ML20153C545

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Insp Repts 50-413/88-25 & 50-414/88-25 on 880626-0725. Violations Noted.Major Areas Inspected:Plant Operations, Surveillance & Maint Observations,Review of LERs & Followup of Previously Identified Items & NRC Bulletins
ML20153C545
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 08/19/1988
From: Lesser M, Peebles T, Van Doorn P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20153C521 List:
References
50-413-88-25, 50-414-88-25, NUDOCS 8809010174
Download: ML20153C545 (11)


See also: IR 05000413/1988025

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UNITED STATES

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NUCLEAR REGULATORY COMMIS210N

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101 MARf ETTA STREET, N.W.

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ATL ANTA, GEORGI A 30323

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Report Nos. 50-413/88-25 and 50-414/88-25

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Licensee: Duke Power Cc:npany

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.: 50-413 and 50-414

License Nos.: NPF-35 and NPF-52

Facility Name: Catawba 1 and 2

Inspection Conducted: June 26, 1988 - July 25, 1988

Inspectors:,

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'P. K. Van 00 rn

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Date/ Signed

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Approved by:

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T % Pebbles, Section Chief

D' ate Signed

Projects Branch 3

Division of Reactor Projects

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SUMMARY

Scope:

This routine, resident inspection was conducted on site inspecting in

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the areas of review of plant operations; surveillance observation;

maintenance observation; review of licensee nonroutine event reports;

followup of previously identified items; and followup of NRC

Bulletins.

Results: The inspection findings indicate a weakness in the management of

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Technical Specification compliance.

A strength was noted in the

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establishment and use of an on-site design engineering staff.

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second strength was noted in the establishment of station specific

performance indicators with specified goals.

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In the areas inspected, the following violations were identified:

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Failure to maintain two operable channels of valve position

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indication for PORY F: lock Valves (para. 7.c)

Inoperability of containment purge valves due to use of fused

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jumperr (para. 6.b).

This violation is classified as a Licensee

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IdentifiedViolation(L!V).

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

H. B. Barror,, Operations Superintendent

W. F. Beaver, Performance Engineer

W. H. Bradley, QA Surveillance

  • R. N. Casler, Unit 1 Coordinator

R. H. Charest, Station Chemistry Supervisor

T. E. Crawford, Integrated Schedultng Superintendent

W. P. Deal, Health Physics Supervisor

R. M. Glover, Compliance Engineer

  • T. P. Harrall, Design Engineering-

F. N. Mack, Project Services Engineer

W. W. McCollough, Mechanical Maintenance Supervisor

  • W. R. McCollum, Staticn Services Superintendent

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C. E. Muse, Unit 2 Coordinator

  • T. B. Owen, Station Manager
  • C. T. Smith, Maintenance Superintendent

J. M. Stackley, 1, & E. Envineer

D. Tower, Shift Operating Engineer

R. /. Wardell, Technical Services Superintendent

  • R. Whit 6, CSRG Chairman

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J. W. Willis, Senicr QA Engineer, Operations

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

NRC Resident inspectors

  • P. K. Van Doorn
  • M. S. Lerser
  • Attended exit interview.

2.

Unresolved Items

An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation. There were

no unresolved items identified in this report.

3.

Plant Operations Review (71707 cnd 71710)

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a.

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements. Technical

Specifications (TS), and administrative controls. Control room logs,

danger tag logs, Technical Specification Action Item t.og, and the

removal and restoration log were routinely reviewed.

Shift turnovers

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were observed to verify that they were conducted in accordance with

approved procedures.

The inspectors verified by observation and interviews, that the

measures taken to assure physical protection of the facility met

current requirements.

Areas inspected included the security

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organization; the establishment and maintenance of gates, doors, and

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isolation zones in the proper conditions; and that access control and

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badging were proper and procedures followed.

In addition to the areas discussed above, the areas toured were

observed for fire prevention and protection activities.

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included such things as combustible material control, fire protection

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systems and materials, and fire protection associated with

maintenance activities.

The inspectors reviewed Problein

Investigation Reports to determine if the licensee was appropriately

documenting problems and implementing appropriate corrective actions.

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b.

Unit 1 Summary

The Unit continued its current run of 133 days of continuous

operation and achieved one year without an automatic trip above 15%

power.

On July 19, sulfate contamination of the steam generators

occurred when a valve isolating the demineralized makeup water system

from a regenerating demineralizer leaked by, causing sulfuric acid to

be injected into the condensate system. The unit was reduced to 30%

power, although not expeditiously due to misunderstanding of written

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procedures.

The sulfates were cleaned up within a day and the unit

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returned to full power,

c.

Unit 2 Suninary

The Unit started the reporting period at 100% power and tripped on

June 26 when an operator misinterpreted a test procedure step and

shut one Main Steam Isolation Valve.

The unit later restarted,

however, it was forced to shutdown on July 16 when an action

statement expired on the 2A centrifugal charging pump (see paragraph

5.c.).

The unit started up on July 21.

Power escalation was

hampered by problems with the steam dumps and turbine control valves

hydraulics.

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d.

Based upon an event at another facility where unexpectedly high

radiation levels in the reactor building forced evacuation of site

personnel, the inspector asked the licensee whether reportability

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procedures adequately covered events which significantly hamper site

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personnel in the performance of duties necessary for the safe

operation of the plant.

Although this type of event was covered by

procedure RP/0/B/5000/13 the licensee agreed that the procedure could

be improved and has initiated a change to affect this improvement.

No violations or deviations were identified.

4.

SurveillanceObservation(61726)

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a.

During che inspection period, the inspector verified plant operations

were in compliance with various TS requirements.

Typica; of these

requir2ments were confirmation of compliance with the TS for reactor

coolart chemistry, refueling water tank, emergency power systems,

safety injection, emergency ' safeguards systems, control room

vent 116 tion, and direct current electrical power sources.

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inspector verified that surveillance testing was performed in

accordance with the approved written procedures, test instrumentation

was calibrated, limiting conditions for operation were met,

appropriate removal and restoration of the affected equipment was

accomplished, test results met requirements and were reviewed by

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personnel other than the individual directing the test, and that any

deficiencies identified during the testing were properly reviewed and

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resolved by appropriate management personnel.

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b.

The inspectors witnessed or reviewed the following surveillances:

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IP/1/A/3222/000

Channel IV Analog Channel Operations Test

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PT/1/A/4200/09A

Auxiliary Safeguards Test Cabinet Pericdic

Test'

PT/2/A/4200/14/A

Ice Condenser Intermediate Deck Door and

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Inlet Door Position Monitor

PT/2/B/4150/29

Containment Floor and Equipment Drain Sumps

Increase Test

No violations or deviations were identified.

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5.

MaintenanceObservations(62703)

a.

Station maintenance activities of selected systems and components

were observed / reviewed to ascertain that they were conducted in

accordance with the requirements.

The inspector verified licensee

conformance to the requirements in the following areas of inspection:

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the activities were accomplished using approved procedures, and

functional testing and/or calibrations were performed prior to

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returning components or systems to service; quality control records

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were maintained; activities performed were accomplished by qualified

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personnel; and materials used were properly certified. Work requests

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were reviewed to determine status of outstanding jobs and to assure

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that priority is assigned to safety-related equipment maintenance

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which may effect system perfonnance.

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b.

The inspectors witnessed or reviewed the following maintenance

activities:

MP/0/A/150/81

Nuclear Service Water Lube Injection

Strainer Corrective Maintenance

89725WR

Replace KF Filter 2B

MP/0/A/7150/16

Repair 2A NV Pump

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c.

On July 13 operators observed decreasing pressurizer level, charging

flow decreasing from 87 to 50 gpm and increasing VCT level on Catawba-

Unit 2.

The problem was quickly diagnosed to the operating 2A

Centrifugal Charging Pump (NV) and operators recovered from the

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transient by starting the other pump. The licensee initially assumed

gas binding and initiated actions to vent the pump after declaring it

inoperable.

A later attempt to operate the pump resulted in

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significantly reduced flow (25 gpm) and smoke was observed in the

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vicinity of the inboard bearing.

The licensee determined that

disassembly of the pump and replacement of the rotating element was

necessary.

The rotating element was replaced under work request 41005 OPS with a spare rotating element with a similar shop head

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curve.

The new element was retested after installation.

At the

reference operating point of 88 gpm the pump exhibited a head of

approximately 85 psig lower than the head of the old pump.

The

licensee obtained an evaluation by Westinghouse with results

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documented in letters dated July 15, 1988 to T. F

Wyke from

S. S. Kilburn and July 19, 1988 to R. Puryear from Dan Dudek and

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Steve Swanther.

The evaluation concluded that the' flow

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characteristics of the system were not materially altered and the

pump will operate adequately under runout conditions. The inspectors

performed independent calculations to verify the results.

The root

cause for failure of the pump has not been determined.

Disassembly

of the old rotating element has revealed indications of excessive

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internal pump recirculation.

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No violations or deviations were identified.

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6.

Review of Licensee Non Routine Event Reports (92700)

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a.

The below listed Licensee Event Reports (LER) were reviewed to

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determine if the information provided met NRC requirements.

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determination included: adequacy of description, verification of

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compliance with Technical Specifications and regulatory requirements,

corrective action taken, existence of potential generic problems,

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reporting requirements satisfied, and the relative safety

significance of each event.

Additional inplant reviews and

discussion with plant personnel, as appropriate, were conducted for

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those reports indicated by an (*).

The following LERs are closed:

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413/87-45

Technical Specification Violation due to

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inadequate procedural

guidance and a

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personnel error.

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413/88-03 Rev. 1

Technical Specification Violations on Wide

Range Temperature Monitoring Instrumentation

due to Installation and Design'0eficiencies.

413/88-20

Technical Specification Violation involving

Pressurizer PORV's and Associated Block

Valves Position Indication.

b.

On December 8.1987, the licensee determined that the Containment

Purge (VP) system had been inoperable in September 1986 during core

alterations in that Train B would not have isolated on a high

relative humidity condition as required by TS 4.9,4.1.b.

The reason

for the inoperability was that a set of fused jumpers used for

troubleshooting were never removed.

The jumpers were used without

declaring the system inoperable or without performing a 10CFR50.59

evaluation.

The licensec reported the inoperability in LER

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413/87-45. Corrective action included requirements in IP/0/A/3890/01

Controlling Procedure for Troubleshooting and Corrective Maintenance,

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for technicians to consult with engineers prior to using fused

Jumpers and precautions of instrument loop inoperability when using

fused jumpers to troubleshoot intermittent electrical faults.

Appropriately a Notice of Violation is not proposed as permitted by

Appendix C of 10CFR2 and this event is classified as a Licensee

Identified Violation 413/88-25-02.

Inoperability of Containment

Purge Valves due to use of fused jumpers.

One licensee identified violation as described above was identified.

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Follow-uponPreviousInspectionFindings(92701and92702)

a.

(Closed)

Violation 413/87-30-01:

Unauthorized Isolation of an

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Auxiliary Feedwater Pressure Switch rendering the Auxiliary Feedwater

System unable to function as designed under certain conditions. The

licensee responded to the violation in correspondence dated

December 31, 1987.

Corrective action included review, revision and

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implementation of safety related instrumentation valve lineups done

after extended outages, increased guidance upon identifying

instrument valves out of position and training.

Based upon these

corrective actions this item is closed.

b.

(Closed)

Violation 413,414/87-30-02:

Failure to establish adequate

measures to periodically calibrate all safety related instruments.

The licensee responded to the violation in correspondence dated

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November 13, 1987 and December 28, 1988.

Correc'tive action included

identification and completion of instrument calibrations that had not

yet been done, evaluation of those instruments discovered to be out

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of tolerance, and development of administrative guidance to ensure

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instrumentation added by modifications is identified in the periodic

calibration program.

Based upon these corrective actions this item

is closed.

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c.

(Closed)

Unresolved Item 413, 414/87-33-01:

Two channels of valve

position indication for PORV's and PORV block valves not installed as

required by TS 3.3.3.6.

TS 3.3,3.6 requires 2 channels of . valve

position indication for each pressurizer PORV and PORY block valve.

The licensee's use of- a non-safety related strap on resistance

temperature defector (RTO) as the second channel for the PORV

position indication was deemed acceptable by the NRC:

The licensee

Fowever failed to maintain 2 channels per PORY block valve operable

from initial licensing until May 20, 1988 at which time the channels

were declared inoperable and a seven day action s?,atement was

entered.

At this time the licensee determined that an independent

position indication for each block valve was available at the test

patch panel and initiated action to verify operability. .The licensee

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was unable to obtain operable channels on Unit 2 without entering .

containment.

To avoid an unnecessary shutdown, the licensee

requested an uergency TS change for Unit 2 to require only one

operable channel. The request was granted and issued as amendment 39

for Unit 2, effective May 27, 1988.

This is identified as a

violation of TS 3.3.3.6, violation 413,414/88-25-01:

Failure to

maintain two operable channels of valve position indication for PORY

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block valves.

This violation has minor safety significance as the

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basis f6r the Technical Specification (Regulatory 1.97 and TM1-2

Action Plan Item II. D.3) indicates that one channel per. valve may be

acceptable.

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d.

(0 pen) Unresolved Item 413.414/88-22-03:

Potential Inadequate

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Venting of ECCS Systems.

The inspectors reviewed change 7 ~ to

PT/2/A/4200/06 and change 11 to PT/1/A/4200/06, (implemented June 30,

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1988) ECCS Valve Lineup Verification which includes actions to meet

monthly T.S. requirements to vent discharge piping of ECCS systems.

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As a result of the inspector's questions concerning adequacy of

vanting, one vent valve in each train was identified to be,at a

higher elevation and~therefore a better valve to ensure the systen is

water solid.

The licensee was previously using the highest vent

valve in the flowpath but not the system high point.

The inspectors reviewed PT/2/A/4200/10A, ND Pump 2A Performance Test

conducted on Febrcury 1, 1988.

Horizontal vibration readings of the

pump were noted to fall into the alert range as defined by Table

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IWP-3100-2 of section XI of the ASME ?ailer and Pressure Vessel Code.

The problem was corrected when the pump was adequately vented. The

Nnspectors determined the the licensee does not have written

procedures for fill and vent of safety related systems. The licensee

stated that typically a system or component would be isolated with a

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RemovalandRestoration(R&R). The R&R defines the boundaries and is

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also used to fill and vent the system.

This item remains open

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pending continued review of ECCS venting and apparent requirements by

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T.S. 6.8.1 and Regulatory Guide 1.33 to have and maintain written

procedures for system fill and vent.

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(Closed) Unresolved Item 414/86-38-01:

No Criteria Established for

Documentation of Reverification of Reperformance of Station Status

and Prerequisites of Interrupted Tests.

The licensee has addressed

this issue via Revision 9-to Station Directive 3.2.2, Development and

Conduct of the Periodic Testing Program.

This change adequately

addresses this concern and no significant problems were identified as

a result of the weakness. Therefore, this item is closed.

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(Closed) Inspector Followup Item 413/86-05-01:

Revise Station

Directive 3.2.2.

Revision 9 to the Station Directive (SD) has been

issued which addresses notification of the Shift Supervisor when a

test is not completed within the allowed TS interval.

This

adequately addresses the NRC concern.

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(Closed) Inspector Followup Item 413/86-36-01, 414/86-39-01:

Revision of SD 3.2.2 to clarify administrative controls for test

interruption.

SD 3.2.2 has been appropriately revised,

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(Closed) Inspector Followup Item 413/87-30-04:

Evaluation of

Subcooling Nuisance Alarm.

The licensee has evaluated the setpoint

for the alarm and has raised the setpoint by 3'F thereby elimincting

the nuisance alarm,

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(Closed) Inspector Followup Item 413,414/88-08-03;

Upgrade Program

For Use of Jumpers to Operate M0V's. Tha licensee added centrols to

troubleshoot motor operated valves to IP/0/A/3890/01, Controlling

Procedure for Troubleshooting and Corrective Meintenance.

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procedure requires

troubleshooting to be conducted under

IP/0/A/3820/04, Operating Checkout of Limitorque and Rotork Valve

Actuators or IP/0/A/3820/07

Troubleshooting and Maintenance of

Rotork Actuators.

Procedures now require consultation with

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operations and/or Technical Support pe sonnel when bypassing

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interlocks, permissives, automatic functions, and torque / limit

switcher during troubleshooting.

Additional precautions must be

taken to ensure a moto: does not reach stall torque situations.

A specialized training package, Basic Troubleshooting and Corrective

Muintenance Guidelines for Motor Operated Valve Actuators has been

genermd and is to be incorporated into the station personnel

training program.

Based on this the item is closed.

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(Closed) Inspector Followup Item 413,414/88-15-01:

Inoperable RN Pit

Level Transmicters Interpretation Implementation.

The licensee

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comitted to writing a procedure to implement an interpretation of TS 3.3.2 item 149 concerning operability of RN pit level transmitters,

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The procedure has been implemented as enclosure 4.15 of

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OP/0/A/6400/06C, Nuclear Service Water System.

The enclosure

specifies actions to be taken in the event of an inoperable

transnitter to ensure that the actions are at leut as conservative

as the instrument's automatic actions.

Sased upon the inspectors

review of the enclosure this item is closed.

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(0 pen) Inspector Followp Item 413,414/88-15-03:

Changes in RHR

Operation with Low Flow Annunciators.

The inspector reviewed

enclosure 4.1 of Revision 9 of OP/1(2)/A/6200/04, Residual Heat

Removal System (ND).

The change requires that the ND cross connect

valves be isolated when the system is used for routine decay heat

removal.

This ensures that with the reactor coolant system filled,

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normal ND flow rates will not result in a low flow alarm.

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licensee has also initiated a Station Problem Report (SPR CNPR03449)

to reduce the setpoint of the low flow annunciator, such that it will

not be in alarm when a lower flow is required during reactor coolant

draining operations,

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While reviewing the change, the inspector noted that NI-173 and

NI-178 (ND pump discharge isolation valves to the cold legs) are

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simultaneously shut in order to recirculate flow and obtain boron

concentration samples.

This makes both trains of ND isrperable, as

TS 3.5.3 requires at least one train's valve to be open.

In the past

the unit has unknowingly been placed S ou action statement, however,

there is no evidence that the licensee had ever violated the action

statement.

The licensee has stated it would be prudent to isolate

one train at a time for sampling and has agreed to revise the

procedure.

8.

Followup of NRC Bulletin 88-05(92701)

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As a result of inspections directed by NRC Bu11etin 88-05, Non Conforming

Materials Suppled by Piping Supplies. Inc. u Folsom, New Jersey and West

Jersey Manufacturing Company at Williamstcwn, New New Jersey.

The

licensee was to date identified 10 non conforming socket weld flanges.

The systems involved include Steam Supply to the Auxiliary Feedwater Pump

Turbine, Diesel Generator Air Start, Auxiliary Feedwater and Main

Feedwater.

Proper notification to the NRC have been made in'each case.

The licensee is performing an analysis in each case to justify continued

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operation.

No violations or deviations were identified.

9.

Licensee Weakness Regarding Management of Technical Specification

Compliance

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The licensee has had a history of difficulties in complyirg with Technical

Specifications (TSs) at Catawba Nuclear Station.

The cause of this

problem is, in part, weaknesees in the original TS review which resulted

in some TSs which were unclear, some which did not meet plant design, and

some where ;ompliance with the letter of TSs goes beyond the intent of or

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the basis for the TS. Licensee personnel, on occasion, have chosen not to

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follow the letter of TSs while meeting intent or safety aspects.

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Confusing TSs have led to personnel errors.

The number of TS changes that

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are able to be processed in a given time period by NRC due to Federal law

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and the licensee due to manpower makes it difficult to affect all changes

necessary in a timely manner.

For example 41 amendments were processed in

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1987 and to date, 28 amendments have been proce: sed in 1988.

Changes

which suppart clarifications and improvements in complying with intent

appear to have a low priority since these are in competition with the

necessary changes such as those which support upcoming modifications.

This typically leads to delays between when the need for _the changes is

identified and submittal to NRC of 7 months and greater, up to 2 years.

The licensee uses a TS Interpretation Manual to provide guidance and also

has procedure guidance relative to support systems required for

operability of TS systems.

Use of the manual has typically been reactive

rather than proactive and some interpretations have been made without use

of the manual.

Issuance of guidance has not always been timely.

Issues

which illustrate this weakness are as follows:

Control Room Ventilation - instrumentation in TS did not meet plant

design. TS has been changed.

original TS was excessively

Auxiliary Building Ventilation

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restrictive, i.e. 24-hour action in lieu of 7 days.

Caused by poor

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review and resulted in several discretionary enforcement actions

before TS was finally changed.

D.C. Power Sources (TS 3.8.2.1) - action e, is poorly worded. This

has lead to confusion surrounding entering TS 3.0.3 (see LER 413/87-32 and NRC Report 413,414/87-33).

An interpretation has been

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issued but the poor wording remains.

Violation 414/87-05-05(LER414/87-05)- corporate personnel issued a

TS interpretation allowing site personnel 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to isolate a

containment isolation valve in lieu of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> required by TS 3.6.3.

Violation 414/87-25-01 - licensee inappropriately took credit for

pegged high gauges for channel checks of Auxiliary Feedwater System

flow instruments.

Unit 2 design results in normally pegged high

gauges requiring special methodology to meet standard TS.

Violation 414/87-30-01 - power range neutron flux trip setpoint was

not evaluated by corporate personnel in accordance with the equation

required by TS 2.2.1.

Auxiliary Feedwater valves were

Violation 413/414/87 44-01

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throttled when TS requires the valves to be fully open.

No TS

interpretation was issued although operations personnel had

interpreted the intent of the TS to allow this operations mode. The

need for this TS to be changed was recognized by the licensee in

November 1986, and was not submitted to NRC until February 1988.

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Violation 414/87-44-03 - a confusing TS for the shared Control Room

Ventilation contributed to both trains being inoperable from

emergency power for a period of time.

The licensee recognized the

need for changing this TS in December 1987 and the request has not

yet been submitted to NRC.

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Violation 414/87-88-07 - licensee used unqualified instrumentation to

compensate for inoperable acoustic monitors for pressurizer safety

valves.

TS uses the term valve position indication with no

amplifying information.

Violation 413,414/88-25-01 - two channels of pressurizer PORV block

valve position indications were not available per TS which were also

a standard TS.

Corporate personnel indicated to site personnel that

two indications rather than two separate channels were acceptable and-

met basis for TS rather than requiring compliance with the letter of

the TS. This issue was raised in late 1987. An emergency change was

granted for Unit 2 in May 1988 and additional changes for Unit 1

block valves and PORV position indicators are yet to be submitted to

NRC.

LER 413/88-13 - both trains of Containment Spray were made legally

inoperable.

A poorly written TS contributec to this problem.

The

need for a TS change was recognized in December 1987 and is yet to be

submitted to NRC.

Unresolved Item 413/86-17-01 - licensee chose not to follow letter of

TS and does not vent pump casings of running pumps while taking

credit for the surveillance which requires venting.

Although the

exemption appears to be technically reasonable, the licensee has yet

to submit a TS change request to NRC.

While these situations are not individually significant, TS non-compliance

can lead to significant problems,

Licensee management has recognized the

need for inprovement in this area and reformatting of operator guidance

information is in progress.

The licensee indicated that this issue will

be further reviewed to determine the need for additional corrective

actions.

Further followup will be conducted in this area by the RI. This

is Inspector Followup Item 413/88-25-03: Weakness Regarding Management of

Technical Specification Compliance.

10. Licensee Strengths

a.

The licensee has completed staffing of an on-site Design Engineering

(D/E) group.

This group is providing more timely response to issues

involving D/E and providing a more thorough understanding of the

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issue. Several interfaces with this group by the inspectors has been

beneficial.

The presence of this group is considered to be a

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strength.

b.

The licensee had recently established a site Performance Indicator

,

Program.

Indicators have been established for material conditions,

modification backlog, comitment index, personnel exposure, people

performance (errors), cost per kilowatt-hour, safety system

unavailability, gross equivalent availability factor, preventive to

corrective maintenance ratio and work request backlog.

Challenging

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