT setpoints to l accommodate the new core limits utilize the previously used I methodology and retain the margin originally included. The LOCA I analysis demonstrates that the Emergency Core Cooling System (ECCS) !
acceptance criteria of Title 10, code of Federal Regulations, Part f 50, Section 46'(10 CFR 50.46) continue to be met. j In the March 6, 1986 Federal Register (51 FR 7750-51), the Nuclear Regulatory Commission (NRC) published a list of examples of license amendments that are not likely to involve a significant hazards con-sideration. Example (iii) of that list relates to a change resulting j from a nuclear reactor core reloading, if no fuel assemblies signifi- !
cantly different from those found previously acceptable to the NRC for a previous core at the facility are involved. As noted in Section 3.0 (Nuc1 ear Design) of the enclosed Plant Safety Evaluation for the Trojan Nuclear Plant Fuel Upgrade, the change from the current standard fuel ,
core to a core containing the upgraded fuel will not require changes to I the current nuclear design bases presented in the Trojan FSAR. An evaluation of the fuel upgrade has demonstrated that the impact of the l fuel upgrade does not cause a significant change to the physics charac- l teristics of the Trojan core beyond the normal range of variations seen j from cycle to cycle. I Example (vi) of the April 6, 1986 list relates to a change which may l either result in some increase to the probability or consequences of a previously analyzed accident or may reduce in some way a safety margin, but where the results of the change are clearly within all acceptance ,
criteria, with respect to the system or component, specified in the l Standard Review Plan. As noted above, the nuclear design bases in the Trojan FSAR remain applicable. Use of the upgraded fuel does not require changes in the nuclear design methods or philosophy, although increased emphasis is placed on the use of three-dimensional modeling due to the ,
axially heterogeneous characteristics of the core with axial fuel l blankets.
The thermal-hydraulic design for the upgraded fuel has been reanalyzed
} with FAH equal to 1.62 to support a Technical Specification increase j
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f i LCA 161 page 6 of 7
, inF{H from 1.49 to 1.56. The effect of the increase in FAH 0" Departure 1from Nucleate Boiling Ratio (DNBR) is offset'by a reduction in the safety analysis DNBR margin. Thus, the transient value of DNBR (for the affected DNB events) will be lower. For this reason, revised core limits were generated based on the increased limit on.FAH, Based on the new core protection limits, the Overtemperature'and Overpower AT setpoint equation constants were recalculated, consistent with the methods outlined in WCAp-8746; " Design Bases for the Thermal Overpower and Overtemperature Delta-T Trip Functions".
A Loss-of-Coolant Accident (LOCA) analysis was also performed to demon-strate that use of the upgraded fuel design, with FAH increased to 1,62 and the maximum LOCA Fq increased to 2.5, is acceptable with respect to the ECCS Acceptance Criteria of 10 CFR 50.46. In addition to the increased peaking factors, the analysis also assumed a core thermal power level of 102 percent of 3558 MWt, and 11.5 percent uniform steam generator tube plugging., The analysis results demonstrate that for both small and large breaks (up to and including the double-ended severance of-a reactor coolant pipe), the ECCS meets the 10 CFR 50.46 acceptance criteria.
Lastly, Example (ix) of the April 6, 1986 list relates to a repair or replacement of a major component or system important to safety, if the-following conditions are met:
(1) The repair or replacement process involves practices Which have been successfully implemented at least once on similar components or systems elsewhere'in the nuclear industry or in other industries, and does not involve a significant increase in the probability or consequences of an accident previously evaluated or create the possibility of a now or different kind of accident from any accident preciously evaluated; and (2) The repaired or replacement component or system does not result in a ;
significant change in its safety function or a significant reduction in any safety limit (or limiting condition of operation) associated with the component or system.
Consider the nuclear ~ fuel upgrade as replacement of a major component important to safety. As noted in Section 1.0 (Introduction and Summary) of the enclosed plant Safety Evaluation Report for the Trojan Nuclear riant Fuel Upgrade, four fuel assemblies Which incorporated the recon-L stitutable top nozzles, axial blankets, and extended burnup capability were loaded into the V.C. Summer Unit 1 core and were used for power production from December 1984 to March 1987. After two cycles of
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operation, with an average burnup of approximately 30,000 mwd /MTU, all 1; four assemblies had maintained good mechanical integrity with no evidence of mechanical damage or weer on the VANTACE 5 components and were reloaded into the core for a third operating cycle.
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. SAFETY / ENVIRONMENTAL EVALUATION
SUMMARY
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. Safety and environmental evaluations were performed as required by-10'CFR 50 and the TTS. This review determined that.'the' proposed changes
' do not create an unreviewed-safety question since Plant operations remain consistent with the' Updated FSAR, adequate surveillance is' maintained, and there is no'significant adverse impact on the environment. An'evalu -
ation of the radiological impact'on postulated accident consequences due to the extended fuel burnup is presented in Appendix B of the enclosed Plant Safety Evaluation' Report for the Trojan Nuclear Plant Fuel Upgrade.
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