ML20150C335

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Ack Receipt of 880113 Response to SALP Repts 50-317/86-99 & 50-318/86-99 During May 1986 - Aug 1987.No Changes to SALP Rept Deemed Necessary Based on Response & 871214 Mgt Meeting
ML20150C335
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 03/14/1988
From: Russell W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Tiernan J
BALTIMORE GAS & ELECTRIC CO.
References
NUDOCS 8803180139
Download: ML20150C335 (4)


See also: IR 05000317/1986099

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MAR 141988

6

Docket Nos. 50-317/50-318

Baltimore Gas and Electric Company

ATTN: Mr. J. A. Tiernan

Vice President

Nuclear Energy

Post Office Box 1475

Baltimore, Maryland 21203

Gentlemen:

Subject:

Systematic Assessment of Licensee Performance (SALP) Report Numbers

50-317/86-99 and 50-318/86-99

This refers to the evaluation of the Calvert Cliffs Nuclear Power Plant oper-

ated by the Baltimore Gas and Electric Company conducted by the NRC staff on

October 16, 1987. This report was . forwarded to you on December 3,1987 and

discussed with you in a meeting held at the Calvert Cliffs Nuclear Power Plant

on December 14, 1987.

The list of attendees at the December 14 meeting is attached as Enclosure 1.

The NRC _ SALP Report is attached as Enclosure 2.

Our letter of December 3

(Enclosure 3) forwarded the SALP Report and solicited your comments within

thirty days of the December 14 meeting.

Your letter of January 13, 1988, in

response to the SALP Report is attached as Enclosure 4.

Your response of January 13, 1988, has been reviewed; it appears to address the

concerns expressed in our report and during the December 14 meeting.

No

changes to the SALP Report were deemed necessary based on discussions during

the management meeting or you written response.

Our overall assessment of activities at the Calvert Cliffs facility during the

assessment period indicated an adequate level of performance. Although several

significant program area strengths were noted, such as your trip reduction

efforts and the performance of your licensed and non-licensed staff, several

weaknesses were noted warranting continued corporate management attention.

These weaknesses included the timeliness and comprehensiveness of root cause

determinations, staffing shortages in the engineering and maintenance areas and

problems in the control of interfaces among the engineering, maintenance and

operations organizations.

Your presentations made at the December 14, 1987

management meeting and further described in your written response, indicate a

recognition of these weaknesses alona with a positive attitude toward improving

performance in these areas.

OFFICIAL RECORD COPY LIMROTH 136 3/2/88 - 0001.0.0

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03/08/88

8803180139 880314

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ADOCK 05000317

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MAR 141988

Baltimore Gas and Electric Company

2

We believe ' that our meeting and interchange of information was beneficial;

future meetings between Region I management and plant management to apprise us

of your progress and to discuss matters of mutual interest 'are encouraged.

No . reply to 'this letter is required.

Your actions in response to the NRC

SALP will be reviewed as part of the ongoing inspection program at Calvert-

Cliffs.

-Your cooperation is appreciated.

'

Sincerely,

Orfcinni Signed By

5:U. .?: ". LI ELL

William T. Russell

Regional Administrator

Enclosures:

1.

List of Attendees

.- 2 .

SALP Report Nos. 50-317/86-99 and 50-318/86-99

3.

NRC Letter to BG&E, dated December 3,1987

4.

BG&E Letter to NRC, dated January 13, 1988

cc w/encis:

i

M. Bowman, General Supervisor, Technical Services Engineering

T. Magette. Administrator, Nuclear Evaluations

Public Document Room (POR)

Local Public Document Room (LPDR)

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Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of Maryland'(2)

Chairman Zech

Commissioner Roberts

Commissioner Bernthal

Commissioner Carr

Commissioner Rogers

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0FFICIAL RECORD COPY LIMROTH 136 3/2/88 - 0002.0.0

03/08/88

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Baltimore' Gas and Electric Company-

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RegionI-DocketRoom(withconcurrences)'

J. Taylor, DED0

-J. Lieberman, OE

W. Russell, RA

J. Allan, DRA

W.- Johnston,'DRS

F. Congel, DRSS

D. Holody, ES

Management Meeting Attendees

DRP .'VISHLIST Coordinators (2)

M. Perkins, Management Assistant, DRMA (w/o encis)

L. Tripp, DRP Section Chief

0.=Limroth, DRP

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D. Trimble, RI -'Calvert Cliffs (w/ concurrences)

R. Bores, Technical Assistant, DRSS

S. McNeil, LPM, NRR

K. Abraham,-PA0 (14) (SALP Reports Only)

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OFFICIAL RECORD COPY LIMROTH 136 3/2/88 - 0003.0.0

03/08/88

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ENCLOSURE 1

Attendees At SALP Management Meeting - December 14, 1987

1.

Baltimore Gas and Electric Company

G. V. McGowan, President

E. A. Crooke, President Elect

J. A. Tiernan, Vice President, Nuclear Energy

J. R. Lemons, Manager, Nuclear Operations

L. B. Russell, Manager, Nuclear Maintenance

W. J. Lippold, Manager, Nuclear Engineering Services

R. M. Douglass, Manager, Quality Assurance and Staff Services

R. P. Heibel, General Supervisor, Operations

P. T. Crinigan, General. Supervisor, Chemistry

L. A. Sundquist, General Supervisor, QC and Support

N. Millis, General Supervisor, Radiation Safety

R. L. Wenderlich, General Supervisor, Electrical and Controls

R. P. Sheran, General. Supervisor, Mechanical

M. E. Roberson, General Supervisor, QC and Support Services

A. R. Thorton, General Supervisor, Plant and Project Engineering

M. E. Bowman, General Supervisor, Technical Services Engineering

R. F. Ash, General Supervisor, Design Engineering

J. T. Carroll, General Supervisor, Quality Assurance

K. Nietmann, General Supervisor, Nuclear Training

2.

U. S. Nuclear Regulatory Commission

W. T. Russell, Regional Administrator, RI

W. F. Kane, Directo', Division of Reactor Projects (DRP), RI

R. D. Capra, Director, Project Directorate I-1, Office of Nuclear

Reactor Regulatiran (NRR)

J. T. Wiggins, Chief, Reactor Projects Branch No. 3, DRP, RI

L. E. Tripp, Chief, Reactor Projects Section No. 3A, DRP, RI

T. Foley, Senior Resident Inspector, Calvert Cliffs Nuclear Power Plant

S. D. McNeill, Project Manager, PD I-1, NRR

D. Trimble, Resident Inspector, Calvert Cliffs Nuclear Power Plant

3.

Others

T. Magnetta, State of Maryland

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ENCLOSURE 2

.

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT

J. 50-317/86-99; 50-318/86-99

BALTIMORE GAS AND ELECTRIC COMPANY

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CALVERT CLIFFS NUCLEAR POWER PLANT

ASSESSMENT PERIOD: May 1, 1986 - August 31, 1987

"T'77d OIh7

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TABLE OF CONTENTS

P, age

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I.

INTRODUCTION

1

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A.

Purpose and Overview . . . . . . . . . . . . . .

1

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- B.

SALP Board Members . . . . . . . . . . . . . . .

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- II. CRITERIA

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III. SUMMARY OF RESULTS. .-. . . . . . . . . . . . . . . .

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A.

Overall Summary

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B.

Background . . . . . . . . . . . . . . . . . . .

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C.

Facility Performance Analysis Summary. .

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D.

Unplanned Shutdowns, Plant Trips, and

Forced Outages.

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IV.

PERFORMANCE ANALYSIS

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Plant Operations

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B.

Chemistry and Radiological Controls . . . . . . .

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Maintenance . . . . . . . . . . . . . . . . . . .

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D.

Surveillance

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Emergency Preparedness

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F.

Security and Safeguards .

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G.

Refueling, Outage Management

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H.

Engineering Support .

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Licensing Activities

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Assurance of Quality

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K.

Training and Qualification Effectiveness. . . . .

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SUPPORTING DATA AND SUMMARIES . . . . . . . . . . . .

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Investigations, Petitions and Allegations . . . .

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B.

Escalated Enforcement Actions . . . . . . . . . .

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C.

Management Conferences

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D.

Licensee Event Reports

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TABLE 1 - INSPECTION REPORT ACTIVITIES . . . . . . . . . .

T1-1

TABLE 2 - INSPECTION HOUR SUMMARY

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TABLE 3 - ENFORCEMENT ACTIVITY

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TABLE 4 - LICENSEE EVENT REPORTS . . . . . . . . . . . . ,

T4-1

TABLE 5 - SUMMARY OF LICENSING ACTIVITIES

T5-1

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INTRODUCTION

A.

Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an inte-

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grated NRC staff effort to collect the available- observations and

data on a periodic basis and to evaluate licensee performance based

upon this information.

The SALP program is supplemental to normal

regulatory processes used to ensure compliance to NRC rules and

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regulations.

The -SALP program is intended to be sufficiently diag-

nostic to provide a rational basis for allocating NRC resources and

to provide meaningful guidance to. the licensee's management to pro-

mote quality and safety of plant operation.

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The NRC SALP Board, composed of the staff members listed below, met

on October 16, 1987 to review the collection of performance observa-

tions and data and to assess licensee performance in accordance with

guidance in NRC Manual Chapter 0516, "Systematic Assessment of

Licensee Pe rfo rmance" .

A summary of the guidance and evaluation

criteria is provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the Calvert Cliffs Nuclear Power Plant for the period

May 1,1986 through August 31, 1987.

It is noted that the summary

findings and totals reflect a 16 month assessment period.

The SALP Board was comprised of the following:

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Chairman

W. F. Kane, Director, Division of Reactor Projects (DRP)

Members

T. T. Martin, Director, Division of Radiation Safety and Safeguards

(DRSS) (Part-Time)

W. V. Johnston, Acting Director, Division of Reactor Safety (DRS)

(Part-Time)

R. A. Capra, Acting Director, Project Directorate I-1, NRR

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S. J. Collins, Deputy Director, DRP (Part-Time)

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R. R. Bellamy, Chief, Emergency Preparedness and Radiological

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Protection Branch, DRSS (Part-Time)

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J. P. Durr, Acting Deputy Director, DRS (Part-Time)

J. H. Joyner, Chief, Nuclear Materials Safety and Safeguards

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Branch, DRSS (Part-Time)

L. E. Tripp, Chief, Reactor Projects Section (RPS) No. 3A, DRP

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T. Foley, Senior Resident Inspector, Calvert Cliffs Nuclear Power

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Plant

S. A. McNeill, Project Manager, Project Directorate I-1, NRR

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Other Attendees (non-voting)

D. C. Trimble, Resident Inspector, Calvert Cliffs NPP

D. F. Limroth, Project Engineer, RPS 3A, DRP (Part-Time)

A. B. Sidpara, Reactor Engineer, RPS 3A, DRP (Part-Time)

C. A. Carpenter, Reactor Engineer, RPS 3C, DRP (Part-Time)

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II. CRITERIA

Licensee performance is assessed in selected functional areas. Functional

areas normally represent areas significant to nuclear safety and the

environment.

One or more of the following evaluation criteria were used to assess each

area.

1.

Management involvement and control in assuring quality.

2.

Approach to resolution of technical issues from a safety standpoint.

3.

Responsiveness to NRC initiatives.

4.

Enforcement history.

-5.

Operation events (including response to, analysis of, and corrective

actions for).

6.

Staffing (including management).

7.

Training and qualification effectiveness .

However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories.

The definitions of

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these performance categories are:

Category 1:

Reduced NRC attention may be appropriate.

Licensee manage-

ment attention and involvement are aggressive and oriented toward nuclear

safety; licensee resources are ample and effectively used such that a high

level of performance with respect to operational safety is being achieved.

Category 2: NRC attention should be maintained at normal levels. Licen-

see management attention and involvement are evident and concerned with

nuclear safety; licensee resources are adequate and reasonably effective

so that satisfactory performance with respect to operational safety is

being achieved.

Category 3:

Both NRC and licensee atten+ ion should be increased. Licen-

see management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear

strafned or not effectively used such that minimally satisfactory perform-

ance with respect to operational safety is being achieved.

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The SALP Board may determine to include an appraisal of the performance

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trend of a functional area. Normally, this performance trend is only used

where both a definite trend of performance is discernible to the Board and

the Board believes that continuation of the trend may result in a change

of performance level.

Improving (declining) trend is defined as:

Licensee performance was determined to be improving (declining) near the

close of the assessment period.

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III. SUKVRY OF RESULTS

A.

Overall Summary

Our assessment of your performance during this assessment indicates

that three broad problem arc.n were evident; (1) management control

of interfaces between c'epartments (i.e., dissemination of engineering

requirements to the field, integration of syste.s engineers into the

plant staff, and functioning together as a team), (2) insufficient

resources in the maintenance and engineering departments hampering

their ability to support operations (slow resolution of recurrent

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equipment problems), and (3) ineffective use of available tools to

recognize emerging plant problems (i.e. QA audits, lack of independ-

ence of oversight committees).

There were additional weaknesses in surveillance testing, communica-

tion of results to appropriate levels of management, and adequate

followup / resolution of indicators of potential epipment operability

problems. As a result, optimal equipment operability / reliability was

not always achieved.

Furthermore, post-maintenance and surveillance

testing appeared to be oriented toward demonstrating Technical Spec-

ification compliance rather than assuring equipment reliability.

Existing systems have achieved limited success in prioritizing main-

tenance activities and resolving long standing deficiencies.

The

failure to demonstrate timely decision making and protective action

recommendations in the emergency planning area indicated reduced

attention to this function. Housekeeping was obserYed to deteriorate

during outages, particularly in individual contaminated areas.

In

addition to being hindered by interface, coordination, communication,

and resourc-e problems, engineering appeared to be overloaded with

better direction and guidance needed regarding prioritization.

Notwithstanding the weaknesses discussed above, notable areas of

strength were observed.

These include (1) the Trip Reduction Task

Force and a Trip Evaluation Review Group that were instrumental in

helping prevent trips from recurrent causes and provided root cause

diagnosis of the cause(s) of feed pump trips, (2) performance of

licensed operators, (3) the in plant radiation protection program

which continued to achieve good control of exposures and a strong

ALARA effort, (4) the 10 year In-Service Inspection program which was

well managed and displayed good initiative in implementing state-

of-the-art techniques that often exceeded regulatory requirements,

(5) a loss of off-site power event which was handled well, (6) well

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coordinated and managed refueling and outage activities, (7) consoli-

dation and movement of engineering functions to the site, (8) the

technical ability, credibility and effectiveness of the QA department

by recent initiatives to add more technically oriented staff and to

use outside consultants to assess performance in complex areas, and

(9) well trained and highly motivated plant employees and first line

supervisors.

In summary, although significant areas of strength were noted, overall

performance slipped during this period.

Recognition and resolution

of deficiencies, including timeliness and comprehensiveness of root

cause analyses, continued to be a problem although some progress was

noted toward the end of the period. Improved interfaces between the

Engineering, Operations and Maintenance Departments to assure that

they work together effectively as a team is considered to be the

primary area for improvement.

B.

Background

1.

Licensee Activities

Unit 1

Unit I was at full reactor power (825 MWe) at the beginning of

the assessment period. From May 16 to May 19, 1986 the unit was

at reduced power (790 Kde) for installation of a new type of

traveling screen. On June 20, puwer was reduced to li; to permit

a containment entry to add oil to No. 12A reactor coolant pump

upper oil reservoir. The unit was returned to 100?; power oper-

ation on June 22, 1986.

On July 10, a ^

ge influx of jellyfish, crabs, ar.d marine life

caused shear pias on the travelling screen motors to shear thus

necessitating a power reductiori. This was followed by several

days where the bay oxygen concentration was below normal causing

increased marine life to accumulate at the intake structure. On

July 20, reactor coolant pump 128 tripped off, due to grounds

within a capacitor, also causing a plant trip. The unit was re-

turned to service the following day.

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On August 3, the licensee reduced power to perform a temperature

coefficient surve'llance.

During much of the month of August,

licensee personnel espent considerable time in preparation for

the upcoming ten year In-Service Inspection (ISI) and refueling

outage scheduled for October 25, 1986. On October 10 an oper-

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ator mispositioneJ a condenser off gas discharge valva causing ay ['

loss of condendir . vacuum and. a turbine trip, resulting in a

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reactor trip.

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the restart from thi,s trip, the unit

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tripped again 'on~9rtng

October 11 from 15% power 'due to arial flux

offset.

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October 11, 1926 and continued routine operation.

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the unit was shut down to comence the p/

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On October 24,

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In-Service Inspection and refueling outage.

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The licensee had requested and was granted an emergency Tech-

nical Specification change to allow refueling 'to be conducte:i

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without an operable diesel generator specifically assigned to

schedule.

Work activities proceeded in a systematic, harmon-

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that unit.

The unit continued the outage keeping close to

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ious, and steady manner.

However, final repair'o1 the No. 12

diesel generator (OG), repairs to the main generator collector

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and retaining ring and failure of the #118 reactor coolant pump

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shaft seal all contributed to delays (a few days each) in outage.

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recovery activities.

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On December 31, the unit was refueled and ready for startup

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activities while a taitirg resolution of the hydrogen seal and

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main generator beriing problems.

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Unit I was returned to power operation on 'Janbary 12, 1987. A

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manual trip occurred on January 27 following"a loss of instru-

ment air pressure due to an operator error in returning

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instrument air >ystem to a ncrmal valve alignment at the con-

clusion of a system performance test.

Two condensate booster

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pumps were damaged during the event, which delayed unit start up

until January 31.

On February 1, Unit 1 was manually tripped

following a turbine run back due to low stator cooling liquid

pressure.

The' manual trip was in anticipation of an automatic

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trip on high reactor coolant system pressure.

The unit was

returned to power on February 2.

On February 7, tthe unit was

removed from the grid to repai'e an oil leak on a turbine

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intercept valve.

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On March 10, the reactor coolant quench tank rup'ture disk rup-

tured due to a leaky pressurizer safety valve.

Tne unit was

subsequently shut down, the safety valves ' replaced and the

pressurizer- vent valves repaired. .The unit was returned to

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power operations on March 15.

During the week of March 23, NRC

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regional specialists reviewed environmental qualification (EQ)

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outstanding items and observed apparent inadequacies,in the pro-

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Routine operations continued until - April

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licensee identified additional EQ deficiencies and the unit was

shut down to correct discrepancies.

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On April 14, 1987, containment spray was inadvertently initiated

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due to operator error in performing a valve lineup,

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'On April 23, 1987, the licensee informed the NRC that certain

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replacement items (principally threaded fasteners) not fully

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meeting AMSE code requirements bad been used in Class 1, 2, and

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3 systeks on both units.

Whih the non-conforming parts ap-

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peared to have been manufactured from ths' correct material, they

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did not meet. code requiremenil, with. respect to marking, certifi-

cation and, in sone cases, non-destructive examination. Resolu-

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tion of this issue coupled with the EQ problems forced Unit 1 to

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extend the shutdown.

On May 27, VAit 1 entered Mode 1 after completing surveillance,

Mechanical Commercial Quality and EQ post maintenance testing.

The unit paralleled- to the grid, escalated in power on May 28

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and remained at 10C% power throughout the remainder of the

period.

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Unit 2

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Unit 2 began the a.sjessment period at full rpctor power (825

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MWe). The unit was manually tripped on May 21, 1986 because of

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a loss of steam generator feed pumps (SGFP). \\"he cause of the

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loss of tne SGFPs was not determined.

On May 23, 1986 the unit

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was pa N ileled to the grid.

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On May 27, 1986, the unit was automatically Wipped due to loss

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of SGFPs. On May 28, 1986, the unit was paralleled to the grid

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and remained at 60% power (520 MWe) to test the 3GFP instrumen-

tation.

Testing of the SGFP instri. mentation remained in pre-

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grass from May 28, 1986 until June ?.

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On July 25, a decision was made/to shut down daa to a concern

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regarding increasing vibration ' trends on reactor coviar,t pump

'(RCP) #218. ' Before shut down commenced, a RCP #21A seal prass-

ure transmitter flex hose end fitting separated causing' 'a

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reactor coolant leak. An Unusual Event was d2clared as requirep

by the site Emergency Plan due to any forced shut down required

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by Technical Specifications. The plant remained shut down while

industry experts evaluated vibration trms from RCP #218 until

August I when the unit was rvstarted.

On September 5, the unit tripped due to a failed surge capacitor

on No. 21A Reactor Coolant Pump.

The unit . was returned to

operation on September 7.

Full power operation continued until

September 12 when operators manually tripped the plant due to a

loss of No. 21 SGFP and an impending low steam generator water

level.

The unit was returned to service on September 14;

however, power level was maintained at 60% (capacity of a single

feed pump) while the Trip Fvaluation and Review Group (TERG)

directed troubleshooting efforts on 21 $GFP control system. On

Septerber 18, the unit underwent a controlled shutdown antici-

pating the inability to neet a Technical Specification Limiting

Cordition for Coeration Action Statement due to an inoperable

emergency diesel generator. With NRC concurrence, the unit was

returned to 60% power until September 20 when repairs were com-

pleted.

Full power operations were resumed.

During September

considerable time 'was devoted to resolving problems associated

with No. 12 emergency diesel generator jacket water cooling

pressure oscillations, apparently caused by cart.on monoxide (CO)

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leaking into the cooling system. Tnese , efforts extended from

September 10 through Octcber 7.

Unit

operated at full power until February 28,' when the unit

trippsd on low steam generator water level due to a level con-

trol system failure.

T hc. unit had been in operation for 169

consecuttyedays.

On March .13, the Unit shut down to commence its 10 year In-

Service, Inspection 'nd Refueling Outage.

.

a

On July 3, the unit was paralleled to the grid ano tripped on

low steam pressure dud to an incorrect rheo < tat setting in the

turbine control circuit initial valve posfu on limiter.

The

unit returned to power operations.later that day 5ut was. limited

to reduced power operation due to turbine bearing vibration.

It

was brought to zero power and a balance shot was performed. on

July 8; therc rets gned to power or. July 9,1987.

J

.3

i

e,

,

f

. - - .

.-.

-.

-~

-

.-

.-.-L-

-- ,

].

A

.

_

~

,

so.

ayl

t

w

'

10

2.

Inspection Activities

-Two NRC resident inspectors were assigned during the inspection

period. The total NRC inspection effort for the period was 4018

hours (3013.5 annualized) with a distribution in the appraisal

functional areas as shown in Table 2 (Inq ection Hour Summary).

Table 1 lists every NRC inspection conduct.ed at Calvert . Cliffs

during this period.

During the period, NRC team inspections wee conducted of the

following areas:

a.

Actions taken relative to Gener.ic Letter 83-28 in the area

of Equipment Classification, Vendor Interface, Post Main-

tenance Testing, Surveillance and QA/QC overview (Inspec-

tion Report 317/86-10, 318/86-10.

b.

Emergency Preparedness Partial Scale Exercise and subse-

quent remedial drill (Inspection Report 317/80-14).

c.

Follow up of licensee actions relative to deficiencies pre-

viously identified regarding Post Accident Sampling capa-

bilities (Inspection Report 317/87-03).

d.

Follow up inspection of Environmental Qualification defic-

iencies, Post Maintenance Testing, use of Commercial Grade

Fasteners (Inspection Report 317/87-13 and 318/87-14).

Inspection Activities are summarized in Tables 1 and 2. Enforce-

meat activities are summarized in Table 3.

This report also discusses "Training and Qualification Effec-

1 -

tiveness" and "Assurance of Quality" as separate functional

areas.

Although these topics, in themselves, are assessed in

'

the other functional areas through their use as criteria, the

two areas provide a synopsis.

For example, quality assurance

ef fectiveness has been assessed on a day-to-day basis by resi-

dent inspectors and as an integral aspect of specialist inspec-

tion.

Although quality work is the responsibility of every

employee, one of the management tools to measure this effective-

ness is reliance on quality assurance insoections and audits.

Other major factors that influence quality, such as involvement

of first-line supervision, safety committees, and work atti-

tudes, are discussed in each area.

The topic of fire protection is not discussed as a separate

functional area because of insufficient inspection activity. The

available observations on fire protection and housekeeping are

included in the various relevant functional areas.

~

.

11

C.

Facility Performance Analysis Summary

Category

Category

Last Period

This Period

Functional Area

10/1/84-4/30/86 05/1/86-08/31/87

Trend

1.

Plant Operations

2

2

Improving

2.

Chemistry and

Radiological Controls

1

1

3.

Maintenance

2

2

4.

Surveillance

1

2

5.

Emergency

Preparedness

1

2

6.

Security and

Safeguards

1

1

7.

Refueling, Outage

Management

2

1

Declining

8.

Engineering Support

N/A

3

Improving

  • 9.

Licensing Activities

1

2

10. Assurance of Quality

2

2

11. Training and

Qualification

2

2

Improving

Effectiveness

[

..

12

D.

' Unplanned Shutdowns,-Plant Trips, and Forced Outages

' UNIT 1

Functional

D,te & Power Level Description

Cause

Area

07/20/86 - 100%

Loss of flow and automatic

Long-standing

reactor trip; reactor

repetitive

coolant pump surge

design

capacitor failure

deficiency

Engr.

,

10/10/86 - 100%

Automatic turbine / reactor

trip; loss of condenser

vacuum due-to' auxiliary

operator mispositioning

an off gas discharge valve

Personnel error Ops.

10/11/86 - 15%

Automatic reactor trip';

Inadequate

axial flux offset during

procedure and

start up

training

Ops.

01/27/87 - 100%

Manual reactor trip due to

imminent steam generator low

level caused by loss of

instrument air due to the

same auxiliary operator as

above mispositioning valves

-

during a restoration from a

performance test

Personnel error Ops.

02/01/87 - 70%

Manual reactor trip in

anticipation of high RCS

pressure following a turbine

run back caused by low

stator cooling liquid

Inadequate

pressure

procedure

Ops.

02/07/87

Unit was removed from the

grid to repair an oil leak

on the turbine intercept

valves

03/10/87 - 100%

Controlled shutdown due to

a blown RCS quench tank

!

rupture disc caused by leaky

code safety valves and

Component

insufficient spare parts

failure

Ops.

.

13

i

'

Functional

Date & Power Level Description

Cause

Area

04/01/87 - 100%

Controlled shutdown to

Implementation

correct environmental

of inadequate

qualification program

program

deficiencies

Engr.

07/14/87 - 20%

Automatic reactor trip due

to high steam generator water

level resulting from a transient

on the 16A feedwater heater

combined with operator over

Personnel error /

boration

training

Ops.

07/23/87 - 100%

Total loss of offsite power

initiated by a ground fault

(tree near relay at offsite

transmission line) and overly

sensitive protection relay ~at

Calvert Cliffs

Other

N/A

l

-

_ _ _ _ _ - _ _ _ _ _ _

t-

.

14

-.

' UNIT 2

Functional

Date & Power Level Description

Cause

Area

05/21/86 - 100%

Manual' trip due to loss

of a steam generator feed

Grounds in FW

pump

control circuit

Maint.

~05/27/86 - 100%

Automatic trip due to loss

of a. steam generator feed

Grounds in FW

pump

control circuit

Maint.

'

07/25/86 - 100%

Controlled shutdown to

Random

repair RCP seal flex hose

component

. transmitter line

failure

Engr.

09/05/86 - 100%

Reactor coolant pump surge

capacitor failure

Design

Engr.

09/12/86 - 100%

Manual reactor trip due to

loss of a feed pump.and

impending low steam

Grounds in FW

generator water level

control circuit

Maint.

09/18/86

Unit underwent a controlled

shutdown anticipating the

inability to meet a TS LCO

Maint.

02/28/87 - 100%

Automatic reactor trip on

low steam generator level

resulting from the failure

of ccntrol system component

Random

i.e., downcomer lead / lag

component

unit

failure

07/03/87 - 15%

Automatic reactor trip on

low steam pressure due to

Inadequate

improper setting of the

vendor

turbine control circuitry

guidance

Maint.

07/08/87 - 60%

Controlled shutdown to

perform a turbine balance

Normal

shot

maintenance

Maint.

l

l

l

-.

.

____ _

.-.

. _ _ _ _ _ _ _ _ - _ _ _ _ _ _ ~

.

15

Functional

Date & Power Level

Description

Cause

Area

07/17/87 - 80%

Controlled shutdown to

repair vent and drain valves

leaking greater than T/S

Random

limit and correct turbine

component

vibration

failure

07/23/87 - 100%

Total loss of offsite power

(see Unit 1, same trip)

Other

N/A

.

. ..

.

.

..

..

.

_

16

. . '

IV. PERFORMANCE ANALYSIS-

A.

Plant Operations (40.9%)

1.

Analy si s -

The previous SALP determined the Operations area to be Category

2.

It concluded that management needed to be more aggressive in

pursuing recognition of safety issues and perform more thorough

and comprehensive root cause analysis of the issues.

During the beginning of this period, inadequate pursuit of

safety issues continued to be a problem as demonstrated by the

,

three successive reactor trips caused by multiple grounds in the

feedwater control system on May 21, May 27, and August 12, 1986.

The utility responded to the concerns identified in the previous

SALP by instituting a "Trip Evalu'ation Review Group" (TERG) and

a "Trip Reduction Task Force".

The feed pump trips were subse-

quently diagnosed by the TERG.

Throughout the period the TERG

Improved the root cause analysis of operational problems.

Previously,

slow to recognize potential safety issues, the

licensee aggressively pursued RCP subharmonic vibration prob-

lems, unknown elsewhere in the industry, and an Emergency Diesel

generator gassing problem.

In addition to pursing root cause analysis of reactor trips (see

Engineering section of this report), the licensee recognized the

relatively high number of reactor trips (14) during the last

period and instituted a Trip Reduction Task Force.

Recommenda-

tions of the task force appear to be well founded and compre-

hensive, however, many which have a high potential for reducing

reactor trips were slow to be implemented because of engineering

delays and/or resource constraints, i.e, instrument air upgrades

and

replacing RCP surge capacitors.

Those recommendations

requiring minimal time and resources have been implemented.

Much of the initial task force momentum now appears to have

weakened.

A significant portion of the 14 reactor trips which

occurred during this period would have been avertert had all the

recommendations been implemented at the start of this period

(i .e. , loss of instrument air, axial flux offset, steam genera-

tor feed pump trips and two RCP surge capacitor trips).

_ - _ _ - _ _ _ _ _ _ _ _ _ -

_ _ _ _ -

.

u

17

-

During the sixteen month period, five personnel errors occurred-

within -the. Operations area (see Table 4). No consistent trends

or management inadequacies were evident. Operations Department

shift personnel have undergone "team training" sessions on the

simulator and in the classroom to -improve the communications,

coordination and help better use synergism in the recognition.of

plant transients.

Two procedural

inadequacies resulted

in

,

reactor trips (see Table 4).

These were isolated instances and

not indicative of a general problem.

The large number of licensed operators (75 active licenses; 41

SR0's, 34 RO's) allows the Operations Department to utilize

experienced licensed individuals to rotate through a "Procedures

Development" group and a "Tagging Authority" group. Procedures

Development has been tasked with the improving procedures in

general.

Specific upgrades of each procedure which has the

potential for causing plant trips and improving the Emergency

~0perating Procedures (EOPs) were in progress.

Several other

significant

initiatives

have

been

implemented

to

develop

improved procedures.

In spite of the noted personnel and procedural errors, operators

have responded extremely well to plant events and transients.

On several occasions, operators prevented unnecessary plant

transients due to equipment failures (instrument air malfunc-

tions)

by

their

attentiveness

and quick

response,

i.e.,

July 1,1987, during a loss of No. 13 vital AC Instrument Bus

-

causing a loss of four reactor trip breakers and one channel of

ESF. Only by close adherence to procedure and maintaining com-

posure did operators determine the plant had not tripped. Dur-

I

ing the total loss of offsite power event, operators and the

Operations staff performed professionally, conservatively, and

demonstrated the culmination of knowledge by consolidating

emergency preparedness training, emergency operation procedure

training, knowledge of plant conditions and excellent use of

operating instructions in responding to a single event. Opera-

tors performed in a normal fashion; calm, deliberate, and per

procedures.

Notwithstanding the licensee responsiveness to the last SALP,

improvements in the effectiveness of the Plant Operations Safety

Review Committees manner of doing business may be warranted.

The "organization" might be more effective if (1) the prepond-

erance of the attending members were were not directly respon-

sible to the chairman; (2) the chairman was less aggressive ar.d

influential; (3) recommendations were made independently to the

plant manager; and (4) further use of subcommittees was evalu-

ated.

Further, a recent Quality Assurance Audit also noted this

lack of independence and potential for a slight bias towards

plant operation.

. .

.

..

________ - ___- -_ _____--_ _ _ _

.

18

Routine tours of the facility and discussions' with workers have

indicated a very favorable attitude towards plant management and

the . company.

Management was frequently involved. in onsite

activities, managers and the Vice President were usually in at-

tendance at outage meetings 'and most managers were routinely

seen touring the plant on housekeeping inspections.

Periodi-

cally, during outages, all work was stopped in order to stress

the importance of housekeeping.

Generally, housekeeping was

good, however, housekeeping areas within the contaminated, con-

trolled areas were sometimes poorly maintained.

Tools, hoses

and debris were found in some areas with boric acid crystals and

valve leakage.

The licensee continued to display a strong commitment toward

licensed operator training, evidenced by a high success rate in

NRC Reactor Operator (RO) and Senior Reactor Operator (SRO)

examinations. Written and operating examinations were adminis-

tered to four SR0s, all of whom passed, and six R0s, one = who

failed the simulator portion of the examination, and two who

failed the written and operating section. Subsequent'v, two R0s

were re-examined and found satisfactory.

During this period,

the simulator was first used for examinations and performed

well.

The training program appears to be strong overall with' some

minor weaknesses.

For example, the requalification training

program adequately covered the potential axial shape index prob-

lems during start up at the end of cycle with a large xenon

transient in progress, but operators had not practiced such a

start up on the simulator.

The Shift Engineer Pragram was also strong.

Degreed engineers

obtain SR0 licenses and are integrated into operational shifts.

The prospective shift engineers must qualify on all plant oper-

ator watch stations prior to the license class and serve as

control room supervisors and plant watch supervisors as well as

STAS.

The 75 licensed operators provide a considerable depth of talent

to allow for training, vacations, sickness, promotions, and

spare people on shift without unnecessary overtime. The opera-

tions staff is a solid stable work force with little turnover.

A new Assistant General Supervisor of Operations position has

also been allotted and filled.

Shift turnovers were thorough,

one-on-one walk throughs of the control panels with review of

administrative logs.

Shif t Supervisors and Control Room Opera-

tors routinely demonstrated a very conservative approach to

safety.

They are technically knowledgeable, professional, well

trained and provide an added level of assurance in safe opera-

tion.

They typically have good morale, attitudes, and an excel-

lent rapport with the facility staff

.

19

The operations group worked harmoniously with maintenance, HP,

and others throughout this period in 'the area of coordinating

maintenance and operations activities (see outage activities for

engineering. interface). They helped set maintenance priorities,

optimized scheduling, tagged equipment out of service 'at .the

proper . time, and ensured post maintenance testing was accom-

plished.

They improved their guidance on what specific post

operational tests were required for various types of mainten-

ance.

The licensee placed strong emphasis on planning. Improvement in

prior planning, setting priorities, and assignment of responsi-

bilities was evidenced in the establishment of pre-shif t brief-

ings to the oncoming watch section of non-licensed operators. A

recently established morning operations meeting between depart-

ment general supervisors, principal and system engineers and

planners now sets the day's priorities, discusses delays, coor-

dinates activities, and assigns responsibilities. A revised

"Plan of the Day" now includes maintenance, surveillance, and

other expected facility activities rather than a simple status

of each reactor.

The licensee's approach to the resolution of technical issues

from a safety standpoint generally exhibited conservatism and

was technically sound and thorough.

Reactor coolant pump shaft

and cover cracks, LPSI header relief valve weld cracks, and RCP

suction deflector ring failure demonstrated technically sound

resolutions.

However, occasionally during the period,

NRC

intervention was necessary to cause management to be aware of

deficiencies associated with surveillance testing or events

relating to the operability of safety-related equipment. Occas-

ionally, safety related equipment was initiated and failed to

operate.

If attempted a second time and it operated and passed

a Technical Specification surveillance test, the original fail-

ure was not always recorded or identified to management. Once

aware, appropriate reviews and action was taken (see Surveil-

lance section referencing additional details).

In summary, in spite of several visible events which drew atten-

tion to th? facility (EDG gassing, RCP shaft cracking, contain-

ment spray down), numerous program improvements were made. Many

were made in response to the last SALP, others in response to

the licensee's recognition of weaknesses.

The Plant Operations

Safety Review Committee has a potential to be biased towards

operations since the structure places the Chairman in a position

to

lose

objectivity.

Post-maintenance

operational

testing

requires improvements. A formal mechanism appeared to be lack-

ing which ensures that all failures are brought to the appro-

priate level of management attention in a timely fashion. Per-

formance of operating department personnel, especially licensed

operators, was excellent.

. - . . .

..

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. _ - .

. _ _

_ _______ -_.

_

_ _ _ _ _ .

_ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _

.

20

2.

Conclusion

Rating: 2

Trend:

Improving

3.

Board Recommendation

Licensee: None

NRC:

None

.

i

l

l

l

!

.

  • -

21

,

B.

Chemistry and Radiological Controls (11. 6's)

1.

Analysis

The Radiological Controls Program was rated Category '1

last

assessment period. Significant concerns with management control

over the PASS system were noted which led to escalated enforce-

ment and issuance of a civil penalty although the root cause(s)

of this problem primarily reflected on performance in other

functional areas.

During this period, there were seven inspections by regional

specialists in the chemistry and radiation control areas and

routine coverage by the resident inspectors. The in plant radia-

tion protection program was effectively impiemented during both

operational and outage conditions.

The radiation protection organization, particularly in the ALARA

area, was well-defined and adequately staffed, with well-

qualified individuals.

An appropriate number of trained and

qualified contractor technicians were used to support the out-

age. The use of contractors to supplement radiation protection

staff.was well controlled.

The licensee continued to implement

an effective radiation worker training program. Both the radia-

tion protection ALARA and operations groups were aggressive in

assisting in the development of this program. Procedures in the

radiation protection area were well-defined and well-imple-

mented. A need for the proceduralization of certain non-routine

activities, such as the use of steam generator TLD phantoms or

operation of non- routine survey instruments was identified as

an area for improvement.

l

The licensee's external exposure controls program continued to

be effective and contributed to overall program strength. Infor-

,

maticn concerning radiological survey data and conditions was

readily available to workers signing into the work area. Daily

exposure tracking was well-controlled;

reports of accruing

l

exposure for each worker were reported to responsible super-

l

visors twice daily during outage conditions. The licensee ef-

fectively utilized their Special Work Permit (SWP) system to

establish radiological controls.

l

Two unrelated deficiencies occurred during this period in the

area of High Radiation Area controls. During one incident iden-

'

tified by the licensee, two individuals "jimmied" the locked

door to a High Radiation Area and entered rather than waiting

for the HP technician to arrive with the key. Subsequent inves-

tigation, prompted by an allegation, identified that a set of

1

l

.__

. _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ .

. - _

,

22

master keys to the station's locked -High Radiation Areas was

uncontrolled.

No examples of unauthorized use were identified

indicating a significant breakdown of controls in this area had

not occurred.

Licensee corrective actions were timely and

comprehensive.

An effective internal exposure controls program was in place.

The ifcensee aggressively utilized containments and portable

ventilation as methods of controlling airborne activity. Post-

ing of airborne areas and tracking of MPC hours were performed

at action levels more ccnservative than those required by regu-

lations.

Recurring problems were noted with the auxiliary

building drain system, which repeatedly backs up and causes con-

tamination of previously clean flour areas. This creates a sit-

uation that radiation protection personnel are forced to live

with and indicates that plant management needs tc be more

aggressive

in resolving the root causes of this problem.

Similarly, as discussed in the Operations functional area, more

attention needs to be focused on cleanup of individual contam-

inated areas.

The ALARA program continued to exhibit strong performance. ALARA

pre-outage involvement and planning was substantial; numerous

exposure / savings mechanisms (nock-up training, automated equip-

ment, closed circuit TV, temporary shielding) were utilized dur-

ing the outage. Actual exposure for 1986 for the two units was

347 person-rem vs. a projected goal of 390 person-rem. The 1987

-

goal was only 405 man rem, although considerable high rad work

was necessary.

Experience through the end of the SALP period

indicated that this goal was achievable.

This

experience

indicates an aggressive goal setting program was in place and

was used to improve ALARA performance.

The solid radwaste program was ef fective. An aggressive program

for volume reduction resulted in disposal of volumes approxi-

mately one half of those at comparable PWRs. The organizational

responsibilities for processing, preparation and shipping solid

radwaste materials were clearly -defined in procedures, well

l

understood by the responsible groups, and functioned smoothly

j

during the assessment period.

,

i

_ . _ . .

.

_ . , - _ - _ _

. - . .

. , , _ _

, _ . _ _ , ~ . _ _ _ _

_ _ _ . , , . _ . . . . ,

_ , - _ -

_

_

._. _ _ _ _ _ _ __ _ _ _

.

23

The presence of failed fuel pins presented a technical challenge

to the solid radwaste program which was recognized, adequately

analyzed and handled.

Properly constituted corrective actions

were taken to prevent regulatory problems; 10 CFR 61 scaling

factors were modified to reflect the new conditions.

A high

degree of quality control involvement in solid radwaste activ-

ities was effective in ensuring the waste classification, form,

and packaging requirements were being met.

The radioactive effluents control program exhibited positive

controls over radioactive releases and radwaste system operation

with well stated procedures to promote proper performance. When

the plant vent wide range gas monitor (WRGM) original calibra-

tion data was deemed insufficient, the licensee declared the

monitor inoperable, submitted an LER, and notified the NRC.

Management controls resulted in timely restoration; alternative

sampling techniques were used in the interim.

Routine surveillances of the radiation monitoring and air clean-

ing systems were found to meet frequency requirements in all

cases.

In the previous assessment period the licensee had

failed to take carbon samples at the required frequency.

This

suggests an increased level of management involvement.

Routine radiochemical analysis of reactor coolant parameters was

satisfactory.

In one instance identified by the licensee, a

surveillance was missed, due to sn inadequate shift turnover.

-

Managnment response and mitigation efforts were timely.

This

event was a singular occurrence and did not suggest a program-

matic breakdown of management controls.

During the assessment period, licensee management took aggress-

ive action to correct the inoperability of the PASS system iden-

tified in the previous assessment. The original PASS system was

taken out of service and the NSSS sample sink was modified to

meet NRC requirements.

The resolution of the PASS deficiencies

by modifying the NSSS sample sink demonstrated a clear under-

.

standing of issues by the licensee as wall as a technically

(

sound approach.

Furthermore, twelve items were reviewed during

a special NRC follow up inopection and eleven, including all the

'

violations, were closed, indicating timely and thorough resolu-

tion of issues.

i

l

l

l

l

!

. _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _

_ _ _ _ _ _ _ _ - _

_

_ _ - _ . _ - _ -

_ _ _ _ _ _ _

__

. _ - _ _ _ _

.

24

}

The

licensee's

program

for. the

Radiological

Environmental

Monitoring program was found to be generally adequate.

Sampling

frequencies, type of measurements, analytical sensitivities, and.

reporting schedules generally complied with Technical- Specifica-

-tion . requirements.

A measurement quality ccntrol program was

implemented including participation'in the EPA Cross Check Pro-

gram. Measurement results'of the collected TLDs between the NRC

and the licensee were generally in agreement.

In summary, the in plant radiation protection program continued

to be effectively implemented during this assessment period. In

particular, good controls were in place and exercised, exposures

were tracked well .and maintained -low, . the ALARA program was

strong, and radioactive effluents and radwaste were minimized

with appropriate monitoring.

2.

Conclusion

Rating:

Category 1

Trend:

None-

3.

Board Recommendation

Licensee: None

,

NRC:

None.

-

.

-

C.

Maintenance- (13.9%)

1.

Analysis

The previous SALP rated the maintenance area as Category. 2.

Material . condition weaknesses required continued effort in-

several areas, but increased management attention and resources

were being devoted to these areas.

Additional . I&C engineering

support

was needed because of - weaknesses in the staffing,

direct line supervision, vendor support, and spare parts areas.

The . licensee was to evaluate the impact of secondary system

maintenance problems on reactor trips and determine if poor

maintenance

and/or design weaknesses were contributing to

,

balance of plant related trips.

During this period, regional specialists conducted six inspec-

tions of this area. Resident inspectors also routinely reviewed

this' area.

During this period, the I&C _ area significantly improved; a new

general supervisor aggressively pursued issues, assigned respon-

sibilities, and held personnel accountable. Systems were imple-

mented which trended and provided status of control room defici-

ency tags.

Some progress was made in reducing the number of

control room MRs. Problems identified last pe'riod regarding the

operability of main steam isolation valves were resolved by the

replacement of those valves; a major modification performed very

well.

As noted in the Operations area, operators, engineers,

and maintenance personnel attended factory acceptance testing

and worked with the vendor to develop operational test, opera-

ting and maintenance procedures.

Grounds on the Feed Water

Control System are also under control.

Several enhancements

took place (separation of power supplies and replacement of

numerous parts with state of the art controls). A task force to

improve the feed systems reliability generated several re com.--

mendations not yet fully implemented.

The licensee installed

two new and improved travelling screens at either end of the

intake structure, where most jelly fish accumulate.

Both communications and coordination between maintenance, oper-

ations, and engineering showed improvements.

General super-

visors visited other nuclear plants to obtain alternatives in

order to improve the recognized weaknesses in the MR system. A

"Perfect Planning" effort was effective in planning outage

activities (see the Outage activities section for datails).

-

-

-

-

- - . - - - . _

___ _ _ _ ____ _ _____ _ _

__j

,

26

Training of both electrical and mechanical personnel improved.

All maintenance' training programs are now' INPO accredited. All

maintenance personnel receive two weeks ' of general- training.

Although improved, the volume of out of service instruments af-

fecting the control room operators performance was excessive,

about 15 per unit.

Additionally, several instruments that do

not have MRs attached were inappropriate for operator use in

that the normal operating parameters were at the top or bottom

5% of the scale.

For example,100% steam flow is recorded at

the very top.

Similar problems exist with the surge line tem-

perature and pressurizer water temperature indicators.

These

examples of maintenance and design / engineering inadequacies had

the potential to adversely affect operator performance.

Other indications of inadequate maintenance impacting operations

was the safety injection tank in-leakage problem.

Operators

must keep No. 21 charging pump in pull to lock in order to pre-

vent dilution of the safety injection tanks (SIT) because of

back leakage through several valves inner-connecting the sys-

tems. Maintenance and testing efforts to date were ineffective.

Similarly, the Instrument Air System air dryers / regeneration

units repeatedly failed to transfer and caused a loss of instru-

ment air.

This problem has been tolerated for several years

causing either plant scrams or near misses.

Only af ter NRC

inspector prompting did the licensee effectuate some improve-

ments to alleviate the problem.

-

Service water pumps and auxiliary feed water pump packings con-

tinued to be a problem.

Maintenance spent considerable time

reworking these packings without significant success. Engineer-

ing efforts were in progress to improve these, however, this

problem has persisted reveral years. Other equipment seemingly

out of service for extended periods were:

the plant air com-

pressors, intake air coolers, and screen wash pumps. Resolution

was slow.

Programs and efforts to address such problems have not worked

very well for the following reasons:

(1) The Integrated Management System (IMS) has been implemented

which provides a systematic method for prioritizing plant

betterment and projects by development of benefit to cost

ratios. The IMS system appeared to hinder improvements in

several areas by excessively cancelling or delaying many

enhancements recommended by veteran supervisors, because

the benefit to cost ratio requirements were not met. Super-

visors appear to have insufficient involvement in the set-

ting of priorities.

This caused several long standing

deficiencies.

--

-

_.

_ _ _ _ _

.

27

(2) During the last three years the Integrated Corrective

Action Program (ICAP) was under developnent to assist in

tracking component failures and identifying rework. Manage-

ment has not tracked component failures or repetitive main--

tenance during this time because ICAP was imminent. Trend-

ing or evaluations of repetitive failures do not occur by

other than. supervisor recollection.

(3) Currently, no consolidation program exists which, during

the life of a component, reverifies vendor technical manual

design requirements or FSAR requirements. Nor is component

performance ascertained during post maintenance testing

(PMT).

Most often PMT only assures that the component

operates.

The above problems and numerous others identified by MRs were

situations which

hinders

plant

operations.

They

existed

-throughout the period and reflected the need for additionel

staffing and resources.

The

licensee focused on preventive maintenance (PM).

PMs

existed for both safety related and non-safety related compo-

nents.

PMs had high priority.

Procedures were general.ly good

and a feedback mechanism existed through engineering back to the

maintenance procedure group. However, PM frequency was based on

arbitrary judgment or coincided with Technical Specification

required surveillance frequencies. Often, routine PMs were per-

formed on components seldom operated since the previous PM,

i.e. , ESF components, yet many outstanding corrective mainten-

ance items were not corrected in a tinely manner.

PM results

were not trended or thoroughly evaluated ww.h could provide a

better basis- for frequency of performance.

A better use of

maintenance history or component failure trends would also pro-

vide an excellent tool for managing the limited maintenance

resources.

Another area recognized by the licensee as being deficient was

poor work practices apparently due to a lack of pride in owner-

ship. At times tools and work-related debris were found scat-

tered about after completion of maintenance.

Cleanliness and

housekeeping were at times also below standards.

Maintent.1ce

management attempted to increase craft "job satisf action" by

minimizing reassignment of people from jobs in progress to a

"more urgent job".

This previous practice caused a lack of

ownership of jobs and personal pride in performance.

Operations

I

_ _ _ _ _ _

.

28

personnel would lose confidence in maintenance personnel's abil-

i ty to stay with or adequately complete a job.

Recognizing

maintenance problems, operations personnel were sometimes reluc-

tant to submit MRs believing .they would not be adequately ad-

dressed.

By allowing the same people to start and finish a job,

more. pride and ownership is expected to occur and workers will

receive either positive or negative recognition for "their" job.

Progress has been made despite the above. problems.

Grounds on

the feed system, gassing problems on Emergency Diesel Genera-

tors, replacing two reactor coolant pump rotating assemblies,

back to back ten year In Service Inspection and refueling out-

ages followed by Environmental Qualification and Commercial

Quality issues placed severe stress on the entire plant staff.

Notwithstanding, since the licensee implemented its response to

the last SALP, there has been only one maintenance-related plant

trip compared to eight last period. The procedure to calibrate

the Turbine Generator Electro-Hydraulic Controller was deficient

in prescribing a new micrometer setpoint for a newly purchased

turbine simulator control davice resulting in a reactor trip.

Meetings are now held daily to coordinate maintenance, engineer-

ing, and operations.

Prioritizing MRs, troubleshooting, deter-

mining root causes, scheduling and tracking work activities dur-

ing operation has greatly improved towards the end of this

period, due to the coordination by this morning meeting.

Nuclear maintenance tracks maintenance-related reactor trips,

-

control room instrumentation out of service, valves repacked,

Mode 1 corrective maintenance working backlogs and Mode 1 cor-

rective maintenance orders older than three months. Maintenance

orders are further divided and trended by numbers due to numer-

ous causes for delay.

This trending / tracking system worked

well.

A recently established oil analysis and vibration trending pro-

gram was somewhat successful in predicting component failures.

Previously, problems had occurred with adding the wrong type of

oil to components.

The licensee recognized most of the above problems as well as

others. They established programs or placed these items on the

Key Items List with assigned responsibilities and priorities.

The programs are showing improvement. As an example, the 2000

valves repacked last year resulted in a reduction in dissolved

oxygen by a factor of 5 in Unit 2 condensate. An "Investigative

Planner" has been established to troubleshoot and correct minor

deficiencies within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the MR origination.

This

resulted in a 35% reduction in the MRs greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

old.

._

+

7

29

-

In summary, maintenance' faced a great work load and still demon-

strated slow improvements as compared to last period.

Manage-

ment programs effectiveness appeared constrained by limited man-

power and resources and engineering support. - Use of the IMS to-

prioritize resource use appeared to be ineffective in resolving

long standing deficiencies.

Lack of effective use of trending,

maintenance history and component failures reduces resource

efficiency. Some poor work practices continued to exist due to

lack of attention to detail and insufficient supervision. Post

maintenance testing requires improvement.

2.

Conclusion

Rating:

2

Trend:

None

3.

Board Recommendation

Licensee: Review adequacy of programs for prioritiz'ation.

NRC:

None

. - .

..

.

. .

.

. . ..

.

.

..

.

.

.

.

..

.

..

,

,

30

-

D.

-Surveillance (8.2%)

1.

Analysis

The previous SALP determined performance in this area . to be

Category 1.

Conservatism was noted in licensee policies for

entering and interpreting Technical Specification action state-

ments.

It- was concluded that the program was effectively

managed utilizing good procedures which were rarely violated. It

was noted that a significant problem existed with erosion of

steam piping and that a more aggressive corrective action pro-

gram was needed.

The resident inspectors examined surveillance activities as part

of the routine inspection program. Three inspections by region

based personnel examined activities associated with two plant

ten year In Service Inspections (ISI).

Surveillance activities

related to specific areas of inspection were reviewed during

several additional inspections conducted by NRR and region based

personnel.

The surveillance /ISI program continued to be effectively managed

with only one minor instance of a missed surveillance (radio-

chemical analyses) as discussed in Section IV.B.

Methods for

scheduling tests improved. In addition to the normal surveil-

lance testing /ISI workload, additional effort was required to

successfally complete two ten year in service inspections.

In-

-

creased effort and resources were dedicated to the secondary

piping corrosion / erosion inspection and replacement program.

There were ne, instances of low pressure steam line ruptures, as

had occurred previously, during this period.

As noted in previous SALP reports, workers performing tests and

inspections were knowledgeable of the systems and testing

requirements, and QC involvement was evident.

Licensee policies and procedures did not adequately address

intermittent equipment failures or significant degradations when

the equipment, without undergoing corrective maintenance, was

retested and functioned properly.

Those procedures permitted

such equipment to be declared operable without first requiring

either root cause determination and correction or, in cases

where the root cause cannot be immediately identified, thorough

evaluation of operability and need for compensatory actions.

They also were weak in requiring documentation of these failures

and degradations.

This allowed a problem with intermittent

. .

__

,

_ _ - _ - _ _ _ _ - _ _

__ _ _ _ _ _ - _ _

_ _ _ . _ _ _ _

__-

_

_ _ - - _. _ _ _ _ _ -

. _ _ _ _ _ _ _ - .

_ _ - _ _ .

..

~

31

tripping of the steam driven auxiliary feedwater pumps to per-

sist for an extended period without being recognized by plant

management and demonstrated that the surveillance program was

not being used as effectively as possible in identifying equip-

ment performance and reliability problems.

Such experiences

indiccte that equipment operability has been adversely affected

by inadequate recognition and communications of surveillance

problems as well as a lack of thoroughness in troubleshooting -

and root cause analysis.

POSRC review and plant management

actions on operability issues appear to have been more keyed

towards Technical Specification compliance than on reliability

and safety.

.

The following deficiencies were noted during the period. They

appeared to be unrelated in nature and not indicative of any

significant programmatic weaknesses. Problems were noted by the

NRC and the licensee's QA group with 1.nproper segregation and

storage of out-of-calibration measuring / test equipment.

Three

inadequacies of a more significant nature were .found by the

licensee and NRC in surveillance test procedures. One resulted

in long term inoperability of the wide range noble gas monitors,

the second in inadequate testing of a dynamic response circuit

in the Reactor Protective System, and the third in a failure to

periodically verify closure of certain containment penetrations

prior to movement of irradiated fuel.

As discussed in the Engineering Support functional area, the

licensee has become more proactive in identifying deficiencies.

Examples in the surveillance area of this overall trend in-

cluded:

system engineer discovery of two of the surveillance

test procedure deficiencies noted above, the conduct of a steam

generator tube inspection program that exceeded regulatory

requirements, and continued conduct of an aggressive secondary

piping inspection and replacement program. Another example of

particular note was licensee adaptation, as an industry first,

of current state of the art ultrasonic examination technology to

the field (UDRPS system) and successful use of this system dur-

ing two ten year In Service Inspections. The use of this system

enabled the licensee to conduct inspections which, in many

cases, exceeded regulatory requirements.

The In-Service Inspection (ISI) group and the metallurgical

engineering group which supports ISI activities have histor-

ically been staffed by very technically competent individuals.

This strength continued throughout this assessment period.

In

_ - - - _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ -

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _

__

_ - - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _

.-

.

32

addition to ISI activities, both groups provided valuable sup-

port to the plant in assessing emerging problems such as reactor-

coolant . pump shaft and cover cracking ind; cations. One area for

improvement the licensee was requested to consider, and which

may assist an already very capable ISI staff in achieving

superior performance, would be the addition of an- independent

Level III. Examiner to review all ISI data.

In summary,

the surveillance /ISI program was well managed.

Workers performing . tests and inspections were knowledgeable of

the systems and testing require.

'ts.

The ISI program was

carried out and supported by par:

Jlarly well -qualified per--

sonnel and went beyond regulatory equirements. However, licen-

see

policies and procedures do not adequately address inter-

mittent equipment failures or degradation. Also, the surveil-

lance program was not being used as effectively as possible to

identify equipment performance and reliability problems.

2.

C_onclusien

~

Rating:

2

Trend:

None

3.

Board Recommendation

Licensee:

Assess

overall

controls

(policies,

procedures,

-

reporting requirements, decision making, trending, and assign-

ments of responsibility)' for identifying and resolving inter-

mittent equipment failure problems.

An NRC/ Licensee meeting

should be scheduled to discuss the results of this assessment.

'NRC: None

__ ____

_ _ _ _ _ _ _ _ _ _ _

_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ -

..

'

33

E.

Emergency Preparedness (7.7%)

1.

Analysis

Licensee performance. in- this area was rated as Category 1 during

the

previous

assessment

period based upon

good exercise

performance and the licensee's own initiatives in emergency

preparedness.

During the current assessment period, there were three region-

based inspections of emergency preparedness activities which

included a routir e safety inspection, observation of the annual

exercise, and observation of a follow up remedial drill. Obser-

vations regarding implementation of the site emergency plan

during an approaching hurricane in August 1986 and during the

loss of offsite power event in July 1987 are included.

Emerg-

ency planning was also one of.the key areas examined during the

Operational Safety Review Team (0SART) review.

The licensee adequately addressed deficiencies in previous

exercise performance through appropriate program changes and

retraining.

Concerns remained in the areas of emergency notif-

ications and issuance of protective action recommendations (PAR)

for sheltering, evacuations, and authorization of potassium

iodine (KI) to personnel. During the partial

participation

exercise hela on September 9, 1986, NRC observed sweral signif-

icant weaknesses in the licensee's performance.

A recurring

ceficiency occurred relating to an inadequate decision making

process for pars.

The recommendations made to of fsite author-

ities were untimely and did not exhibit conservatism primarily

due to problems in overall direction and control of the accident

and dose assessment staffs.

Dose assessors were observed to

have difficulty in obtaining proper information for input into

the dose assessment model.

Additional inaccuracies were ob-

served in determination of source terms, release pathways, and

calculation of integrated offsite dose.

The lack of efficiency

'

in information flow between the radiological assessment staff

together with a complacent attitude displayed by key response

personnel were the contributing factors in inadequate and

untimely

recornmendations for protective measures.

Scenario

difficulties and inconsistencies may have contributed to this

delay.

E

e

.

  • -

34

A Confirmatory Action Letter (CAL) was issued following the

exercise which outlined the major deficiencies.

The CAL re-

quested that the licensee take corrective measures by conducting

a review of the ineffective portions of the Emergency Plan and

Implementing Procedures and provide specialized training in weak

areas. On October 16, 1986, a remedial. drill was held to deter-

mine licensee responsiveness to initiatives in the areas of

protective action recommendations, dose assessment, and infor-

mation flow during emergencies.

Licensee performance in the

deficient areas was acceptable during the remedial drill. Acci-

dent assessment, notifications, communications, and protective

action recommendations were timely, but concerns remained about

the effectiveness of the de:e assessment program. The licensee

subsequently implemented changes to radiological

assessment

procedures and staff direction and control assignments for

evaluation and communication of dose projections. The licensee

emphasized the dose assessment area after the remedial drill

through specialized training and drills; improvements were shown

in subsequent drills.

The licensee had ample full-time onsite and corporate staff

assigned. Assistance was also provided by the Training Depart-

ment staff to integrate corrections of deficiencies in exercise

performance or programmatic areas into emergency response train-

ing. Emergency Response Facilities (ERF) were dedicated for

emergency preparedness and were adequately maintained.

The

overall capability of Emergency Operations Facility is excel-

lent. However, improvements could be made in the size and space

availability cf the Technical Support Center.

During an approaching hurricane in August 1986, the licensee

declared an Unusual Event.

Timely, conservative measures were

taken for hurricane preparation.

In July 1987, the plant

l

experienced a significant loss of offsite power event resulting

in the tripping (shut down) of both units, operation in natural

circulation core cooling conditions for an extended period

(approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />), and declaration of an "Alert" condition

in accordance with the site emergency plan.

During the event,

,

!

operations and plant staff personnel responded correctly and

l

properly implemented emergency operation procedures and the

emergency plan.

Communications to the NRC were notably excel-

lent. This event demonstrated the effectiveness of the emerg-

ency plan as well as operations and emergency plan training

programs.

l

-

_

. , . ,

.

.

.

-.- - - - - -

_,

\\

,

.

,

(?

35

i

.<

'

' .

Il

s

.

1

t,

-

$

'

The licensee has ,eitablished a close working relationship with

off . site" of ficials and support groups.

Evidence cf a strong

commitraent to train and inform these groups as well as members

of 'the general public. regarding site activities is evident,

a

In summary, the level of staffing and training to administer

y

'(

basic emergency ' preparedness program functions appears adequate,

x A

however, performance of response persennel during the annual

{ I,'W

,

exercise was parginal . The poor performance appeared to be due

to a complacent attitude and inadequate management attention

-(

rather than a programmatic problem.

The licensee immediately

t.

7

recognized the weakness and performance has improved consid-

(

\\

I

erably since the, annual exercise. This improved perforreance was

demonstrated duriitg the recent loss of all offsite power event.

',1

"

,

,

,

2.

Conclusion

(

<

,

Rating:

Category 2

Trend:

None

.

a

1.

Board Recommendation

r.

,

Licensee: None

NRC:

None

a

\\

L

>

-

-s

8

T

l

J

nom .m.

s.

... . .. _

.y

[

. _-

.

.

.

.

_ .

.

.

.l_Q

r

.

,

,

y

'

<

f

<

36,

$

,

F' .

N:ority 'and / afeguards -('2!29) ,

^

y

.

1

'

1.

Analysis (

>

During the previous SALP - periot, tt e licensee's performance in

this area was Category 1.

W mjor regulatory issues were

-

identified.

,,

There was one physical security and one material control and

accounting inspection conducted by region-based inspectors dur-

,

ing this assessment period.

A mrnagement meeting, at the

request of the. licensee, was held tc discuss the circumstances

of a repetitive violation.

,;

1

.

Both plant and corporate security.tranagement: continue to be

!

aggressively involved in the securitj . program at Calvert Cliffs

-(

and sin nuclear power plant securi i,y , in general.

This was

3

demonstrated by the licensee's concinuing attention to program

L

i s

iy

improvements, e.g., providing a firearms range on owner control-

y

led property adjacent to the site to facilitate i;he maintenance

of firearm skills by members of the security force between

4-

s

requalification periods, the installation of two rhw explosive

'

detectors to facilitate searches at the main entry point to the

,

<

,

protected area, and training program initiatives that are dis-

cussed later in this assessment. Additionally, the licensee was

<-

actively following up on the concerns identified during the

Regulatory Effectiveness Review that was condt.cted in October

-

4

/

1985 by the NRC. Even those findings that were 'not NRC require-

ments were actively pursued by the licensee On an effort to

enhance and upgrade the security systems and we.'e included with

the licensee's previously planned security program upgrades that

'

began in 1982.

Security management also continued , to actively

/

p

interact with other utilities regarding securit9 matters, by

-4

membership in the Region I Nuclear Security Association and

other groups engaged in nuclear plant security matters.

-

' '

Security supervisors were well trained and continued to provide

effective supervision over security force membens who performed

<

'e

their assigned duties in a competent and professional manner.

Security force members were very knowledgeable" and actively

'

encouraged to participate in program implementation and enhance-

ments by making recommendations, particularly duri[.g critiques

after drills and exercises.

The licensee also rentred that

feedback was provided on all routine security duties.

These

0

initiatives were very effective in sustaining the high level of

morale exhibited by members of the security force.

\\

l

.

_ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _

_

N

,. L

';)

,

a

-

n

1

,.

,

Lt

t

  • -
37

'

.4

(

5,#'

The l'icensee deve)cped and implImented a - specialized security

.

training' course fod members < of the site' quality assurance staff

-to enable th:Mf 6 lequipmentn 'tcMnduct a more effective aud1+ fof.l

nel' an Q c

performance.

'I additirdn,. the

licensed gorittnued to maintain effective int 4rface and liaison

with 'lo%1. law enforcement and emergency services : agencies

through periodic meetings and on site drills and familiarization

tours.' Both of-these provided valuable-feedback to the training

program during thf s ass'essrpdt period and were further evidence

of the licensee's interest in implementing an e,ffective security

,

"

program.

During this assessment per od, a "opetitive violation occutted

~

J

involving the. control of vehicles while inside the protected

area.

The licensee requested a management meeting :to discuss

the- previous and additional proposed corrective actions.

The

licensee's corrective actions were extensive and adequate to

<

prevent recurrence. No similar problems were identified during

-the remainder of the assessment period.

The viol.ation identi-

fied in the matr,f al control and accounting area involved the-

licennee's faildre to maintain adequate records to demonstrate

j

i

that physical inventories of special nuclear meterial,s were con--

ducted int accordance with NRC regu'ations / TW7)censee took'

immediate and appropriate action tcr correct arfor ssion in.the

accounting procedure to prevelt recurre*ce. , N ither of the

violations were indicative of a programmatic prcb e% inUprompt

and effective corrective action Jundertaken was 'eddenM yof the

licensee's interest in implementing high ouality' secunty and(

effective safeguard programs,

/

)-

p

x><,

j

Five security event reports were submitted in accordancejwith.

the requirements cf 10 CFR 73.71.

Three reports were r6 quired

,

4

as a rqsult of a recurrent hardware ;>re;bler with th() security

'

computer early in 'the assessment periodf<That problem was pur-

fourth,y the venefor and no recurrence has 'been experienced.

sued b

A

treport, involving the computer,, resulted from an error

madn by a. rraintenance tech ician.

%e fifth >repory <resulted

when a fde bomb-like objeqd was foudd in a building inside the

plant protected area. The 'five events were pro;:orly responded

l

to by the security forcuand appropriate compensatory measures

!

were implecented in each case.

The flicensee's Security Con-

l

i.ingency Pian (SCP), as interpreted by NRC, committed to report-

ing of events, such ar ; the 'three cdmputer related hardware

events, to the TMC

but two such previous events had not been

reported when 'M, occurred.

However, NRC regulations do not

require reportd of such events.

The li';ensee corrected some

ambiguous language / n the SCP that caused the confusion in the

i

reporting commitments.

Each report was clear an# concise and

provided an adequate explanation df the event to enable NRC

analysis.

This demonstrated ptop u management oversight and

l

review of events and reports submitted to NRC.

l

f

'+

,

  1. ,

,

L-

_

.s

,-.

.

,

..

~_

_

.

- , . _

.

,

.I

p

.

,

'

38

-

l

During the assessment period, the licensee submitted three

revisions to the security plan and a revision to the SCP under

the provisions of 10 CFR ' 50.54(p).

Some minor l modifications

were necessary to several changes but only two changes required

additional information.

Plan changes were of high quality' and

demonstrated management's continuing oversight of the program to

ensure it was consistent with NRC performance objectives.

Per-

sonnel-involved in maintaining plans current and consistent with

NRC objectives were very knowledgeable of NRC requirements.

During the assessment period enhancements of the personnel

screening program were made' by implementation of the Nuclear

Employee Data System.

In summary, the licensee continued to maintain an effective

physical security and safeguards program.

Efforts to improve

and upgrade.-the operation and reliability of system and equip-

j

ment and the performance of personnel were continuing.

2.

Conclusion

Rating:

Category 1

Trend:

None

3.

Board Recommendation

.

Mcensee: None

N

None

E:

i

-

-

- ,_ _ _ _ , . - . _ _

- . , . _ , _ - _ _

.

~

39

G.

Refueling, Outage Management (6.7%)

1.

Analysis

The previous SALP included Engineering Support within this area

and

rated this area as Category 2.

Routine activities were

well planned and coordinated.

Strong management influence in

decision making was evident. Good communications and orchestra-

tion of activities were demonstrated resulting in meeting of

scheduies and minimizing man rem exposure.

Two areas, post

accident sampling, and environmental qualification of equipment

lacked sufficient management attention and required NRC invcive-

ment to identify deficiencies.

.

There were two ten year In Service Inspections and refuelings

conducted during this evaluation period. Outage activities mon ~-

itored

included:

pre-outage

planning meetings,

responsible

engineer presentations on Facility Change Requests (FCRs) and

major modifications, morning coordination / status meetings, steam

generator eddy current testing, reactor vessel level instrumen-

tation modifications, refuelings, in service inspection of the

reactor vessel, replacement of reactor coolant pump rotating

assembly, replacement of main steam isolation valves, numerous

other refueling activities,

i.e., leak rate testing, nozzle dams

work, hydrostatic tests, and human factors improvements made in

the control room.

.

Refuelings typically were characterized by good communications,

excellent planning, good control over contractor personnel, and

a strong management involvement.

Engineering's onsite presence demonstrated a notable strength

by providing responsible engineers to brief general supervisors

and principal engineers at pre-outage meetings on all the sched-

uling, support coordination, responsibilities, potential problem

areas, and details of the more complex evolutions planned to

occur during the outage. This process called "Perfect Planning"

brought together all facets of job planning including ALARA

engineering, mock up training, procedures and spare part status,

and ensured all involved personnel were aware of their assigned

responsibilities.

This planning technique was used primarily

for critical path high impact items and jobs that have never

d

been performed before, jobs with significant potential man rem

l

exposure, or with interfaces between many groups. This technique

impro ed the efficiency and reduced exposure for M5!V replace-

ment, core exit thermocouple modifications and RCP rotating

,

1

l

.

.

_

-

'

.

. -

40

,

assembly replacement.

The outage coordination meetings - held

daily tracked critical paths for primary work, secondary work,

refueling and other major job efforts, ensuring delays for any

reason were minimized and necessary support was provided. These

meetings ' facilitated strict adherence to the schedule 'of activ-

ities. Good communications existed between departments and con-

tractors.

Site management were regularl

in attendance.

The

morning meeting and specific technical meetings thereafter were

succinct and effective.

The outage management section, a divisioa of the Operations

Department, utilized senior reactor operators as operations /

maintenance coordinators to facilitate the availability of

equipment, to ensure operations was aware of ongoing maintenance

and to expedite the isolation of equipment though the tagging

authority.

Another good initiative was the use of shift and

area coordinators /facilitators who facilitated material, coor-

dinated and assigned priority to jobs within an area when con-

flicts arose,

i.e., containment coordinator.

4

Outage meetings were periodically supplemented with "pep talks"

from the Vice President stressing quality work, safety first and

doing the job right the first time. Management conveyed clearly

that plant operation was second to safety and quality work.

Beyond a normal refueling, the two refueling outages involved

the following:

two In Service Inspections of reactor vessel

-

components; a problem with #12 Emergency Diesel Generator gas-

sing; main generator collector ring cracks; failure of #118

reactor coolant pump seal after replacing all of the other RCP

seals; replacement of two reactor coolant pump rotating assem-

blies; replacement of about 2,000 feet of secondary steam piping

and repacking about 2,000 valves with a constant load Chesterton

packings; replacement of the MSIVs on each unit; and installa-

tion of a new plant computer.

These were accomplished with a

site person rem exposure of less than the tight goals despite

additional required work and no individual receiving more than 2

rem thereby exhibiting good planning and control.

During these

events, numerous technical problems faced the licensee. Each in

time was reselved in a technically sound and thorough manner.

Despite the problems experienced beyond a normal refueling, both

the refueling and ISI portions were successfully completed. The

added complications, generator collector ring cracking, environ-

mental qualification and mechanical commercial quality issues

extended each outage, however these did not appear to influence

.

the licensee's well coordinated persistent pace.

Personnel

i

attitudes and morale remained high despite the setbacks.

,

.

,.~,

-,--4

- , . , . . .

.

.,-.-,._._..y...

- , , _ _ _ , - , ,

._.-.--_,,,..---~%

.

-

_ _ _ _ _ _ _

.

-

41

Some problems, however, appeared to be persistent. Upon return-

ing to power operations, an excessive number of maintenance

requests remained outstanding. Some of this was attributable to

the marginal post maintenance test program and the limited

resuurces in wintenance.

However, another contributing factor

was the licensee's tolerance to live with out of service or

deficient equipment upon return to power operation (see also

maintenance functional area).

Another area of concern was the amount of debris in the reactor

coolant system. During tha current fuel cycle, coolant activity

on Unit 2 has been relatively high, 5 micro curies per cubic

centimeter gross activity and 0.3 micco curies per cubic centi-

meter dose equivalent Iodine 131.

This appears to be caused by

debris within the RCS causing fuel pin failures.

The failure

mechanism appears to be debris-related fretting, indicating that

material control practices during outages while systems were

open were weak.

Clean area controls during refueling were

strictly adhered too around the reactor vessel .

However, the

controls was not so strict around other arear where the primary

system was cpen.

The licensee first cle,rly recognized this

problem af ter examining the fuel during this outage.

As an

initial corrective action step the licensee stressed cleanliness

controls in the Calvert Cliffs News Letter to heighten employees

sensitivity to the issue.

Further procedural controls are

planned for future outages.

Similarly, overall housekeeping

significantly declined during the outages, particularly in some

-

contaminated areas as discussed in previous functional areas.

In summary, outages and refuelings were well managed.

Opera-

tions personnel and other outage coordinators /facilitators were

effective in achieving good coordination of activities including

unexpected problems encounters. . ate in the refueling outages.

In

particular,

planned maintenance,

in-service inspeccions,

nodifications and major outage usks were effectively scheduled,

nordinated and managed. Despite the good overall management of

outages, problems were noted near the end of the period as

housekeeping in contaminated areas dt.+.erioratea and the plants

were returned to service with an eacessive number of maintenance

requests outstanding and equipment out-of-service.

2.

Conclusion

Rating:

Category 1

Trend:

Declining

3.

Board Recommendation

Licensee:

Set goals for minimizing out of service equipment

before returning to power operations.

NRC:

None

___

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - . _ _ _ _ _ _ _ _ _ - . - - - _ _ _ _ _ _ _ _ _ _

_ _ . _ _ _ _ _ _ _ _ _

______________J

.

42

.*-

H.

Engineering Support ( 6.8*4)

1.

Analysi s

Although this area was not rated separately in the previous

SALP, problems were . identified with (1) a lack of management

attention in the establishment of a viable Equipment Qualifica-

tion (EQ) program and (2) inadequate orchestration of multi-

disciplined tasks in that responsibility and authority were not

vested in individuals in such a manner to ensure effective task

completion. This area was covered as a part of several individ-

ual and team inspections during this assessment period. Further.

evidence of the above concerns was seen during this assessment

period.

Specifically, they were the root causes of significant

deficiencies identified in the EQ program.

Those deficiencies

primarily involved the use of unqualified taped electrical

splices. -The second problem continued to exist in that the

roles and responsibilities of systems engineers (individuals who

are key coordinators in assuring proper maintena.nce, perform-

ance, and design improvement of plant systems) were found to be

p6orly addressed in plant procedures and appeared to be too

broad, thus reducing the effectiveness of this function.

Related to the above problems, communications, both formal and

informal, between engineering and other plant groups were weak.

For example, important mechanisms for communicating engineering

requirements to the field were unclear.

Similarly, the engi-

neering personnel were not made aware of the fact that the set-

points for certain Reactor Protection System (RPS) constants

were net being adjusted to values recommended by the NSSS vendor

following core reloads. The licensee has experienced difficulty

in getting engineers out of their office area and into the plant

and communicating with operational and maintenance personnel to

more fully realize the benefits of the relocation of all engi-

neering functions to the site.

The EQ issue pointed out a failure of engineering department and

plant management to give credence to and heed the advan::e warn-

ings of both the QA grtup ar.d the NRC of program weaknesses.

It

also pointed cut a need for management to more frequently

utilize third party expertise to provide assessments of the ade-

quacy of more specialized or technically complex programs.

1

_ . _ _

..

.

. _ _ _ _ _

__ _

_

__

._.

. _- .-_ _

.

-43

~

During. this period, the licensee pursued an emergency diesel

generator gassing problen which was originally thought to be

only slightly excessive. As the licensee pursued the problem,

it became worse and more complicated durir.g repair attempts

requiring several changes to the Technical Specifications.

The

licensee was candid and responsive to. NRC concerns which facil-

itated an acceptable and timely resolution, however, communica-

tion with- NRC on the issues exhibited a lack of coordination

between engineering and operations.

'

,

During the assessment period, a great deal of licensee manage-

,

ment and NRC attention was focused on the engineering depart-

'

ment.-

Licensee managers now recognize that tho engineering

function was operating unc'er resource' constraints that, at least

in part, prevented (1) the timely close out of Facility Change-

.

Requests for which - physical work has been completed (approxi-

!

mately 400 changes outstanding near the end of the SALP period),

(2) better root cause analysis - of plant maintenance problems,

(3) timely engineering of facility modifications, and (4) needed

improvements in engineering tools

(e.g.,

improved means for

determining and maintaining design basis information).

Resource

constraints additionally s1 wed the development of a performance

based training program fo. the engineers.

The fact that the

general experience level of the systems engineers was low added

'

emphasis to the need for such a training program. Additionally,

.

-the engineering department iad internal and/or external commit-

l

ments to complete final corr ?ctive actions for the EQ and MCQ

-

issues, complete upgrades in the 0-list, and to develop master

'

calibration

data

sneets

in

supprt

of

I&C

nmintenance

activities.

While pe rforman: e in the engineering support area

was hindered by work overloae, it also suffered from inefficient

,

control

cod

t. s e of exist'.1g resources due to insufficient

prioritization c.r.d poor coor dinstion.

Immediately prior to and Juting the assessment period, all

.

engineering support functions for the plant, with the exception

of the metallurgical engineer cg group, were moved to the site

and consclidated under one t ,:: ear Engineering Services Depart-

ment.

At the same time, ite systems engineer function was

implemented.

The consolidat'v, coupled with two 10 year ISI

and refueling outages and several plant problems as discussed

previously placed considerable stress on the engineering organ-

ization.

In spite of this and extending beyond response to

i

crisis situations, there were notable accomplishments which

benefitted the plant and which indicate strong potential for the

'

engineering

group,

with

proper

development,

to

further

contribute to the overall improvement of plant operation and

maintenance.

- , . - _ . -

_ _ _

_

.

4

44

l

(1) The Engineering Department directed the efforts of the

"Trip Evaluation Review Group (TERG)".

As noted in the

operations section,

this group successfully identified

-problems' in the feedwater _ control systerr.

Two reactor

trips were caused by failures of reactor coolant pump (RCP)

capacitors. Engineering performed testing to determine if

tne capacitors could be replaced with an-alternative.

Cur-'

rently, a modification is in progress to replace the

capacitors with inductors.

There have been no repetitive

r2 actor trips due to the same cause or unidentified root-

cause since TERG establishment except for the RCP-capacitor

failures.

(2) The organization has become more proactive in identifying

deficiencies.

For example, engineering personnel identi-

fied the MCQ fastener and the RPS set point problems, and

they discovered a significant error in vendor guidance for

calibration of the wide range noble gas monitors. This was

partially due to systems engineers being available to pro-

vide focused attention on assigned systems.

(3) The engineering group provided two useful tools for pre-

dictive maintenance through development of the oil analysis

program and enhancements in the equipment vibration mon-

itoring and analysis program.

(4) The engineering departrent's ISI group and the metallur-

gical laboratory group took state of the art ultrasonic

examination technology and, as an industry first, adopted

it to the field (UDRPS system). This system was then very

successfully used during two 10 year ISI inspections. Also,

for the first time, a zero channel head entry device

(SM-10) was used on a CE designed plant for steam generator

tube eddy current inspection which resulted in an estimated

10 man rem exposure reduction per unit. The ISI group and

the metallurgical laboratory group have historically been

staffed by very technically competent individuals.

These

individuals also provided valuable support to the plant in

analyzing reactor coolant pump shaft and cover cracking

problems.

(5) The licensee's secondary piping inspection / replacement pro-

gram continued to receive high priority.

(6) Upon the initiative of the QA group, immediately following

the SALP period the licensee performed a proactive, in-

house inspection similar to the NRC Safety System Func-

tional Inspection (SSFI) to examine engineering configura-

tion controls. A contractor familiar with SSFI techniques

assisted them in this effort.

.__

.-

'

.

..

~

45

(7)' 500 safety-related loop drawings were- developed to better

support

Electrical

& Controls maintenance activities.

(8) Although progress was slow,_some of the long-standing tech-

nical problems have been resolved 'or appear to _be on the

path to resolution. Examples include: replacement'of high

maintenance requirement main steam line isolation valves

with components of superior design, improved packing. per-

formance for the charging pumps, improved reactor coolant

pump seal rebuild capability, intake structure traveling

screen / screen wash system improvements, and updating of

Unit 2 main feedwater controls.

In summa ry , the consolidation and movement -of all engineering

functions to the site and the implementation of the systems

engineer concept were positive steps toward improving engineer-

ing support of the plant.

Problems still existed with:

(1)

full integration of the Nuclear Engineering Services Department

into the plant staff which includes improved communications as

well as systems engineer training and involvement with opera-

tions/ maintenance personnel to improve engineer credibility and

effectiveness; (2) assessment and, where needed, redefinition of

the roles / responsibilities of systems engineers; (3) for multi-

discipline tasks, lack of clear assignment of responsibility;

(4) providing the necessary resources ~to complete corrective

'

actions for past problems (e.g., EQ, MCQ, FCR backlog) and to

providing better maintenance support and to resolve long stand-

-

ing technical problems; and (5) ensuring appropriate management

attention is given to identified deficiencies (e.g., QA findings

and recommendations).

Several corrective actions have been

initiated (e.g. , team training for managers, daily operations /

maintenance / engineering meetings).

Accomplishment of such a

large agenda of improvement efforts will require dedicated and

skillful management attention.

During the latter part of the

assessment period, areas of improvement were noted.

These

included system engineer identification of problems,

self-

identification and correction of MCQ problems, the SSFI initia-

tive to evaluate engineering configuration controls and improved

engineering support for the licensing functional ereas.

2.

Conclusion

Rating:

Category 3

Trend:

Improving

.

-

46

3.

Board Recommendation

Licensee:

Perform independent assessment of the engineering

organization which identifies engineering functions and includes

a review of the overall system for establishing priorities,

assigning responsibilities, and obtaining resources.

NRC:

None

.

!

[

l

l

I

l

1

l

l

l

l

_ _ _ _

.

47

-

I.

Licensing Activities

(1.9%)

1.

Analysis

This licensee was rated Category 1 in this functional area for

the previous SALP evaluation period. Management involvement and

control of licensing activities, as well as licensee responsive-

ness to NRC initiatives were viewed as strengths because the

licensee assisted in resolving several NRC initiatives and its

submittals were of high quality with noted improvement in the no

significant hazards analysis provided in support of Technical

Specification (TS) amendment requests. Weakness was noted only

in the communications between the operations and licensing

staffs concerning the reliability of equipment controlled by TS.

During the current SALP evaluation period, a number of signifi-

cant occurrences had a decided impact upon the evaluation of the

licensee in this functional area.

These occurrences included

(1) the degrdation of the #12 emergency diesel generator (EDG)

which necessitated one exigent and two emergency TS amendment

requests, (2) the licensee's shift to a 24-month operating cycle

which necessitated submittal and review of a wide range of TS

4.mendment requests, and (3) the licensee's discovery of environ-

mental qualification deficiencies and of the improper use of

uncertified material replacement parts.

Licensing activiths

are summarized in Table 5.

.

In responding to .1ese occurrences and to other issues and

even'.s over the course of the SALP ra+ing period, the licensee

demonstrated generally good management overview with respect to

licensing

activities.

The

senior

engineering

management

actively participated in these actions by orioritizing these

actions with the concurrence of the Manager of Nuclear Opera-

tions. Assignment of priority was based upon the impact on cur-

rent or future planned plant operations and upon the licensee's

evaluati;n of the safety significance of the item.

Generally, the licensee responded to the NRC ii a timely manner,

particularly, with regard to requests for additional information

made to obtain technical support for licensee requested activ-

ities. Licensee responses to NRC initiated issues were normally

thorough and of high technical quality.

Response was not as

prompt to NRC issues of generic concern.

Due to a staffing

shortage, the licensing activities prioritization scheme adver-

sely impacted the timeliness of NRC requested and required

licensing activities which the licensee of ten viewed as a lower

priority.

As a result, senior management diverted manpower

_ _ _ _ _ - _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_.

_ _ _ _ _ _ - -

_ _ _ _ _ .

____ ____ ___ ______ __- _ __

-

..

,

-

48

resources away from these NRC initiated activities 'to those

deemed to be more in the interest of the utility. The licensee

requested extensions for responding to several NRC generic

letters and deferred action on SPOS

opera'ility,

Dedicated

o

Control Room Design Review and the annual FSAR update.

Senior management attention towards NRC . licensing requirements

during this rating period was found to be inconsistent with

regards to ensuring licensee compliance with the various report-

ing requirements.

Several required reports were filed late and

'

some annually required reports (e.g., challenges to and failures

of the pressurizer PORV's and code safety valves) had not been

filed for several years. No licensee unit was tasked with the

responsibility for or the authority to ensure that these reports

were submitted as required.

The licensee possesses significant technical capabilities in

most of the engineering and scientific disciplines necessary to

resolve issues of concern to the NRC and the licensee. However,

in several instance > these capabilities were not reflected in

the quality of the submittals. Most of the licensee's evalua-

tions of the significant hazards considerations were accurate

though brief, thus routinely requiring additional information to

>

justify the request.

The licensee has characterized every

amendment request submitted during the rating period as not

presenting any possible significant hazards considerations.

In

three instances, however, the NRC determined that these charac-

-

terizations of the amendment requests were not justifiable based

upon technical facts.

Several instances of poor senior management review and/or inade-

quate engineering analysis occurred during this rating period.

.

!

These instances included: (1) a requestad TS main steam isola-

tion valve closure time limit, tested under no steam flow condi-

i

tions, that would have placed the plant outside the analyzed

bounds of the steam line break design basis event; (2) a change

to the NRC approved peak reactor coolant system (RCS) pressure

limit for the feed line break (FLB) event from 110% design RCS

pressure to 120% design RCS pressure in the FLB event's safety

analysis. This was made to justify a proposed increase in the

moderator temperature coefficient limit.

This change in peak

pressure was not indicated in the licensee's TS amendment re-

,

quest.

This peak pressure change was not reviewed by the

i

licensee's safety review committees; (3) the justification for

continued Unit 1 operation with an existing flaw in the main

steam line was technically deficient; and (4) numerous technical

inconsistencies and regulatory inadequacies existed in the

,

licensee's submittals of the exigent and the first of two

!

emergency TS amendment requests for the #12 EDG.

. - -

- - __ -

- - - - , - -

- ---. ---

~_-

,

-

'

49

Over the last six months, marked improvement has been observed

with respect to senior management involvement in and the quality

of the technical responses to non-routine licensing activities,

particularly the environmental qualification and replacement

parts certification -deficiencies arising at Calvert' Cliffs.

,

Licensing issues were carried out by three different groups in

the Technical Services Engineering section of Nuclear Engt:eer-

ing Services. Primary NRC/ licensee interface was with the Fuel

Cycle Management unit, and the Licensing and Operational Safety

uni * . The third group that carried out licensing activities was

the Analytical Support unit. NRC interface with this unit was

minimal.

The Licensing unit was capably staffed though there was a staff

turnover of approximately 45% during this rating period. _Though

the level of experience appreciably declined, this unit's work

.,

product continually and significantly improved due to the per-

sistence and dedication of the unit's staff and to the quality

of training provided.

NRC communications with the Licensing

unit were marked with good relations, a high degree of coopera-

tion and a free exchange of information.

This unit actively

sought to improve communications.

The Fuel Cycle Management unit had an experienced staff with

significant expertise in the technical issues of fuels manage-

ment. Staff turnover was low.

The quality of this unit's work

-

product

remained adequate during this period with no signifi-

cant decline or improvement noted. However, many tasks assigned

to this unit remained incomplete over periods of several years.

For example, the Fuel Cycle Management Facility Change Request

(FCR) process is used to initiate TS changes, core reloads and

other related changes; and modifications, tests and experiments

as permitted under 10 CFR 50.59. No FCRs have been completed by

this unit since April 1983 although 24 such actions, including 5

core reloads and 10 TS amendments (9 of which were approved by

the NRC) were initiated since this date.

The licensee attri-

buted this failure to insufficient manpower. The licensee also

attributed this unit's failure to maintain its training records

to this manpower shortage.

Communications with this unit were

adequate though they were hesitant to inform the NRC of problems

with licensing actions in a timely manner.

In summary, the licensee's greatest strengths were the signifi-

cant technical capabilities that its staff possesses and the

management's recently demonstrated determination to improve the

quality of their licensing actions, as particularly demonstrated

through the improvements in performance level made by the Licen-

sing and Operational Safety unit.

Still, improvement is needed

in (1) in the quality and level of management overview, (2) the

.

'

50

quality and comprehensiveness of the hazards analyses provided

by the various engineering units to support licensing's develop-

ment of justifications for TS amendment requests, and (3) the

staffing level required to parmit response to NRC initiatives in

a more timely fashion and to permit the staff to perform all

tasks that are required, particularly for Fuel Cycle Management.

2.

Conclusion

Rating:

Category 2

Trend:

None

3.

Board Recommendation

Licensee: None

NRC:

None

.

-_

_ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _

. . .

'

51

.

J.

Assurance of Quality (0.0%)

1.

Analysis

'

The primary purpose of this functional area is to assess the

effectiveness of the licensee's program for identifying and cor-

'

recting problems.

It includes management control, verification.

and oversight activities which affect or assure the quality of

plant activities,--structures, systems, and components.

It also

,

assesses the attitude and performance of plant staff personnel.

Various aspects of this area were routinely examined as part of

the resident inspector and region-based specialist inspection

programs. A specific QA program review was performed as part of

one team inspection.

!

The previous SALP noted that although an extensive quality pro-

.

'

gram existed throughout the organization, its effectiveness in

incorporating quality into such important plant activities as

identification of root causes of plant trips and installation of

the Post Accident Sampling System was not clearly visible. QA

t

audits were often quite superficial and were not identifying

,

real

problems and root causes.

A Category 2 rating was

assigned.

.

'

In response to these concerns, immediately before and during

this assessment period, several improvements were made.

More

i

-

technically-oriented personnel with a wide variety of plant and

engineering experience were added to the QA unit.

The former

,

General Supervisor, Operations was assigned to manage the QA

unit and has helped to refocus attention more on technical and

performance aspects of areas reviewed rather than just on QA

programs. The findings and recommendations included in several

audit reports during the period were candid and demonstrated

,

l

that deeper levels of insight were being gained into subject

i

areas.

The "Trip Evaluation Review Group" concept was imple-

'

!

mented, and that group was effectively utilized in identi fying

root causes of plant trips.

Increased emphasis was placed on

,

(

interdepartmental

coordination

and

planning

for

major

j

modifications.

During the previous SALP period the licensee consolidated all

departments with nuclear

responsibilities

under

one

vice

president and moved all of these departments to the plant site.

One objective of the move was to improve communications and

interfaces between departments.

The consolidation has had

i

!

_ _ _ _ _ _

_ _ _ _

__

_ _ - _ _ _ - _

_ _ _ _ _ _ _ _ _ _ _ _ - _

_ _ .

_

9-

%

'

52

.

beneficial

effects

this period

as evidenced by increased

involvement of engineering in ' resolving daily plant problems.

The Operations department began to better prioritize anc commun-

.icate its needs for support to both the maintenance.and engi-

neering departments.

Many examples 'were noted- where inter-

departmental interfaces were effective such as in the conduct of

outage activities and in response to emergent equipment problems

such as reactor coolant pump shaft cracking. However, the dis-

covery of major deficiencies in the Equipment Qualification' (EQ)

program and, later, the discovery by the licensee of problems

with use of mechanical commercial quality (MCQ) fasteners demon-

strated that some of the interdepartmental interface problems

,

that had existed prior to the reorganization were still present

c

and were significant.

For example, documents providing engi-

neering guidance to craf t personnel were inadequate. Engineer-

ing personnel were not aware of improper as-built or as-

maintained conditions in the field. Additionally, it was noted

that the licensee was experiencing problems in fully integrating

engineering personnel into the plant staff and in defining their

responsibilities.

Senior management involvement and oversight was weak throughout

the establishment of EQ program.

Although clear warnings of

problems were provided (before and following the reorganization)

by both the NRC and the licensee's QA group, sufficient manage-

ment attention was not paid to them.

The fact that the licensee has of ten demonstrated their capa-

bility to work as a team in successfully resolving plant prob-

lems once those problems are fully recognized by senior plant

+

management suggests that the more significant weakness of

management may lie in their tools and abilities for perceiving

problems.

For example, management did not recognize the need

for third party expertise to provide an independent assessment

,

of the EQ program. In the area of safety review committees, the

Off Site Safety Review Committee (OSSRC) was principally made up

of on site managers. With such strong day to day involvement in

plant activities, members are less likely to be able to provide

independent views on plant activities and may be slow to

recognize emerging plant problems.

The high proportion of

operations department membership on and control of the Plant

Operations and Safety Review Committee (POSRC) has the potential

,

for unduly biasing that committee toward operation and may

<

thereby lessen its effectiveness in identifying safety concerns.

In the area of plant operation, the licensee lacks a policy to

4

uniformly ensure aggressive pursuit of the root cause of inter-

,

mittent failures of plant equipment.

Very little trending of

equipment performance is done to identify imper.di ng failures.

I

-.m-

m

u

.

53

The licensee has taken several new initiatives which address

some of these problems.

The QA unit recently began using out-

side consultants in specialty areas.

For example, immediately

following the SALP period, a consultant was used to perform an

inspection similar in nature to the NRC's Safaty System Func-

tional

Inspections (SSFI).

Additionally, QA personnel were

being used to investigate plant events and make corrective

action recommendations to the POSRC.

In combination, these

efforts appear to improve the credibility of the QA unit with

line organizations as well as adding effectiveness to QA func-

tions.

The upgrades in QA helped the licensee to become more

proactive in identifying their problems. Evidence was also seen

of other plant groups becoming increasingly proactive.

For

example, problems with the use of commercial quality fasteners

g

in code class systems and insertion of improper values for cer-

tain constants in the Reactor Protection System were identified.

New programs were developed to provide early indication of

impending equipment failures (oil analysis and vibration pro-

grams). There wu strong management support for using state of

the art equipment in performing ISI inspections which exceeded

code requirements and increased resources were expended on iden-

tification and precautionary replacement of secondary piping

subject to erosion / corrosion problems. Of significant note, the

licensee volunteered for and participated in the first Inter-

national Atomic Energy Agency (IAEA) Operational Safety Review

Team (0SART) Inspection conducted in the United States.

.

In general, plant employees are well trained, highly motivated

and well supervised at the first line level.

I;owever staffing

constraints appear to hamper the ability of the maintenance and

engineering departments to support operations in areas such as

final close out of Facility Change Requests (FCRs), timely up-

date of engineering construction standards, timely engineering

of needed facility modifications, and correction of control room

deficiencies.

In several areas such as outage management and control, radia-

tion protection and security, effective programs and initiatives

have been implemented thereby assuring quality in these areas as

discussed earlier in this report.

For example, the licensee's

radiation protection and ALARA programs continued throughout the

period to be effective in reducing overall personnel exposures.

The quality of personnel screening was enhanced through imple-

mentation of the Nuclear Employee Data System which is a coop-

erative ef fort by several utilities to exchange security and

health

physics

information

on

employees

and

contractor

personnel.

_ _ .

_ _ _.

__

_

_

__

-

_ _ _

.

54

In summary, weaknesses were ated in senior management control

of interfaces between departments and ability to get departments

to function together more effectively as a team.

Although

significant improvements have been made in the QA group, manage-

ment was not effectively utilizing the information they pro-

vided. Potential weaknesses were seen in the ability of licen-

see senior management to perceive plant problems and determine

root causes and in the safety committees' abilities to provide

independent views on plant activities to management.

Resource

constraints are hampering the ability of the maintenance and

engineering departments

to

support

the

operations

group.

Several initiatives were taken by the licensee during the period

to help the organization become more proactive in identi fying

plant problems. These included participation in the first OSART

inspection conducted in the United States.

Plant personnel are

highly motivated and,

in general, well qualified and well

supervised at the first line level.

2.

Conclusion

Rating:

Category 2

Trend:

None

3.

Board Recommendation

Licensee:

-

,

(1) Review composition of POSRC and OSSRC to determine if they

are sufficiently independent from plant operations to pro-

vide objective assessment and root cause analysis.

(2) Senior corporate management attention is needed to assure

proper functioning of the operations-maintenance-engineering

on-site interface.

NRC: Perform an integrated performance appraisal

inspection

concentrating

on

the

functioning

of

departmental

interfaces.

- _ _ _ _ _ _ _ _ _ - _

, . . ..

, .

.

.. ..

.

.

..

..

..

.. . .

.

_ _ _ _ _ _

gE

55

K.

Training and Qualification Effectiveness (0.0%)

1.

Analysis

The previous SALP recognized that the licensee had expended

significant resources in upgrading training facilities and pro-

grams.

It pointed out that significant improvements were made

in a previously weak maintenance training program, however the

effectiveness of those improvements was not yet apparent. Appro-

'

priate . management attention was being devoted to training.

A

Category 2 rating was assigned.

Although attributes of this topic are discussed in other SALP

.,

functional areas, the topic is segregated here because of its

importance, and to provide a synopsis of the training and qual-

ification programs.

Training effectiveness was assessed pri-

marily by observations of performance of licensee personnel and

reviews of- non-licensed staff training and training associated

with the post accident sampling system, solid radwAste handling,

and health physics activities. An NRC team inspection, in part,

assessed engineering staff training. NRC licensing examinations

were administered twice during the assessment period.

During this assessment period, the licensee continued to dedi-

cate significant attention and resources to training.

In May

1987, the final five training programs requiring INP0 accredi-

tation were accredited. With all 10 of their training programs

accredited, the licensee is now a member of the National Academy

for Nuclear Training.

Beyond accreditation the licensee is continuing to upgrade

training programs.

For instance, the 1986 operator requalifi-

cation examinations more accurately assessed cperator capabil-

ities to perform job functions by greater usage of questions

dealing with real-life situations.

In cooperation with the

University of Maryland, the licensee is developing an educa-

tional proseam, offered on site, which will lead to a Bachelor's

degree in Nuclear Science.

Some courses in the program have

already been provided to interested employees.

Based upon an

analysis of systems engineer job functions (i.e.,

performance-

based analysis), training needs were assessed, and a systems

engineer training program was developed. Implementation of this

program began immediately following the SALP period.

During

outages, maintenance and technical staff training instructors

joined plant maintenance crews,

thereby contributing their

expertise and example to craf t r.ctivities as well as enhancing

their credibility with field personnel

and updating their

knowledge of current plant problems.

!

_ _ _ _ _ _ _ .

.

56

The license training program for operators was effective in

preparing candidates for examination (further detail is provided

in the plant operations analysis section). The training program

for shift engineers was excellent in that it included senior

operator training / examination as well as shif t technical advisor

training.

Additionally,

those individuals received further

on-the-job training by virtue of being fully utilized on shift

as control room supervisors.

In July 1987, the plant experienced a significant loss of off-

site power event resulting in the tripping (shut down) of both

units, operation in natural circulation core cooling conditions

for an extended period (approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />), and declaration

of an "Alert" condition in accordance with the site emergency

plan.

During the event, operations and plant staff personnel

responded correctly and properly implemented emergency operating

procedures and the emergency plan.

Communications to the NRC

were excellent.

This event demonstrated the effectiveness of

the operator and emergency plan training programs.

Effec'ive training was also evident in two very specific areas,

post

accident

sampling

and

steam

generator

nozzle

dam

installation / removal (which resulted in low man-rem exposures).

The general experience level of system engineers was low. As

noted above a training program for these individuals was only in

the initial stages of implementation. Although NRC inspections

have not specifically identified plant problems attributable to

engineer training deficiencies, inspectors did note that oper-

ators and technicians generally lack confidence in the level of

knowledge of the system engineers.

Therefore, the engineers

were not typically viewed as a useful source of expertise in

solving technical problems.

Training weaknesses contributed to two major problems in the

maintenance area. Maintenance planning, QC and craft personnel

were not sufficiently aware of engineering requirements for

replacement mechanical fasteners. As a result, commercial qual-

ity fasteners were improperly installed in ASME Code Class I,

II, and III systems.

Similarly, Electrical and Controls per-

sonnel

lacked sufficient guidance and training to properly

install electrical splices for equipment included in the elec-

trical equipment qualification (EQ) program.

.

57

-

Three reportable events, although not principally caused by

training deficiencies, did indicate ' weaknesses in (1) non-

licensed operator understanding of the safety significance and

administrative controls associated with refueling water tank

level switches, (2) non-licensed operator understanding of the

operating principle of the condenser air removal system which

caused a unit trip, and (3) licensed operator ability to fully

anticipate and control axial flux distribution during plant

start up near end of core life.

In summary, the licensee continued to provide the necessary

resources and management attention to training.

Emphasis is

needed in training craft and QC personnel on engineering

requirements.

Because craft training programs have only been

recently finalized and accrt:dited, their effectiveness could not

be fully assessed.

Adequate training was not provided for

engineering personnel and was a significant weakness.

2.

Conclusion

Rating:

Category 2

Trend:

Improving

3.

Board Recommendation

Licensee: None

-

.NRC :

None

.

.. .

.

.

.

.

_ _ _ _ .

.

58

-

V.

SUPPORTING DATA AND SUMMARY

A.

Investigations and Allegations Review

Two allegations were received in April 1986 regarding personnel

"Jimmying" a high radiation door and that additional keys to high

radiation areas were maintained by several people within the plant

and were generally uncontrolled.

These were

substantiated.

A

violation was issued and licensee response was prompt and effective.

B.

Escalated Enforcement Actions

1.

Civil Penalties

None.

2.

Orders

None.

3.

Confirmatory Action Letters

October

1,

1986 Confirmatory Action Letter issued concerning

deficiencies identified in Emergency Preparedness exercise. A

remedial drill was held with acceptable results.

C.

Licensee Conferences Held During The Assessment Period

April 28, 1987 - Enforcement Conference at Recion I to discuss de-

tails of the isolation of the refueling water tank level switches

resulting in the loss of the automatic feature of the RAS.

May 6,

1987 - Enforcement Conference at Region I to discuss under-

lying causes of violations noted in the Environmental Qualification

Program.

July 13,1987 - Senior NRC manager.ent met with senior BG&E management

at Bethesda, Md. to discuss %dicators of declining performance.

D.

Review of Licensee Event Reports Submitted by the Licensee

The overall quality of Licensee Event Reports (LERs) is good. Over

the assessment period there was a significant improvement noted in

the discussions of safety consequences. Improvements were also noted

in discussions of corrective actions and operator actions.

Areas

which would benefit from added attention lxiude descriptions of

personnel / procedure errors, component failures and safety system

responses.

_ _ _ . . . . _ . . . . .

._

.

59

-

Two LERs (317/86-04 and 318/86-06) concerned failed reactor coolant

pump surge capacitors.

Those failures led to reactor trips. A mod-

ification to remove the capacitors and use inductors for surge sup-

pression is nearing the end of the engineering design phase.

Two LERs (318/87-03 and 318/87-04) reported repeat cracking on a

branch line for a relief valve for the Low Pressure Safety Injection

System.

Three LERs (318/86-04, 318/86-07, and 318/87-02) involved grounds and

component failu ce in Unit 2 feed water control systems. Corrective

actions taken in s,.is area may have largely resolved the problems as

evidenced by no recurrences for a major portion of the SALP period.

Two LERs (317/87-07 and 317/87-09) describe problems with improper

electrical splices on components in the Equipment Qualification pro-

gram and use of improper fasteners in code class systems. Both prob-

lems largely resulted from inadequate engineering guidance to field

personnel.

Four LERs (317/87-03, 317/87-05, 317/87-08, and 317/87-11) involved

personnel, errors and three LERs (317/86-07, 317/87-04, and 318/87-05)

involved procedure errors.

%

..y

...

TABLE 1

INSPECTION REPORT ACTIVITIES-

REPORT NUMBERS

TYPEJ

TOTAL'

INSPEJTION DATES INSPECTION

HOURS

' DESCRIPTION

86-09

86-09

RESIDENT

247.

ROUTINE RESIDENT INSPECTION

05/01/86 06/30/86

86-10

86-10

SPECIALIST

24

GENERIC' LETTER 83-28 EQUIPMENT

06/16/86 06/20/86

CLASSIFICATION, VENDOR INTERFACE, POST

MAINTENANCE TESTING, PLANT SURVEILLANCE

AND QA/QC OVERVIEW

'

86-11

86-11

RESIDENT

261

ROUTINE RESIDENT' INSPECTION

07/01/86'08/31/86

<

'

86-12

86-12

SPECIALIST

40

WRITTEN AND OPERATING EXAMINATIONS

08/11/86 08/15/86

ADMINISTERED TO SIX REACTOR OPERATOR AND

FOUR SENIOR REACTOR OPERATOR CANDIDATES

86-13

86-13

SPECIALIST

40

EMERGENCY PREPAREDNESS EXERCISE

07/21/86 07/25/86

86-14

86-14

SPECIALIST 260

EMERGENCY PREPARE 0 NESS EXERCISE AND

09/08/86 10/17/86

REMEDIAL DRILL

86-15

86-15

SPECIALIST

24

SURVEILLANCE AND CALIBRATION TESTING

08/18/86 08/22/86

PROGRAM AND CONTROL 0F MEASURING AND

TEST EQUIPMENT

86-16

86-16

RESIDENT

206

ROUTINE RESIDENT IMSPECTION

09/01/86 10/17/86

86-17

86-17

SPECIALIST

74

IMPLEMENTATION OF RADIATION

09/15/86 09/19/86

PROTECTION PROGRAM AND OUTAGE

-

PREPARATIONS INCLUDING ALARA EXPOSURE

AND RADI0 ACTIVE MATERIAL CONTROL

'

86-18

86-18

RESIDENT

209

ROUTINE RESIDENT INSPECTION

10/18/86 11/30/86

L

i

f

_ _ _ _ _ _ _ _ .

.

Table 1

T1-2

-

REPORT NUMBERS

TYPE

TOTAL

INSPECTION DATES INSPECTION

HOURS

DESCRIPTION

86-19

86-19

RESIDENT

289

ROUTINE RESIDENT INSPECTION

12/01/86 01/12/87

86-20

86-20

SPECIALIST

94

PLANT OPERATIONS AND SURVEILLANCE

11/03/86 11/07/86

PROGPEMS FOR CONTAINMENT INTEGRITY,

ISOLATION VALVES AND AIR LOCKS,

HYOR0 GEN CONTROL AND OTHER SYSTEMS

86-21

86-21

CANCELLED

86-22

86-22

MEETING

NA

LICENSEE REQUESTED MEETING

86-23

SPECIALIST

24

REV!EW 0F THE ISI PROGRAM, OBSERVATIONS

11/17/86 11/21/86

0F ULTRASONIC AND EDDY CURRENT

EXAMINATIONS AND REVIEW OF NDE PROCEDURES

86-24

86-23

SPECIALIST

30

MAINTENANCE PROCEDURES, ELECTRICAL,

11/17/86 11/21/86

MECHANICAL AND INSTRUMENTATION

MAINTENANCE AND MODIFICATION TASKS AND

QA/QC CONTROL INTERFACES

86-25

SPECIALIST 32

RADIOLOGICAL SAFETY INSPECTION -

12/01/86 12/05/86

IMPLEMENTATION OF RADIOLOGICAL CONTROLS

DURING UNIT 1 OUTAGE

-

87-01

87-01

RESIDENT

196

ROUTINE RESIDENT INSPECTION

01/12/87 02/28/87

87-02

87-02

SPECIALIST 32

FOLLOWUP ON SECURITY PROGRAM EVENT

02/17/87 02/20/87

REPORTS AND A PREVIOUSLY IDENTIFIED

VIOLATION, MANAGEMENT EFFECTIVENESS

AND INDEPENDENT INSPECTION

87-03

87-03

SPECIALIST 84

PASS SAMPLING OF REACTOR COOLANT &

02/24/87 02/27/87

CONTAINMENT ATMOSPHERE, N0BLE GAS

EFFLUENT MONITORS, EFFLUENT MONITORING,

i

IN PLANT RADIO-IODINE MEASURES

87-04

87-04

SPECIALIST 32

NON-LICENSED STAFF TRAINING

02/23/87 02/27/87

i

_ - _ _ _ _ --__ - _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.-_____ _____- __ ____-__ - ____

.

1

Table 1

T1-3

'

REPORT NUMBERS

TYPE

TOTAL

INSPECTION DATES

INSPECTION HOURS

DESCRIPTION

!

- 87-05

87-05

SPECIALIST' 40

WRITTEN AND OPERATING RETAKE

04/20/87 04/24/87

EXAMINATION ADMINISTERED TO ONE

REACTOR OPERATOR AND RETAKE OPERATING

EXAMINATION TO ONE OTHER R0 CANDIDATE-

l

87-06

87-06

RESIDENT

202

ROUTINE RESIDENT INSPECTION

03/01/87 04/13/87

87-07

SPECIALIST 40

UNANNOUNCED OCCUPATIONAL RADIATION

03/23/87 03/27/87

PROTECTION INSPECTION AT UNIT 2

DURING UNIT OUTAGE

87-07.

87-U8

SPECIALIST 40

UNANNOUNCED INSPECTION OF LICENSEE

03/23/87 03/27/87

ACTIVITY IN RESPONSE TO INFORMATION NOTICE 86-03 AND INFORMATION NOTICE 86-53

87-08

87-09

SPECIALIST 40

UNANNOUNCED INSPECTION OF THE LIQUID AND

03/01/87 04/03/87

GASEOUS RADI0 ACTIVE EFFLUENTS CONTROL

<

PROGRAM REPORT

87-09

RESIDENT

24

SPECIAL INSPECTION TO ASCERTAIN

03/26/87 03/30/87

CIRCUMSTANCES INVOLVING ISOLATION OF ALL

RECIRCULATION ACTUATION SYSTEM LEVEL

-

SWITCHES - LER 317/87-05

87-10

SPECIALIST 40

INSPECTION OF IN SERVICE INSPECTION

04/06/87 04/10/87

PROGRAM AND STEAM GENERATOR INTEGRITY

'

87-10

87-11

RESIDENT

187

ROUTINE RESIDENT INSPECTION INCLUDING

04/14/87 05/18/87

DEFICIENCIES IN EQ PROGRAM, REPETITIVE

BRANCH LINE CRACKING AND CQ REPLACEMENT

PARTS

87-11

87-12

SPECIALIST 40

INSPECTION OF NUCLEAR MATERIAL CONTROL

j

04/28/87 05/01/87

AND ACCOUNTING

I

87-12

87-13

SPECIALIST 40

MECHANICAL, ELECTRICAL, AND I&C

04/27/87 05/01/87

MAINTENANCE INCLUDING PROCEDURES,

'

MODIFICATIONS, EQUIPMENT HISTORIES,

TRANSFORMER REVIEWS & QA INTERFACE

j

i

i

)

i

,

l

-

- _ _

_ _______-

.

'

Table 1

T1-4

.

REPORT NUMBERS

TYPE

TOTAL

t )i

'

INSPECTION DATES

INSPECTION HOURS

DESCFfPTION

'

87-13

87-14

SPECIALIST 308

SPECIAL INSPECTION REVIEWING EQ

05/11/87 05/15/87

DEFICIENCIES, COMMERCIAL QUALITY

MECHANICAL FASTENERS, PM TESTING,

ENGINEERING REQUIREMENTS AND QA

s

87-15

SPECIALIST 40

INSPECTION OF IN SERVICE INSPECTION

'

1

05/11/87 05/15/87

REVIEW 0F ISI DATA AND QA COVERAGE,

7

REPAIR ACTIVITIES ON 2-RV-439, EROSIOM/

'

CORROSION EXAMITATIONS

87-14

87-16

RESIDENT

312

ROUTINE RESIDENT INSPECTION

,

,

05/IS/87 06/30/87

'

87-15

87-17

SPECIALIST 39

SOLID RADI0 ACTIVE WASTE PROCESSING,

I

07/13/87 07/17/87

PREPARATION, PACKAGING AND SHIPPING

PROGRAM

87-17

87-19

RESIDENT

276

ROUTINE RESIDENT INSPECTION

07/01/87 07/31/87

,

87-16

87-18

SPECIALIST

32

RADIOLOGICAL ENVIP0HMENTAL MONITORING

07/13/87 07/17/87

PROGRAM

87-18

87-20

SPECIALIST

8

SENIOR N3HAS_ MENT MEETING HELD AT NRC

07/13/87 07/13/87

HEADQUARTERS

87-20

87-22

SPECIALIST

32

INTERNATIONAL ATOMIC ENERGY AGENCY

08/17/87 08/21/87

VISITATION

87-22

87-24

RESIDENT

80

ROUTINE RESIDENT INSPECTION

08/01/87 08/31/87

87-19

87-21

SPECIALIST

CANCELLED

87-21

87-23

SPECIALIST

CANCELLED

(

s

!

'

_.

-_-

_.

..

i u)t% .

(

_

'

\\

,' e

(

'\\

\\.4

TABLE 2

s,,

,

(

CALVERT CLIFFS 1&2

'

INSPECTION HOUR SvKMARY

,

,

4

'XREA

HOURS

HOURS ANNUALIZE0

PERCEN!

OPERATIO,NS

1646

1234.5

40.9

'

RAUCON/ CHEMISTRY

465

348.7

11.6

'

,, . ,

MAh5?ANCE

559

419.3

13.9

y

SURVEILLANCE

332

249 0

8.2

.s

EMERGENCY PREP.

308

231.0

7.7

o

SEC/ SAFEGUARDS

88

66.0

2.2

,

OUTAGES

271

203.3

6.7

,

ENGINEERING

275

206.2

6.8

LICENSING

/

74

55.5

1.9

s

AS'50RAN'CE OF QUALITY

0

0.0

0.0

9 /

I

1 RAINING / QUALIFICATION

0

0.01

0.0

l

!

'

TOTALS:

4018

3013.5

100.0

)

t

i

s

y

N t

,

<

(

v

>

t

'

l

'

.

Ir

E

(

'N

,

I

J,

\\ ,

\\

\\'

s)

r

,

t'

//

s

<

s

,

,

'

\\

'

i/

s

i

f

,

W

%

t

.

. . . ..

-

.

_

._ _

! , 4 4. ,

.

.

'

i,o

TABLE 3

CALVERT CLIFFS 1&2

'

ENFORCEMENT ACTIVI1 6 '

s

A.

Violations versus Functional Area by S'everity Level

No. of Violations in Each Severity Level

AREA

'l

2

3

4

5

DEV

TOTAL

f

OPERATIONS

1

1

,

,

-

>

RADCON/ CHEMISTRY

1

1

3

MAINTENANCE

1

1

?

SURVEILLANCE

-

2

.

2

EMERGENCY 90,EP.

O

SEC/ SAFEGUARD'S

2

2

OUTAGES

0

ENGINEERING SUPPORT

1*

LICENSING

0

ASSURANCE OF QUALITY

0

TRAINING & QUALIFICATION

0

FIRE PROTECTION-HK

0

TOTALS:

T7

l*

  • 0ne or more violations pending in EQ

l

I

.

e

.-

Table 3

T3-2

"~

,B.

Summary of Violations

INSPECTION REPORTS' REQUIREMENT SEVERITY

FUNCTIONAL

' INSPECTION DATES

VIOLATED

LEVEL

AREA

DESCRIPTION

__

__

'86-09-

T . S . . '6 ' 12'.1

-4-

RADCON

FAILURE TO MAINTAIN

.

05/01/86 06/30/86-

CONTROL 0F LOCKED

HIGH RADIATION AREA

KEYS

86-10

T.S.6.8.1

4.

MAINTENANCE

FAILURE TO FOLLOW

06/16/86 06/20/86

PROCEDURES AFFECTING

'

SAFETY-RELATED

ACTIVITIES

86-15

_

10 CFR 50,

4

SURVEILLANCE I&C TECHNICIANS

-08/18/86 08/22/86 APPX. B

USING TEST EQUIPMENT NOT

WITHIN THE. CALIBRATION

DATE AND STORAGE

POTENTI0 METERS OUT

OF CALIBRATION

86-16

SECURITY

4

SEC/SAFEGRDS FAILURE TO FOLLOW

09/01/86 10/17/86 ' PLAN

SECURITY PLAN PROCEDURES

FOR VEHICLE KEY CONTROL

86-20

T.S. 6.8

4

SURVEILLANCE FAILURE ~TO PRuii.5 V-

11/03/86 11/07/86-

REVIEW COMPLETED

SURVEILLANCES AND TAKE

CORRECTIVE ACTION FOR

OUT OF SPECIFICATION

TEST RESULTS

i

!

_

_ _ _ _ _ _ ____ _ -__- - __ _

- ___-_

_

_ _ _ _ _ _ _ _ _ _ _

_

_ _ _ _ _ _ . _ _ _ .

. _ _ _ _ - _ _ _

_ _ __

__

_ _ _ _ _ _ _ _

.

Table 3

T3-3

-

INSPECTION REPORTS REQl'IREMENT SEVERITY

FUNCTIONAL

INSPECTION DATES

VIOLATED

LEVEL

AREA

DESCRIPTION

87-07

87-08

10 CFR 50.49

ENGINEERING

FAILURE TO ESTABLISH

~*

'03/23/87 03/27/87

ADEQUACY OF THE-

MAINTENANCE PROCEDURES

  • Pending

no violation issued yet

FOR MAINTAINING

LIMITORQUE M0V'S

FAILURE TO ESTABLISH

QUALIFICATION OF

ASCO VALVE

LICENSEE FAILED TO

ESTABLISH QUALIFICATION

OF WRAP-AROUND TAPE

SPLICES USED IN PIG-

TAIL LEADS FOR SOLEN 0ID

VALVES

87-09

-

TS 3.3.2.1

4

OPERATIONS

FAILURE TO COMPLY

03/26/87 03/30/87

WITH THE PRECAUTIONS

OF A SURVEILLANCE

TEST PROCEDURE

ISOLATING RAS FUNCTION

,

FOR ECCS & CSS

-

l

l

87-12

87-13 .

10 CFR 50

5

MAINTENANCE

FAILURE TO FOLLOW

'

04/27/87 05/01/87

SAFETY TAGGING

ADMINISTRATIVE

CONTROLS DURING

l

MAINTENANCE ACTIVITY

-87-11

87-12

10 CFR 4

SEC/SAFEGRDS FAILURE ~TO

04/28/87 05/01/87 70.51(D)

MAINTAIN AND KEEP

PHYSICAL INVENTORY

RECORDS TO SUPPORT

THAT INVENTORIES OF

SNM WERE CONDUCTED

BETWEEN 4/30/81

AND 3/30/85

I

i

l

{

l

~

!~

. . - . . . - .

.

.

.

.

TABLE _4

CALVERT CLIFFS 1&2

LICENSEE EVENT REPORTS

A.

LER by Functional Area

Number by Cause Codes

FUNCTIONAL AREA

A

B

C

D

E

X

TOTAL

OPERATIONS

5

3

2

10

RADCON/ CHEMISTRY

-

MAINTENANCE

1

1

1

3

6

SURVEILLANCE

1

1

EMERGENCY PREP.

-

SEC/ SAFEGUARDS

-

OUTAGES

-

i

ENGINEERING SUPPORT

8

8

LICENSING

-

ASSURANCE OF QUALI TY

-

TRAINING AND

QUALIFICATION

-

idTALS:

T i6 l 7

7

7

3

-

-__-__-_____-_;

. . .

[

'

Table 4

T4-2

-

8.

LER Synopsis

CALVERT CLIFFS 1

LER NUMBER EVENT DATE CAUSE CODE

DESCRIPTION-

86-03

04/30/86

A

BATTERY WATER LEVEL EXCEEDED HIGH LEVEL

'

LIMIT

86-04

07/20/86

B

REACTOR TRIP CAUSED BY REACTOR COOLANT

PUMP SURGE CAPACIl0R

86-05

10/01/86-

0

MAIN VENT WIDE RANGE NOBLE GAS EFFLUENT

MONITOR IN0PERABLE DOE TO DEFICIENT

S

PROCEDURE

86-06

10/10/86

A

REACTOR TRIP DUE TO TURBINE TRIP FROM

LOSS OF CONDENSER VACUUM

86-07

10/11/86

0

REACTOR TRIP CAUSED BY HIGH' AXIAL SHAPE

INDEX

87-01

12/10/86

0

VIOLATION OF TECHNICAL SPECIFICATION

FOR OPERABLE SHUTDOWN COOLING LOOPS

87-02

12/03/86

B

MAIN-STEAM PIPING FLAW

87-03

01/27/87

A

REACTOR TRIP AS A RESULT OF LOSS OF

INSTRUMENT' AIR

87-04

02/01/87

0

REACTOR TRIP AS A RESULT OF TURBINE RUN

BACK

87-05

02/17/87

A

INADVERTENT ISOLATION OF ALL

RECIRCULATION ACTUATION SYSTEM LEVEL

SWITCHES

87-06

03/10/87

X

PRESSURIZER SAFETY VALVES 200 AND

201 SET POINTS OUT OF SPECIFICATIONS

87-07

04/01/87

B

ENVIRONMENTAL QUALIFICATION

DISCREPANCIES REQUIRING SHUT DOWN

87-08

04/14/87

A

IMPROPER VALVE LINEUP RESULTING IN

SPRAYING B0 RATED WATER IN CONTAINMENT

BUILDING

i

__

_

-

- - - - _ - - _ _ _ - - - - - - - _ - _

--_--------------a

._

_

._.

._

. _ ,

.

_

--

-

,

Table 4

T4-3

-

LER NUM3ER EVENT-DATE CAUSE CODE

DESCRIPTION

87-09-

04/23/87

8

USE OF FASTENERS (BOLTS, STUDS, THREADEO

R00 & NUTS) IN ASME CLASS 1, .2, & 3,

,

SYSTEMS WITHOUT PROPER CERTIFICATION,

SPECIAL NDE OR MARKING

.87-10

05/22/87

B

PRESSURIZER SPRAY VALVE BONNET WELD

DESIGN DEFICIENCY

87-11

07/14/87-

A

LOSS OF FEED WATER HEATER AND

OVERB0 RATION EVENT WITH REACTOR TRIP

87-12

07/23/87

X

FAULTY 500KV CIRCUIT BREAKER OPERATION

LEADS TO LOSS OF NON-EMERGENCY - AC POWER

CALVERT CLIFFS 2-

86-04

05/21/86

E

MANUAL AND AUTOMATIC TRIPS ON LOW-

STEAM GENERATOR WATER LEVEL

86-05

07/25/86

B

FLEX HOSE FITTING FAILURE ON 21A RCP

REQUIRED UNIT SHUTDOWN AND UNUSUAL

EVENT

86-06

09/05/86

B

REACTOR TRIP CAUSED BY REACTOR COOLANT

PUMP SURGE CAPACITOR FAILURE

-

86-07

09/12/86

B

MANUAL REACTOR TRIP DUE TO PARTIAL LOSS

OF FEED WATER FLOW TO STEAM GENERATORS

87-01

CANCELLED

I

87-02

02/28/87

E

FAILURE OF LEAD / LAG CIRCUIT IN

FEED WATER REGULATING VALVE CONTROL

SYSTEM LEADS TO LOW STEAM GENERATOR

WATER LEVEL REACTOR TRIP

87-03

03/24/87

B

FAILURE OF INLET PIPING TO RELIEF

'

l

VALVE (2-RV-439)

87-04

05/07/87

B

FAILURE OF INLET PIPING TO RELIEF

VALVE (2-RV-439)

87-05

07/03/87

E

FOLLOWING THE CALIBRATION OF THE

TURBINE GENERATOR CONTROLLER, EXCESS

LOAD RESULTS IN A LOW STEAM

GENERATOR PRESSURE REACTOR TRIP

l~

l

l

e

Table 4

T4-4

C.

Licensee Event Reports (LERs)

Tabular Listing

Type of Events

Unit 1

Unit 2

A.

Personnel Error. . . . . .

..6

......0

B.

Design / Man.Constr./Tnstall . . .

5

......5

C.

External Cause . . . . . . . . . 0

......0

D.

Defective Procedure

......4

......0

E.

Component Failure

....0

......3

..

X.

Other

.............2

....0

Total

. .

17

......5

Licensee Event Reports Reviewed:

Unit 1 LER 86-03 through 87-12; Unit 2 LER 86-04 through 87-05.

. .

._-

.

. .- .

_

, _ . _ _

_

.,

~ .

. _ -

_

. . _ , _ _ - .

,

.-

.

TABLE 5

'

'

SUMMARY'0F LICENSING ACTIVITIES

A.

NRR LICENSEE MEETINGS

q

September 19,.1986

Request for Emergency TS Amendment for #12 EDG

September 26, 1986

24-month Cycle Reload

' October 3, 1986

C0 in-leakage into #12 EDG Jacket Cooling Water

' System

!

December 10, 1986

Unit 1 Main- Steam Line Flaw '

January 7,1987 -

Future Licensirg Actions

g q.

May 5, 1987

Materials Qualification Deficiencies

'

B.

NRR SITE VISITS

'

July 14, 1986

Site familiarization and training for new ORPM

July 18, 1986

SALP Meeting

August 1, 1986

Discuss licensing actions status

August 7, 1986

Investigate #12 EDG C0 in leakage

>

i

October 2, 1986

Follow up information on #12 EDG

November 3-7, 1986

Containment Ir tegrity Inspection

j.

April 1, 1987

ATWS Modification Review

May 11-15, 1987

Restart Inspection (joint Region I/NRR team)

June 10, 1987

SG Tube ISI Amendment Request

L

L

August 10-28, 1987

OSART

l

C.

COMMISSION BRIEFINGS

None.

[

!

1

!

l

l

.-

. . .

.-- .

- - . - - .

- . - . . -

. . - . .

. . .

. - .

. - - - . . - - - . - .

.

- _ _ _ - _ _ _ _ _ _ _

.

Table 5

T5-2

-

D.

SCHEDULAR EXTENSIONS GRANTED

September 30, 1986

Order for operable SPDS, Units 1 and 2

E.

RELIEFS GRANTED

March 26, 1987

ASME Section XI Relief - Unit 1 Main Steam Line

Flaw

May 11, 1987

ASME Section XI Relief - Units and 2 Class 1 and

2 Bolting and Control Rod Drive Housing

May 29, 1987

ASME Section XI Temporary Relief - Unit 2

Auxiliary Feed Water Hydrostatic Test

F.

EXEMPTIONS GRANTED

None

G.

LICENSEE AMENDMENTS ISSUED

Date

Unit 1

Unit 2

Title

June 17, 1986 118

100

Miscellaneous TS Changes

June 30, 1996 119

101

Miscellaneous TS Changes

,

August 6. 1986 120

102

Miscellaneous TS Changes

Sept. 8, 1986 121

103

Exigent DG LC0 Change

Sept. 23, 1986 122

104

Emergency Change #12 OG

Oct. 6, 1986

123

105

DFOST Outace Time

Nov. 28, 1986 124

---

Emergency Change Refuel

without a1 EDG

Dec. 19, 1986

I?5

106

RCP Flywheel Inspection /

,

'

Snubber

~ ble Deletion

a

Feb. 25, 1987

126

---

MSIV Replace Closure

l-

April 29, 1987 ---

107

MSIV Replace Closure

1

June 30, 1987 ---

108

Cycle 8 Reload Request

l

l

i

l

_ _ - _ _ _ _ - _ _ _ _ _

.

Table 5

TS-3

"

July 7, 1987

127

109

CEA Misalignment /

Purge Valve Isolation

H.

ORDERS ISSUED

September 30, 1986

Modification of Order on Emergency Response

Capability Schedules (Generic Letter 82-33)

providing a schedular extension for SPOS

Operability.

.

puso

'o,,

UtJITED STATES

ENCLOSURE 3

, ,.

,

i

NUCLEAR REGULATORY COMMISSION

o

$

,I

REGION l

0,%

g

$31 PANK AVENUE

.,6

(

  • . . . . . ,e

KING OF PRUSSIA, PENNCYLVANIA 194o6

Om n31987

DOCKET / LICENSE:

50-317/DPR-53

50-318/DPR-69

Baltimore Gas and Electric Company

ATTN: Mr. J. A. Tiernan

Vice President, Nuclear Energy

Post Office Box 1475

Baltimore, Maryland 21203

Gentlemen:

Subject:

Systematic Assessment of Licensee Performance (SALP) Report

No. 50-317/86-99; 50-318/86-99

The NRC Region 1 SALP Board has reviewed and evaluated the performance of

activities at the Calvert Cliffs Nuclear Power Plant for the period of

May 1, 1986 through August 31, 1987.

The results of this assessment are

documented in the enclosed SALP Board report.

A meeting to discuss the

assessment has been scheduled for December 14, 1987, at the site in Lusby,

Maryland.

l

At the SALP meeting, you should be prepared to discuss our assessments and your

f

plans to improve performance. In particular, you should be prepared to ciscuss

the areas of management control of the interfaces between the Engineering,

Operations and Maintenance Departments, the need for additional resources in

the engineering and maintenance areas and more effective use of self analysis

techniques to recognize emerging plant problems. The meeting is intended to be

a candid dialogue wherein any comments you may have regarding our report may be

discussed. Additionally, you may provide written comments within 30 days after

the meeting.

Fc11owing our meeting and receipt of your response, the SALP report and ycur

l

retponse will be placed in the NRC Public Document Room.

l

Your cooperation with us is appreciated.

l

1

l

Sincerely,

l

William T. Russell

l

Regional Administrator

l

Enclosure:

SALP Report No. 50-317/86-99; 50-318/86-99

l

k

w-

.

)

.

. .

' -ty

.

____

o

,

DEC 031987

Baltimore Gas and Electric Company

2

,

,

cc w/ enc 1:

.

M. Bowman, General Supervisor, Technical Services Engineering

Thomas dagette, Administrator, Nuclear Evaluations

Public Document Room (POR)

Local Public Document Room (LPOR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of Maryland (2)

Chairman Zech

Commissioner Roberts

Commissioner Bernthal

Commissioner Carr

Commissioner Rogers

(

(

l

..-d

&.

ENCLOSURE 4

.

.

.

'

BALTIMORE

GAS AND

ELECTRIC

CHARLES CENTER * R O. BOX 1475 BALTIMORE, MARYLAND 21203

JosCPH A.TIERNAN

Viet PRestDENT

NuCLEAM ENEROY

January 13, 1988

U. S. Nuclear Regulatory Commission

Washington, DC 20555

ATTENTION:

Document Control Desk

SUBJECT:

Calvert Cliffs Nuclear Power Plant

Unit Nos.1 & 2; Docket Nos. 50-317 & 50-318

Systematic Assessment of Licensee Performance (SALP)

REFERENCE:

(a) Letter from Mr. W. T. Russell (NRC) to Mr. J. A. Tiernan (BG&E),

dated December 3,1987, same subject

Gentlemen:

This is in response to Reference (a) and the SALP conference held on December 14, 1987,

at Calvert Cliffs. We appreciate your assessment and constructive criticism of our

nuclear program. Action plans are underway in many areas to strengthen our Nuclear

Program. Enclosure (1) provides some specific comments regarding those efforts.

I will keep you informed of our initiatives and we welcome your comments and insights

,

l

as we continue to strive for excellence at Calvert Cliffs.

Very truly yours,

j

,

!

l

JAT/SRC/ dim

Enclosure

l

~.

cc:

D. A. Brune, Esquire

,

l

J. E.

Silberg, Esquire

.

l

R. A.Capra,NRC

!

S. A.McNeil,NRC

W. T. Russell, NRC

T. Foley/D. C. Trimble, NRC

l

Mi MOr*3-f m

,

l

l

- -

,

'

ENCLOSURE (1)

o

d

REPLY TO SALP REPORT NO. 50-317/86-99; 50-318/86-99

I

,

PLANT OPERATIONS

.

l

We will continue to focus on and strengthen plant operations. For example, we changed

l

the Plant Operations and Safety Review Committee (POSRC) meeting format and introduced

the

facilitator

concept.

The

facilitator

controls

the

meeting

and

ensures

its

i

formality. We will continue to evaluate the effectiveness of POSRC and make changes as

necessary.

l

Communications between the operations organization and the rest of the plant will be

improved. Our supervisory staff has been receiving training to enhance plant teamwork.

I

In August we initiated a morning meeting for plan-of-the-day activities which the

General Supervisor-Operations chairs. The meeting includes engineering and maintenance

personnel and has improved intra-organizational communication.

CIIEMISTRY AND RADIOLOGICAL CONTROLS

No comments.

MAINTENANCE

Additional human resources in the Mechanical and I&C Maintenance areas are being

'

provided through the addition of contractor forces, loaned , crafts from elsewhere in our

company and temporary additions to the complement. The preventive maintenance program

will be improved.

Although we have initiated a strong program to reduce Control Room deficiencies, we

also are not satisfied w ith the number of out-of-service instruments in the Control

Room and we intend to improve in this area. It should be pointed out that the number

of out-of-service instruments has been cut approximately in half in the last 12 months

through our aggressive efforts.

SURVEILLANCE

Documentation of surveillance results will be improved by more aggressively documenting

and reviewing equipment performance. We will continue and strengthen our proactive

efforts regarding equipment problems.

We do not believe that we rely too stringently on the Technical Specification

definition of ' OPERABLE" since we frequently go beyond what is required by the

Technical Specifications in demonstrating operability.

1

'

'

ENCLOSURE (1)

8

REPLY TO SALP REPORT NO. 50-317/86-99; 50-318/86-99

EMERGENCY PREPAREDNESS

In response to your assessments regarding Emergency Preparedness, we agree that

resources are adequate and reasonably effective so that satisfactory performance is

achieved. Your report accurately reflects the shortcomings experienced in the 1986

annual graded exercise.

However, we believe a definite trend of improving performance is discernible in

Emergency Response. The basis for this includes our own evaluations conducted during

i

'

the February 1987 and June 1987 drills and the SALP Boards' summary statement which

says in part: "The licensee immediately recognized the (1986 exercise) weakness and

performance has improved considerably since . . . ." While the SALP Report does not

elaborate on the results of the IAEA, Operational Safety Review Team (OSART) review, it

is worthy to note that Emergency Response received acclaim in several respects.

SECURITY AND SAFEGUARDS

e

We have no general comments, however, we would like to point out that our engineering

organization is responsible for and conducts the inventory of special nuclear materials

(SNM). The security organization would report unaccounted for shipments, suspected

thefts,

unlawful

diversions,

radiological

sabotage,

or

events

which

significantly

threaten or lessen the effectiveness of safeguards.

i

l

.

REFUELING. OUTAGE MANAGEMENT

l

In

1988, we will focus more attention on improving equipment condition and

availability. We have scheduled an outage on Unit No. 2 specifically to improve the

unit's material condition.

1

ENGINEERING SUPPORT

i

.

l

Your observations on our engineering organization are appropriate. As you said, we are

!

improving. However, we will devote additional resources to the situation and will

l

strengthen prioritization and interdepartmental work relations,

i

With respect to working relationships between Operations, Maintenance, and Engineering,

the TERG (Trip Evaluation and Recovery Group) was implemented last year and established

a teamwork approach to problem solving. We will continue to build on that experience.

We have a first draft of a System Engineer responsibilities and interfaces document.

We are gathering comments and finalizing it.

-2-

_____

. . .

i

l

1

o

.

ENCLOSURE (1)

'

.

REPLY TO SALP REPORT NO. 50-317/86-99; 50-318/86-99

'

We have hired a consultant to develop a customized project management training seminar.

.

A key element in development of that seminar was to reach consensus among Operations,

Maintenance, and Engineering on how we want to perform project management at Calvert

Cliffs.

The

consensus

reaching

sessions

are

completed,

the

results

have

been

s

incorporated into the training syllabus, and the first of several seminar sessions is

i

in progress.

1

d

We have hired a consultant to perform an independent assessment of the Nuclear

Engineering Services Department. Expected completion date is second quarter 1988.

We are in the process of shifting the focus of our System Engineers toward more plant

maintenance engineering, in order to unburden System Engineers, project management of

i

additional modifications will be assigned by System Engineers to the Major Projects

Engineering Unit. We are also increasing our staff and the number of long-term

contractors in the System Engineering area. A third systems unit, Auxiliary Systems

Engineering, is being organized and staffed.

We are increasing our staff and the number of long-term ecntractors in the Design

Engineering area. The Electrical Engineering Unit is being expanded and split into an

Electrical Analysis Engineering Unit and an Electrical Modifications Engineering Unit.

We are increasing our staff in Performance Engineering in the area related to the

Preventive Maintenance Program.

j

The System Engineering Training Program has a high prio'rity. We initiated training in

fall 1987, and we expect to accelerate the scope of that training in 1988 and have the

program fully developed and implemented by 1989.

We

are

also

increasing

the

staff

and

elevating

the

Materials

Analysis

and

Non-Destructive Examination Inservice Inspection Work Group to the status of an

organizational unit.

,

LICENSTHQ

We are increasing our staff in the Licensing & Operational Safety and Fuel Cycle

Management Units. Additionally, we will improve the training and experience of our

licensing staff.

ASSUR ANCE OF OUALITY

Our major emphasis in this area is to improve communications and teamwork.

Programs which emphasize communications and team building have been in progress since

Nuclear Energy Division,

July 1987. The programs have included the Vice President

-

all four Nuclear Energy Division Managers, all Calvert Cliffs General Supervisors, and

during 1988 will include all on-site supervision. It is expected that these pro 8 tams,

-3-

._

_ _ _ _ _ _ _ ___-____ ______ ___________________ -

l

f:

l

'

e

,

ENCLO5URE (1)

s

REPLY TO SALP REPORT NO. 50-317/86-99; 50-318/86-99

i

along with a clarification of responsibilities of various key groups, will have the

desired , effect in assuring the proper functioning and strengthening of interfaces

l

between all on-site groups.

TRAINING AND OUALIFICATION EFFECTIVENESS

<

,

i

Added emphas,s is being placed on developing and implementing additional training

i

programs for both craft and engineering personnel during 1988.

l

.

1

e

_4