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Category:ENVIRONMENTAL REPORT
MONTHYEARML20204G2301999-03-18018 March 1999 Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20202G4631999-02-0202 February 1999 Rev 0 to PGE-1076, Trojan Reactor Vessel Package SAR, Environ Rept ML20151X7451998-09-10010 September 1998 Rev 3 to PGE-1063, Trojan Nuclear Power Station,Suppl to Applicant Environ Rept ML20135B3021996-11-27027 November 1996 Rev 2 to Trojan Nuclear Power Station,Suppl to Applicant Environ Rept 1999-03-18
[Table view] Category:ALL VERSIONS
MONTHYEARML20204G2301999-03-18018 March 1999 Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20202G4631999-02-0202 February 1999 Rev 0 to PGE-1076, Trojan Reactor Vessel Package SAR, Environ Rept ML20151X7451998-09-10010 September 1998 Rev 3 to PGE-1063, Trojan Nuclear Power Station,Suppl to Applicant Environ Rept ML20135B3021996-11-27027 November 1996 Rev 2 to Trojan Nuclear Power Station,Suppl to Applicant Environ Rept 1999-03-18
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20211B4501999-08-16016 August 1999 Environ Assessment & Finding of No Significant Impact Re Proposed Action That Would Exempt Util from Security Requirements of 10CFR50.54(p) & 10CFR73.55 & Delete Requirements for Security Plan from 10CFR50 ML20211A7221999-08-16016 August 1999 Environ Assessment & Finding of No Significant Impact Re Issuance of Amend to FOL NPF-1.Proposed Action Would Exempt Util from Emergency Plan Requirements of 10CFR50.54(q), 10CFR50.47(b) & 10CFR50,App E ML20206E0391999-04-28028 April 1999 Environ Assessment & Finding of No Significant Impact Re 970212 Application for Amend.Proposed Amend Would Revise Permanently Defueled TS by Revising Subsection 4.1.1, Replacing Figure 4.1-1 & Adding New Page to Figure 4.1-1 ML20204G2301999-03-18018 March 1999 Rev 4 to PGE-1063, Suppl to Applicants Environ Rept - Post Operating License Stage ML20202G4631999-02-0202 February 1999 Rev 0 to PGE-1076, Trojan Reactor Vessel Package SAR, Environ Rept ML20205P7351998-12-31031 December 1998 Operational Ecological Monitoring Program for Trojan Nuclear Plant,Jan-Dec 1998 ML20205S9851998-12-31031 December 1998 Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY98 ML20206D3231998-12-31031 December 1998 PGE-1065-98, Trojan Nuclear Plant Radioactive Effluent Release Rept for 1998. with ML20151X7451998-09-10010 September 1998 Rev 3 to PGE-1063, Trojan Nuclear Power Station,Suppl to Applicant Environ Rept ML20236Y2851998-08-0808 August 1998 Trojan Nuclear Plant,Sar for Rv Package Environ Rept ML20217D6321997-12-31031 December 1997 Trojan Nuclear Plant Annual Radiological Environ Monitoring Rept for 970101-1231 ML20217H4731997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for Trojan Nuclear Plant for 1997 ML20212H3951997-12-31031 December 1997 Operational Ecological Monitoring Program for Trojan Nuclear Plant,Annual Rept for 1997 ML20217K3991997-10-21021 October 1997 NPDES Noncompliance Notification:On 970906,pH Lower Limit of 6.0 at Discharge & Dilution Structure Was Exceeded.Caused by Workers Rinsing Sodium Bisulfite Barrels Into Outfall.Wrote Procedure to Require Barrel Rinsing Into Floor Drain Sys ML20141D8861997-06-24024 June 1997 Rev 0 to Trojan ISFSI Environ Rept ML20148K3661997-06-0202 June 1997 Environ Assessment & Finding of No Significant Impact Re Issuance of License Amend to possession-only License NPF-1. Proposed Action Would Allow Processing of Fuel & Debris in Plant Bldg as Described in from Licensee ML20137B3181997-03-17017 March 1997 NPDES Noncompliance Notification:On 970225,pH Lower Limit of 6.0 at Discharge & Dilution Structure Exceeded for Approx Ten Minutes.Caused by Inadvertent Discharge of Excess of Sodium Bisulfite.Will Review Drum Rinsing Process ML20136D5761997-03-0606 March 1997 Environ Assessment & Finding of No Significant Impact Re Order Approving Application Involving Proposed Merger of Holding Company for Portlans General Electric Co & Enron Corp ML20137Z4761996-12-31031 December 1996 Trojan Nuclear Plant,Radiological Environ Monitoring Rept for CY96 ML20140D7651996-12-31031 December 1996 Operational Ecological Monitoring Program for Tnp Annual Rept for 1996 ML20138A7681996-12-31031 December 1996 Radioactive Effluent Release Rept for 1996 ML20135B3021996-11-27027 November 1996 Rev 2 to Trojan Nuclear Power Station,Suppl to Applicant Environ Rept ML20137M9121995-12-31031 December 1995 Annual Radioactive Effluent Release Rept for Trojan Nuclear Plant for 1995 ML20058L5971993-11-12012 November 1993 Notice of Environ Assessment & Finding of No Significant Impact Re Consideration of Issuance of Exemption from 10CFR50.120 ML20058A6261993-11-12012 November 1993 EA & Fonsi Re Licensee 930708 Request for Exemption from Requirements of 10CFR50.54(w) Which Requires Utils to Maintain Min of $1.06 Billion of Decontamination Insurance Coverage for Radiological Accident at Reactor Site ML20058M7051993-09-27027 September 1993 Environ Assessment & Finding of No Significant Impact Re Licensee Request for Exemption from 10CFR73.55 Requirements Concerning Physical Protection in Nuclear Power Reactors for Plant ML20057D9981993-09-27027 September 1993 Environ Assessment & Fonsi Granting Licensee Request for Exemption from Portions of 10CFR50.54(q) That Apply to Operating Plants & to Certain Emergency Preparedness Requirements of 10CFR50.47 & 10CFR50 App E ML20056F9951993-06-30030 June 1993 Semiannual Radioactive Effluent Release Rept Jan-June 1993 ML20126F3401992-12-18018 December 1992 Environ Assessment & Finding of No Significant Impact Re One Time Schedular Exemption from Requirements of 10CFR50, App E ML20059D6251990-06-30030 June 1990 Semiannual Radioactive Effluent & Waste Disposal Rept for Jan-June 1990 ML20246F5481989-08-23023 August 1989 NPDES Noncompliance Notification:During Jul 1989,biochemical Oxygen Demand Limit in Sewage Treatment Plant Effluent Exceeded.Main Plant Outfall Ph & Chlorine Monitors Remained Out of Svc During Entire Month Due to Sample Pump Failures ML20246M2481989-07-31031 July 1989 Final Discharge Monitoring Rept for Jul 1989 ML20246K0031989-06-30030 June 1989 Semiannual Radioactive Effluent & Waste Disposal Rept Jan- June 1989 ML20247R7191989-06-0101 June 1989 Environ Assessment & Finding of No Significant Impact Re Mods to control-auxiliary-fuel Bldg Complex ML20247K5701989-05-25025 May 1989 NPDES Noncompliance Notification:During Apr 1989,limit for Flow from Settling Basin Exceeded.Water from Circulating Water Sys Drained Into Recreation Lake from 890409-10.On 890414,high Flow for Daily Settling Basin Noted ML20246P5911989-05-16016 May 1989 Notice of Environ Assessment & Finding of No Significant Impact Re 871120,880527 & 0812 Applications to Change Tech Specs Re Use of New Fuel Design ML20244C4061989-04-30030 April 1989 NPDES Discharge Monitoring Rept for Apr 1989 ML20235K3951989-01-31031 January 1989 Cultural Resource Investigation Series 1, Archaeological Evaluation of Trojan Locality 35C01 ML20245E8801988-12-31031 December 1988 Trojan Nuclear Plant Operational Environ Radiological Surveillance Program 1988 Annual Rept ML20245K6501988-12-31031 December 1988 Operational Ecological Monitoring Program for Trojan Nuclear Plant,Annual Rept 1988 ML20247M9951988-12-31031 December 1988 Amend 1 to 1988 Operational Environ Radiological Surveillance Program Annual Rept,Revising Section 4.4 Re Monitoring Program Problems & Corrective Action ML20207K2111988-09-26026 September 1988 Environ Assessment & Finding of No Significant Impact Supporting Exemption from 10CFR50.54(w)(5)(i) Requirements Re Amount of Onsite Property Insurance Required to Be Carried by NRC Reactor Licensees ML20154B7751988-08-30030 August 1988 Forwards Rept of Violations of NPDES Permit During Jul 1988. Violations Involved Exceeding Limits for Biochemical Oxygen Demand & Suspended Solids in Sewage Plant Effluent ML20153F1541988-06-30030 June 1988 Semiannual Radioactive Effluent & Waste Disposal Rept,Jan- June 1988 ML20151L7891988-03-31031 March 1988 Monthly NPDES Data for Mar 1988 ML20147E4741988-01-11011 January 1988 NPDES Noncompliance Notification:On 871209,sewage Treatment Plant Effluent Max Daily Limit of 6.3 Lb Bod Exceeded W/ Discharge of 9 Lb.Caused by High Influent Flow Rates from Inleakage. Discharge Monitoring Rept,Dec 1987 Encl ML20151Y6311987-12-31031 December 1987 Operational Environ Radiological Surveillance Program 1987 Annual Rept ML20147G2871987-12-31031 December 1987 Discharge Monitoring Rept,Dec 1987 ML20236M8981987-10-27027 October 1987 Environ Assessment & Finding of No Significant Impact Supporting Exemption from Section Iii.G of App R of 10CFR50 Re Fire Protection of Equipment Important to Safe Shutdown ML20235Y8781987-10-14014 October 1987 Forwards NPDES Rept for Sept 1987 & Addl Required Data.Plant Maintained Power Generation Through Month Until Unscheduled Shutdown on 870928 1999-08-16
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1 PGE-1063 Portland General Electric Supplement to Applicant's Environmental Report 1
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Post Operating License Stage Trojan Nuclear Power Station Revision 3 9809170232 980910 PDR
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W ADOCK 05000344 PDR
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l List of Effective Pages !
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Page Number Revision Title page - September 1998 Executive Sumary Original li through iv Original
.v September 1998 l 1 through 3 Original Figure 2.2-1 and 2.2-2 Original
' 4 through 9 Original Figure 2.3-1 through 2.3-3 Original l 10 and 11 Original L
Figure 2.4-1 through 2.4-3 Original l
- l. 12 through 14 Original t.
l Figure 2.5-1 through 2.5-3 Original ,
l 15 Original l 16 and 17 September 1996 18 November 1996 l Figure 3.2-1 November 1996 19 through 22 Original 23 September 1998 24 through 35 Original i-f l
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,yl' EN11RONMENTAL REPORTSUPPLEMENT- POST OPERA TING LICENSE STAGE The plant's once through cooling system remains in service to provide makeup water for the I spent fuel storage pool. The shutdown of the plant has greatly reduced the demand for water l from this system. Chlorination of this system (and the neutralization of the residual chlorine) I continues at this time. The impact of this chlorination on the water discharged to the Columbia River is reduced from previous levels, however, due to the reduced flow requirements.
Discharges originating from blowdown of the reactor coolant system and miscellaneous steam leaks and drains from the plant secondary system have also been eliminated as a result of the I permanent shutdown of the plant.
With the plant permanently defueled, the water use is less than when the plant was operating. l Water is drawn from two wells on site and the Columbia River. The estimated maximum usage l from the wells is 26,925 gpd for potable water and for the demineralized water system, with plans to use an additional 43,200 gpd for potable water, backup fire protection, and air compressor bearing cooling water. The estimated maximum plant usage from the Columbia River is 42,600 gpm (40,000 gpm for the service water system,2,000 gpm for the fire system, and 600 gpm for the screen wash system).
The daily average minimum flow of the Columbia River at Trojan is approximately 120,000 ,
cubic feet per second. The discharge is at the bottom of the river in a manner providing an l average 120-fold dilution by the time the effluent reaches the river surface. Further dilution of
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the discharge occurs rapidly in the river. Within 12,000 feet of the discharge, complete mixing is j expected. i The original Trojan environmental report noted that chemicals from the plant, after dilution by river water, would cause only a slight increase in the concentration of elements and compounds which already existed in the river. The report concluded that the waste discharge from the Trojan plant would have a negligible effect on the chemical composition of the Rainier drinking water and cause no adverse effects on human health from this source. The report also concluded that chemical wastes from Trojan would have a negligible biological impact on the environment of the Columbia River or on the area surrounding the plant. These conclusions have subsequently been supported by the continuing monitoring of the environment in the vicinity of Trojan. The permanent shutdown of Trojan has further reduced any chemical discharges from the levels that resulted from plant operation. Any chemical discharges resulting from decommissioning activities will be made in accordance with the limitations and conditions of the NPDES Waste Discharge Permit issued to the plant.
During plant operation various chemicals were also present in the cooling tower drift. These consisted basically ofinsoluble salts. Chlorine was also present in the cooling tower drift within the cooling tower structure. An asbestos cement material was used for construction of portions of the cooling tower internals. As stated in the original Trojan environmental report, there were no measurable environmental effects expected due to operation of the cooling tower. However, since the cessation of plant operations, the cooling tower is no longer in use and release of any chemicals contained in the cooling tower drift has also ceased.
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