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Category:INTERNAL OR EXTERNAL MEMORANDUM
MONTHYEARML20217F0841999-10-0808 October 1999 Informs That During 466th Meeting of ACRS on 990930-1002, CEOG Proposal to Eliminate PASS from Plant Design & Licensing Bases for CEOG Plants,Were Reviewed.Discussion & Recommendations,Listed ML20217C5311999-10-0808 October 1999 Notification of 991027 Meeting with Representatives of Gpu in Rockville,Md to Discuss Recent Control Rod Surveillance Performance Issues at TMI-1.Proprietary Portions of Meeting Will Be Closed to Public ML20212K8901999-10-0505 October 1999 Notification of 991027 Meeting with Util in Rockville,Md to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TM1-1 ML20216J0151999-09-29029 September 1999 Notification of 991020 Meeting in Forked River,Nj to Discuss Licensee 990922,response to NRC & Other Info Addressing Sale of Portion of Land That Is Part of Plant Site ML20216G3671999-09-10010 September 1999 Forwards CNWRA Program Manager Periodic Rept (Pmpr) for Period 990731-0827 ML20210U7571999-08-20020 August 1999 Forwards Info Received from Gpu Nuclear,Inc on 990820 in Preparation for 990823.Requests Info Be Docketed ML20210C9991999-07-22022 July 1999 Revised Notification of 990813 Meeting with Gpu Nuclear,Inc Rockville,Maryland to Discuss TMI-1 Licensing Action Status. Meeting Date Changed ML20210E9511999-07-12012 July 1999 Notification of 990805 Meeting with Representative of Gpu Nuclear,Inc in Rockville,Md Re Plant,Unit 1 Licensing Action Status ML20212H9621999-06-23023 June 1999 Revised Notification of Meeting with Gpu Nuclear,Inc to Discuss Proposed Mods to RBS Sys Procedures & HPI Cross Connect Lineup.Meeting Rescheduled to 10 A.M. on 990713 ML20195H8521999-06-18018 June 1999 Requests That Encl Questions,Faxed to Gpu Nuclear,Inc on 990616,be Docketed,In Preparation for Forthcoming Conference Call Re TS Change Request 248, Remote Shutdown Sys, ML20195H9911999-06-15015 June 1999 Notification of 990707 Meeting with Util to Discuss Licensee Proposed Mods to Reactor Bldg Spray Procedures & High Pressure Injection Cross Connection Lineup ML20206F2921999-05-0505 May 1999 Forwards Draft Questions Which Were Faxed to Licensee for TMI Unit 1,GPUN on 990505 in Preparation for 990506 Conference Call on TS Change Request 279 ML20206D1291999-04-28028 April 1999 Notification of 990507 Meeting with Gpu Nuclear,Inc in Rockville,Maryland to Discuss Three Mile Island,Unit 1 Licensing Action Status ML20205N3161999-04-0909 April 1999 Notification of Significant Licensee Meeting 99-19 with Util on 990423 to Discuss Emergency Feedwater Flow Discrepancies ML20197G6381998-12-0707 December 1998 Forwards Program Manager Period Rept (Pmpr) for Period 981024-1120 ML20196E2801998-11-30030 November 1998 Discusses Closeout of TAC MA1607 Re Cross Potential for common-cause High Pressure Injection Pump Failure IR 05000289/19983011998-11-0404 November 1998 Forwards NRC Operator Licensing Exam Rept 50-289/98-301 with as Given Written Exam for Tests Administered on 980824-27 at Facility ML20154G3451998-10-0101 October 1998 Rev 2 to Notification of Significant Licensee Meeting 97-73 on 981023 in King of Prussia,Pa to Discuss Actions Taken Re Engineering Corrective Action Performance Assessment Team Findings ML20153D9681998-09-24024 September 1998 Notification of 981006 Meeting W/Gpu Nuclear,Inc in Rockville,Md to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TMI-1 ML20237E8381998-08-28028 August 1998 Notification of 980917 Meeting W/Gpu Nuclear,Inc & Amergen in Rockville,Md to Discuss Sale & Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen ML20237E4591998-08-20020 August 1998 Submits Rev 1 to Notification of Significant Licensee Meeting 98-73 W/Util in Middletown,Pa to Discuss Actions Taken Re Engineering Corrective Action PA Team Findings. Meeting Postponed ML20237C9401998-08-14014 August 1998 Notification of Significant Licensee Meeting 98-73 on 980828 W/Gpu Nuclear,Inc in Middletown,Pa to Discuss Actions Taken Re Engineering C/A Performance Assessment Team Findings ML20247M2191998-05-19019 May 1998 Notification of 980604 Meeting W/Gpu Nuclear Inc in Royalton,Pa to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TMI-1 ML20216B6871998-05-0808 May 1998 Notification of 980527 Meeting W/Representative of Gpu Nuclear,Inc in Rockville,Md to Discuss Licensee 980324 Submittal Re Control Room Habitability at TMI-1 IR 05000289/19980991998-02-26026 February 1998 Notification of Significant Licensee Meeting 98-22 W/Util on 980318 to Discuss SALP for Period Covering 960805-980124,as Documented in SALP Rept 50-289/98-99 IA-98-345, Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 11998-02-0606 February 1998 Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 1 ML20154B7931998-02-0606 February 1998 Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 1 ML20199H6701997-11-20020 November 1997 Notifies of 971212 Meeting W/Gpu in Rockville,Md to Discuss Control Room Habitability at Unit 1 ML20199E7071997-11-14014 November 1997 Revised Notification of 971119 Meeting W/Gpu Nuclear Corp,In Rockville,Md to Discuss Control Room Habitability at TMI-1 Nuclear Facility.Meeting Cancelled Until Further Notice ML20199B3111997-11-0606 November 1997 Notifies of 971119 Meeting W/Gpu in Rockville,Md to Discuss Control Room Habitability ML20212G9531997-11-0505 November 1997 Forwards Gpu SE Re Review of AP600 Shutdowm Ts.Section B.3.9.4 of STS Cites Gpu Nuclear SE 0002000-001 Rev 0,880520 as Ref E Temporary Containment Penetration Closure Devices Equivalent to Valve or Blind Flange ML20216E9871997-09-0808 September 1997 Notification of 970910 Meeting W/Util in Rockville,Md to Discuss Potential Dose Consequences from Postulated Steam Line Break & Postulated Accident Sys Leakage Limits ML20149D8881997-07-11011 July 1997 Notification of Significant Licensee Meeting 97-86 W/Util on 970725 in King of Prussia,Pa to Discuss Apparent Violations Re Failure to Recognize General Emergency Condition During 970305 Exercise ML20140G6231997-06-0505 June 1997 Notification of 970716 Meeting W/Gpun in King of Prussia, Pennsylvania for Presentation & Discussion Re Root Cause Determination for Recent QC Issues Performed by Gpun Per NRC CAL ML20151U4191997-05-23023 May 1997 Discusses Review of Two Addl Concerns Identified in 970407 Memo to Recipient from Special Insp Branch Re Addl Open Items Associated W/Dec 1996 Design Insp Rept 50-289/96-201 ML20148D9851997-05-21021 May 1997 Notification of Significant Licensee Meeting 97-57 W/Util on 970528 to Discuss Formal Exit Meeting for Licensee Remedial Emergency Preparedness Exercise on 970513 & Licensee Discussion Re NRC CAL ML20141E5381997-05-15015 May 1997 Notification of 970530 Meeting W/Representatives of Gpu Nuclear Corp in Rockville,Md to Discuss Status of Licensing Activities Associated W/Plant,Unit 1 ML20138D3161997-04-21021 April 1997 Notification of Significant Licensee Meeting 97-47 W/Util on 970430 to Discuss Root Cause Analysis of 970305 Emergency Preparedness Drill Weaknesses ML20140D5251997-04-18018 April 1997 Notification of 970502 Meeting W/Util in Rockville,Md to Discuss Schedules & Resolution of Issues Relating to Thermo-Lag Fire Barriers ML20135F8801997-03-0404 March 1997 Notification of Significant Licensee Meeting 97-27 W/Util on 970317 to Discuss Emergency Preparedness Insp Exit Meeting ML20138M3111997-02-20020 February 1997 Notification of 970306 Meeting W/Gpu in Rockville,Md to Discuss Three Mile Island,Unit 1 Reactor Pressure Vessel pressure-temp Limit Curves ML20147D8391997-02-12012 February 1997 Notification of 970220 Meeting W/Util Representatives in Rockville,Md to Discuss Status of Licensing Activities Associated W/Plant,Unit 1 Facility ML20133Q3031997-01-16016 January 1997 Notification of Significant Licensee Meeting 97-08 W/Util on 970131 in Middletown,Pa Re Safety Sys Functional Insp Exit Meeting ML20149M0471996-12-10010 December 1996 Forwards Internet Mail Received from PM Blanch ML20129K3731996-11-21021 November 1996 Notification of 961126 Meeting W/Gpun in North Bethesda,Md to Discuss TMI-1 SG Issues ML20135B0871996-11-15015 November 1996 Notification of Significant Licensee Meeting 96-118 W/Util on 961122 to Discuss Plant Motor Operated Valve Testing Program self-assessment ML20129K2561996-11-0505 November 1996 Notification of Significant Licensee Meeting 96-109 W/Listed Attendees on 961202-03 in Philadelphia,Pa to Provide Training,Resolve Interagency Exercise Scheduling Conflicts & Discuss Current Issues in Emergency Preparedness ML20136E3011996-10-31031 October 1996 Forwards Schedule for Activities at Plant for Next Few Months ML20134E9191996-10-29029 October 1996 Forwards Rationale for Inital Plants Selected for Design Insps & for Plants Considered for Second Quarter FY97 Design Insps ML20128G1661996-10-0303 October 1996 Summarizes 960924 Meeting W/Gpu Nuclear Corp in Rockville,Md Re Preliminary Responses to Staff RAI Concerning Request to Change EALs for TMI-1.List of Participants & Copy of Preliminary Response to RAI Encl 1999-09-29
[Table view] Category:MEMORANDUMS-CORRESPONDENCE
MONTHYEARML20217C5311999-10-0808 October 1999 Notification of 991027 Meeting with Representatives of Gpu in Rockville,Md to Discuss Recent Control Rod Surveillance Performance Issues at TMI-1.Proprietary Portions of Meeting Will Be Closed to Public ML20217F0841999-10-0808 October 1999 Informs That During 466th Meeting of ACRS on 990930-1002, CEOG Proposal to Eliminate PASS from Plant Design & Licensing Bases for CEOG Plants,Were Reviewed.Discussion & Recommendations,Listed ML20212K8901999-10-0505 October 1999 Notification of 991027 Meeting with Util in Rockville,Md to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TM1-1 ML20216J0151999-09-29029 September 1999 Notification of 991020 Meeting in Forked River,Nj to Discuss Licensee 990922,response to NRC & Other Info Addressing Sale of Portion of Land That Is Part of Plant Site ML20216G3671999-09-10010 September 1999 Forwards CNWRA Program Manager Periodic Rept (Pmpr) for Period 990731-0827 ML20210U7571999-08-20020 August 1999 Forwards Info Received from Gpu Nuclear,Inc on 990820 in Preparation for 990823.Requests Info Be Docketed ML20210C9991999-07-22022 July 1999 Revised Notification of 990813 Meeting with Gpu Nuclear,Inc Rockville,Maryland to Discuss TMI-1 Licensing Action Status. Meeting Date Changed ML20210E9511999-07-12012 July 1999 Notification of 990805 Meeting with Representative of Gpu Nuclear,Inc in Rockville,Md Re Plant,Unit 1 Licensing Action Status ML20212H9621999-06-23023 June 1999 Revised Notification of Meeting with Gpu Nuclear,Inc to Discuss Proposed Mods to RBS Sys Procedures & HPI Cross Connect Lineup.Meeting Rescheduled to 10 A.M. on 990713 ML20195H8521999-06-18018 June 1999 Requests That Encl Questions,Faxed to Gpu Nuclear,Inc on 990616,be Docketed,In Preparation for Forthcoming Conference Call Re TS Change Request 248, Remote Shutdown Sys, ML20195H9911999-06-15015 June 1999 Notification of 990707 Meeting with Util to Discuss Licensee Proposed Mods to Reactor Bldg Spray Procedures & High Pressure Injection Cross Connection Lineup ML20206F2921999-05-0505 May 1999 Forwards Draft Questions Which Were Faxed to Licensee for TMI Unit 1,GPUN on 990505 in Preparation for 990506 Conference Call on TS Change Request 279 ML20206D1291999-04-28028 April 1999 Notification of 990507 Meeting with Gpu Nuclear,Inc in Rockville,Maryland to Discuss Three Mile Island,Unit 1 Licensing Action Status ML20205N3161999-04-0909 April 1999 Notification of Significant Licensee Meeting 99-19 with Util on 990423 to Discuss Emergency Feedwater Flow Discrepancies ML20203E0321999-02-11011 February 1999 Staff Requirements Memo Re 990211 Affirmation Session in Rockville,Md (Open to Public Attendance) Re Secys 99-044 & 99-045 ML20197G6381998-12-0707 December 1998 Forwards Program Manager Period Rept (Pmpr) for Period 981024-1120 ML20196E2801998-11-30030 November 1998 Discusses Closeout of TAC MA1607 Re Cross Potential for common-cause High Pressure Injection Pump Failure IR 05000289/19983011998-11-0404 November 1998 Forwards NRC Operator Licensing Exam Rept 50-289/98-301 with as Given Written Exam for Tests Administered on 980824-27 at Facility ML20154G3451998-10-0101 October 1998 Rev 2 to Notification of Significant Licensee Meeting 97-73 on 981023 in King of Prussia,Pa to Discuss Actions Taken Re Engineering Corrective Action Performance Assessment Team Findings ML20153D9681998-09-24024 September 1998 Notification of 981006 Meeting W/Gpu Nuclear,Inc in Rockville,Md to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TMI-1 ML20237E8381998-08-28028 August 1998 Notification of 980917 Meeting W/Gpu Nuclear,Inc & Amergen in Rockville,Md to Discuss Sale & Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen ML20237E4591998-08-20020 August 1998 Submits Rev 1 to Notification of Significant Licensee Meeting 98-73 W/Util in Middletown,Pa to Discuss Actions Taken Re Engineering Corrective Action PA Team Findings. Meeting Postponed ML20237C9401998-08-14014 August 1998 Notification of Significant Licensee Meeting 98-73 on 980828 W/Gpu Nuclear,Inc in Middletown,Pa to Discuss Actions Taken Re Engineering C/A Performance Assessment Team Findings ML20248H7001998-05-20020 May 1998 Staff Requirements Memo Re SECY-98-071,exemption to 10CFR72.102(f)(1) Seismic Design Requirement for TMI-2 ISFSI ML20247M2191998-05-19019 May 1998 Notification of 980604 Meeting W/Gpu Nuclear Inc in Royalton,Pa to Discuss Status of Licensing Actions Proposed & Currently Under Review by NRC for TMI-1 ML20216B6871998-05-0808 May 1998 Notification of 980527 Meeting W/Representative of Gpu Nuclear,Inc in Rockville,Md to Discuss Licensee 980324 Submittal Re Control Room Habitability at TMI-1 IR 05000289/19980991998-02-26026 February 1998 Notification of Significant Licensee Meeting 98-22 W/Util on 980318 to Discuss SALP for Period Covering 960805-980124,as Documented in SALP Rept 50-289/98-99 ML20154B7931998-02-0606 February 1998 Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 1 IA-98-345, Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 11998-02-0606 February 1998 Discusses Licensing Basis for Letdown Line Break Outside Containment for Plant,Unit 1 ML20199H6701997-11-20020 November 1997 Notifies of 971212 Meeting W/Gpu in Rockville,Md to Discuss Control Room Habitability at Unit 1 ML20199E7071997-11-14014 November 1997 Revised Notification of 971119 Meeting W/Gpu Nuclear Corp,In Rockville,Md to Discuss Control Room Habitability at TMI-1 Nuclear Facility.Meeting Cancelled Until Further Notice ML20199B3111997-11-0606 November 1997 Notifies of 971119 Meeting W/Gpu in Rockville,Md to Discuss Control Room Habitability ML20212G9531997-11-0505 November 1997 Forwards Gpu SE Re Review of AP600 Shutdowm Ts.Section B.3.9.4 of STS Cites Gpu Nuclear SE 0002000-001 Rev 0,880520 as Ref E Temporary Containment Penetration Closure Devices Equivalent to Valve or Blind Flange ML20216E9871997-09-0808 September 1997 Notification of 970910 Meeting W/Util in Rockville,Md to Discuss Potential Dose Consequences from Postulated Steam Line Break & Postulated Accident Sys Leakage Limits ML20149D8881997-07-11011 July 1997 Notification of Significant Licensee Meeting 97-86 W/Util on 970725 in King of Prussia,Pa to Discuss Apparent Violations Re Failure to Recognize General Emergency Condition During 970305 Exercise ML20140G6231997-06-0505 June 1997 Notification of 970716 Meeting W/Gpun in King of Prussia, Pennsylvania for Presentation & Discussion Re Root Cause Determination for Recent QC Issues Performed by Gpun Per NRC CAL ML20151U4191997-05-23023 May 1997 Discusses Review of Two Addl Concerns Identified in 970407 Memo to Recipient from Special Insp Branch Re Addl Open Items Associated W/Dec 1996 Design Insp Rept 50-289/96-201 ML20148D9851997-05-21021 May 1997 Notification of Significant Licensee Meeting 97-57 W/Util on 970528 to Discuss Formal Exit Meeting for Licensee Remedial Emergency Preparedness Exercise on 970513 & Licensee Discussion Re NRC CAL ML20141E5381997-05-15015 May 1997 Notification of 970530 Meeting W/Representatives of Gpu Nuclear Corp in Rockville,Md to Discuss Status of Licensing Activities Associated W/Plant,Unit 1 ML20138D3161997-04-21021 April 1997 Notification of Significant Licensee Meeting 97-47 W/Util on 970430 to Discuss Root Cause Analysis of 970305 Emergency Preparedness Drill Weaknesses ML20140D5251997-04-18018 April 1997 Notification of 970502 Meeting W/Util in Rockville,Md to Discuss Schedules & Resolution of Issues Relating to Thermo-Lag Fire Barriers ML20135F8801997-03-0404 March 1997 Notification of Significant Licensee Meeting 97-27 W/Util on 970317 to Discuss Emergency Preparedness Insp Exit Meeting ML20138M3111997-02-20020 February 1997 Notification of 970306 Meeting W/Gpu in Rockville,Md to Discuss Three Mile Island,Unit 1 Reactor Pressure Vessel pressure-temp Limit Curves ML20147D8391997-02-12012 February 1997 Notification of 970220 Meeting W/Util Representatives in Rockville,Md to Discuss Status of Licensing Activities Associated W/Plant,Unit 1 Facility ML20133Q3031997-01-16016 January 1997 Notification of Significant Licensee Meeting 97-08 W/Util on 970131 in Middletown,Pa Re Safety Sys Functional Insp Exit Meeting ML20149M0471996-12-10010 December 1996 Forwards Internet Mail Received from PM Blanch ML20129K3731996-11-21021 November 1996 Notification of 961126 Meeting W/Gpun in North Bethesda,Md to Discuss TMI-1 SG Issues ML20135B0871996-11-15015 November 1996 Notification of Significant Licensee Meeting 96-118 W/Util on 961122 to Discuss Plant Motor Operated Valve Testing Program self-assessment ML20129K2561996-11-0505 November 1996 Notification of Significant Licensee Meeting 96-109 W/Listed Attendees on 961202-03 in Philadelphia,Pa to Provide Training,Resolve Interagency Exercise Scheduling Conflicts & Discuss Current Issues in Emergency Preparedness ML20136E3011996-10-31031 October 1996 Forwards Schedule for Activities at Plant for Next Few Months 1999-09-29
[Table view] |
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NOV 151988 Docket Nos. 50-289; 50-320 MEMORANDUM FOR: Lee H. Bettenhausen, Chief, Projects Branch No. 1, Division of Reactor Projects FROM: Curtis J. Cowgill, Chief, Saactor Projects Section 1A, DRP
SUBJECT:
THI STATUS REPORT FOR THE PERIOD OCTOBER 7 - NOVEMBER 5, 1988 Enclosed is the TMI Resident Office monthly status report, which covers both TMI-1 and TMI-2. Th's report is to provide NRC management ;nd the public with highlights of significant events at TMI-1 and THI-2 from an NRC regulatory perspective.
ORKilNAL SIGNED BY Curtis J. Cowgill, Chief Re.ctor Projects Section 1A
Enclosure:
As sta'.ed cc w/ enclosure:
S. Varga, NRR
, T. Martin, EDO 1 J. Partlow, NRR 4 J. Roe, NRR L. Whitney, NRR T. Gerusky, BRP/ DER, Commonwealth of Pennsylvania :
Governor's Office of Policy, Commonwealth of Pennsylvania !
THI Alert Susquehanna Valley Alliance Friends & Family of TMI
- 0. Davonport L. Drey E. Haraler A. Herman H. Hucker J. Johnsrud P. Smith H. Spinelli C. Wolfe Concerned Mothers and Women Public Document Recm Local Public Document Room 0FFICIAL RECORD COPY TMI STAit'5 REPORT - 0001.0.0 I 11/29/80 '
0011300519 001115 PDR ADOCK 05000209 i%
R PNV
. -s
,., i .-
Lee.H. Bettenhausen 2 bcc w/ enclosure:
K. Abraham, RI (2 copies)
M. Miller, RI W. Kane, RI R. Conte, RI (8 copies)
W. Baunack, RI C. Crwgill, RI J. Vechselberger, RI J. ' jell, NRR Region I Docket Room (w/ concurrences) f RI: P RI: DRPH y CCowgill LBetteghausen 11/14/88 1;j {
OFFICIAL RECORD COPY TH1 STATUS REPORT - 0002.0.0 11/29/80 l
ENCLOSURE TMI-1 AND TMI 2 STATUS~
REPORT FOR THE PERIOD OCTOBTR 7 .TdTEMBER 5, 1988~ ,
- 1. TMI .i !
- a. Facility Operations Summary During the repart period, the licensee decided to shut dcwn the reactor to troubleshoot and repair the cause of an oil leak in the lubricating system for the "C" reactor coolant pump (RCF). On October 17, 1988, the plant was taken off line, repairs were completed, and power operations i were resumed on Octobcr 19, 1988. Also, on October 30, 1988, a reactor l trip occurred due to high Reactor Coolant System (RCS) pressure. As of l November 5, 1988, the TMI-1 reactor was at 100 percen+ power with Tave j
- at 579 F and RCS pressure at 2155 psig. l l b. Items of Special Interest j Outage for Reactor Coolant Pump 011 Leak
{
At 1 06 p.m. on October 17, 1988, the licensee shut down the reactor to ;
ar c4 .sh repairs to the lube oil system piping on the "C" RCP motor, t A seak developed on the lube oil syste and the licensee made reactor building entries on Gctober 14, 15, anc '6, 1988, to add oil to the ;
l system. The leak point could not be specifically determined. Also, J
because of relatively high vibrations on tne "0" RCP, the licensee de-cided to re-balance this pump. ;
- The licensee representative traced the oil leak to an area near an oil
, cooler for the RCP. They originally thought the leak was from a piping i cunnection. With the pipe connection repair completed and pending some i additional balancing work on the "D" RCP, the licensee decided to start i l up the reactor (critie.al 11:18 a.m., October 18,1988). Subsequently, !
the post-maintenance test on the "C" RCP revealed that the oil leak was
, from the oil cooler itself. In light of the new work, the licensee de-l cided to shut down the reactor. Following completivn of work on both i l RCP's, the licensee then conducted another reactor start-up (critical 3:41 p.m., October 19,1938).
Reactor Trip on October' 30, 1988 i i i
. On October 30, 1988, at 8:59 a.m., a reactor trip occurred due to hir'1 I
RCS pressure. Based on the nost-trip review, the licensee determined that the main turbine control valves went shut. With the control valves shut, high pressure developed in the steam generator (SG) causing the safety valves to lift (maximum SG pressure was 1060 psig).
f 0FFICIAL RE( N COPY TMI STA' .S REPORT - 0003.0.0 !
11/29/80 h
Encipsure 2 5everal seconds later high RCS pressure developed because of ths loss of heat removal in the SG's. The Reactor Pro'.ection System (RPS) then properly tripped the reactor.
The post-trip plant response was normal. There was no challenge to the Emergency Core Cooling System (ECCS) or the Heat Sink Protection System (HSPS) (safety gr:de initiation and control for the dmergency Fcedwater System). Also, there was no challenge to the Power Operated Relief Valve or the pressurizer safety valves (maximum RCS pressure was 2362 psig).
There was no indication of a radiation release based on a review of plant effluent moni+ ors. Operators initially reported to the NRC Operations Center a stuck open SG safety valve. However, af ter they lowered turbine header pressure, the valve successfully seated.
The licensee made a 10 CFR 50.70 notification at 9:59 a.m., well within allowable reporting requirements; however, the NRC Operations Center first learned of the trip by a local citizen who heard the noise and had
<tsual observation of the SG safety valves lifting.
The licensee's post-trip review determined that it was safe to start up the reactor, although the specific reason for the turbine stop valve closure could not be determined. They determined that more root cause analysis (RCA) on the main turbine's Electro-Hydraulic Control (EHC)
System and the plant's Integrated Control System (ICS) was necessary.
The licensee declared the reactor critical at 10:51 p.m. 0:teber 30,1988.
During testing, the licensee found a malfunctioning power supply in the EHC system, which they replaced. They also found a bad "control card" for one of six intercept valves. The licensee suspected that, if an inte-cept valve went shut, the Main Turbine Monitoring system would sense a power load imbalance that might cause the control valves to go shut.
They replaced this control card and thty were to review the affect of the faulty power supply on the 'tHC system. Also, the licensee is pur-suing additional bench testing on suspect equipmera in an attempt to better underttand the cause of the malfunction.
Other plant Transients Two other minor transient s occurred. On October 11, 1983, an electronic component failed in the unit's Integrated Control System (ICS). At 2:10 p.m., operators observed a drop in steam generator "A" and "B" levels from 19 parcent and 78 percent to 75 percent and 74 percent, respe r ly, with a corresponding partial insertion of control rods. This ap-runback appeared momentarily and then plant parameters appeared 'n to normal. Within a short time period, the transient condition .. ad, Operators took manual control of the ICS to prevent further oscillations and stabilized the plant while Instrument and Control (I&C) technicians identified and corrected the problem. Licensee personnel attributed the problem to a faulty analog memory module that is a component of the unit load demand of the ICS. Plant power decreased approximately 4 percent OFFICIAL RECORD COPY TMI STATUS REPORT - 0004.0.0 11/29/80
Enclosure 3 during the trans' int, which was terminated at 2:21 p.m. Upor replacing the analog memory module, plant conditions returned to normal with the ICS in auto.
On October 13, 1938, another minor plant transient occurred when an I&C technician inadvertently removed an electronic module from service. The technicians were troubleshooting the cause of spurious signals in an electronic component that provides Reactor Coolant System (RCS) hot leg temperature (T-hot) input to the ICS, Subsequent to troubleshooting the instrument loop, the technician removed the wrong module to determine if it was also functioning properly.
Removing t.he other module from service caused an immediate reduction in feedwater flow to the steam generators through the British Thermal Units (BTU) limits function of the ICS. Being prepared for such a plant tr&n-sient, the control room operato.'s responded in restoring feedwater flow.
Instrument and Control (I&C) technicians also quickly restored the input signal; together these actions prevented a plant trip The transient was short-lived as the plant was quickly returned ts :teady-state, full power operation.
- 2. TMI-2 Faci'ity Activities Sur. ary During the reporting period, cutting of the grid forging continued at a slow l pace. This third of five plates comprising the Lower Core Support Assembly
! (LCSA) is the largest of the five plates and proved to be very difficult to cut into the planned four sections for removal. The plasma arc torch is un-able to make complete cuts 1.nd much re-cutting and clearing of cut paths was required. Decontamination of plant surfaces continued at a reduced pace.
Five area > in tne auxiliary building were isolated from routine use and placed
- in an interim status for meeting proposed Post-Defueling Monitored Storage (POMS) conditions.
Decortamination/Dese Reduction Activities Major work emphasis was applied to the reactor building to ensure that this i
portion of the decontamination effort will be comp 12ted first. The majority i of the 143 cubicles in the auxiliary / fuel handling buildings have been de-
{ contaminated and work remaining consists of verifying that the cubicle is l
isolated, equipment secured, and the cubicle is ready for the reduced moni-J toring which would accompany the PCMS phase.
I
- 3. NRC Staff Activities The NRC staff assigned on site consisted of the senior resident inspector, three resident inspectors, a project manager (for TMI-2), and a secretary.
During this ceriod, Region I isst.ed the following inspection reports.
OFFICIAL RECORD C0pY TMI STATUS REPORT - 0005.0.0 11/29/80
e Enclosure 4 TMI-1 (50-289) 88-16 on October 24, 1988, addressing various engineering / technical sup-port outstanding inspection findings. In the cover letter of that report, the NRC staff addressed a concern, which the licensee committed to re-solve, about the potential for overloading an emergency diesel generator.
88-17 on October 17, 1988, addressing the special (outage) team inspec-tion conducted August 8-19, 1988. The NRC staff identified two apparent violations: failure to adequately establish procedures in the operations and maintenance areas and failure to properly change maintenance proce-dures. The licensee had until November 17, 1988, to respond. Overali, the team concluded chat outage activities were conducted in a technically competent fashion.
88-18 on October 12, 1988, addressing routine power operations and the transition period for plant start-up from the last re'ueling outage.
Two apparent violations were identified: exceeding the cooldowo limits for the pressurizer and failure to adhere to low pressure protection limits for the RCS (no licensee response is required) and failure to properly review and approve a change to a maintanance procedure. The licensee had until November 12, 1988, to respond to thc latter violation.
In the cover letter of that report, the NRC staff provided an overall favorable conclusion on the licensee's performance, noting some areas of improvement needed.
88-23 on October 14, 1988, addressing the licensee's fire protection program. No violations were identified.
88-25 on October 14, 1953, addressing the licensee's corporate engineer-ing support functions for TMI-1 (and Oyster Creek). No violations wire identified.
TMI-2 (50-320) 88-14 on October 28, 1988, addressing routine TMI-2 defueling/decon-tamination activities. No violations were identified.
During October 18-19, 1938, the Office of Nuclear Reactor Regulation (NRR) had a team on site to review the licensee-submitted Probabilistic Risk An-alysis (FRA) for THI-1.
During the week of October 31, 1998, NRR had a team at the corporate head-quarters and at the site to review selected licensee actions with respect to improvenents in the instrumentation and control functional areas at TMI-1.
A report will be issuec at a later date, t
OFFICIAL RECORD COPY TMI STATUS REPORT - 0006.0.0 11/29/80
Enclosure 5
- 4. Public Meetings On October 25, 1988, che members of the Advisory Panel on the Decontamination of THI-2 met with the NRC Commissioners. Arthur Morris, chairman of the p&nel and mayor of Lancaster, Pennsylvania, reported the panel's 8-2 vote against Post-Defueling Monitored Storage (PDMS). The panel members discussed their reasons for opposing PDMS. They primarily were the uncertainties in ultimate clean-up and decommissioning funding and the uncertainties in the time the facility would be in a POMS state. The next Advisory Panel meeting will be in early 1989; specifics regarding time and place will be announced in a future monthly st tus report, as well as routine news releases.
The At Mic 'afety and Licensing Board (ASLB) hearings on the disposal of accide it genec + i water ( AGW) at TMI-2 were held on October 31 - November 4,10's8, in Lar >,cer, Pennsylvania. They included an evening session on Nov aber 3, 1988, in which limited appearances were made by members of the
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p tz' l i c . The hearings are scheduled to be completed on November 15, 1988, in P,thesda, Maryland.
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i 0FFICIAL RECORD COPY TMI STATUS REPORT - 0007.0.0 !
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