text
LICENSEE EVENT REPORT (LER)
Form Rev. 2.0 Patility N_me (1)
Docket Number G)
Page (3)
Quad Cities Unit One 0l5l0l0l0l2l5l4 1 l of l 0 l 4 Title (4)
Tug:t Rock Safety Relief Valves Removed From Unit 2 During Q2R13 and From Unit i During QlR14 Did Not Receive As-Found Set Point Testing Within 12 Months Following Removal As Required By ASME/ ANSI OM-1987 Part i Due To A Defective Procedure Which Did Not Provide Clear Guidance of Test Requirements.
Event Date (5)
LER Number (6)
Report Date (7)
Other Facilities Involved (8)
Month Day Year Year Sequential Revision Month Day Year Facility Docket Numberts)
Number Number Names Quad Cities Unit 2 0l5l0l0l0l2l6l5 0l4 1l6 9l7 9l7 ol1l4 0l0 0l5 1
5 9
7 0l5l0lol0l l
l OPERATING THIS REPORT IS SUBM; a a12D PU GUANT TO T iE REQU REA ENTS OF 10CFR MODE (9)
(Check one or more of the following) (Ili l-Ul 20.402(b) 20.405(c) 50.73(a)C)(iv) 73.71(b) 0- U2 POWER Unit 1 - 100 20.405(a)(1)0) 50.36(c)(1) 50.73(a)G)(v)
- - 73.71(c)
LEVEL Unit 2 - 0
- - 20 405(a)(1)Oi) 50.36(c)C) 50.73(a)C)(vii)
Other (Specify (10) l l
20.405(a)(1)0ii)
T50.73(a)G)0) 50.73(a)G)(vtii)(A) m Abstreet 20.405(a)(1)0v) 50.73(a)G)0i) 50.73(a)G)(viii)(B) below and in
- - 20.405(a)(1)(v) 50.73's)G)0ii) 50.73(a)C)(x)
Text)
~
LICENSEE CONTACI FOR THis LER (12)
N /.M E TELEPHONE NUMBER AREA CODE Chules PJterson, Regulatory Affairs Manager, ext. 3609 3
0l9 6l5l4l-l2l2l4l1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SY5 TEM COMPONINT MANUFACTURER REPORTABLE
CAUSE
SYSTEM CUMPONENT MANUFACTURER REPORTABLE TO NPRDS 1D NPRDS I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I SUP >LEMENTAL REPORT EXPECTED (14)
Erpected Month Day Year Subaussion lYES Of yes. compkse EXPECTED SUBMISSION DATE) 70 Date (15) l l
l ABSTRACT (1.mna to 1400 spaces. s.o., approumsicly fitwen smgk opwe typewrmen Ames) (16)
ABSTRACT:
A Target Rock Safety Relief Valve (TRSRV), that was removed from the 2-0203-3A position during the Q2R13 refueling outage on 060195, had not been set pressure tested within 12 months. Also a TRSRV that was removed from the 1-0203-3A position during the Q1R14 refueling outage on 031596 had not been set pressure tested within 12 months. This is contrary to ASME/ ANSI OM-1987, Part 1, Paragraph 1.3.3.1(c)(2) and Technical Specification (TS) Section 4.0.E.
The root cause of the event is a Defective Procedure, which failed to provide clear instructions for ensuring prompt testing in the Target Rock Removal and Installation Procedure (QCMM 0203-31).
Corrective actions include revising the maintenance procedure responsible for the removal of the TRSRV to ensure they are shipped to the testing facility in a timely manner and making improved use of the Nuclear Tracking System to verify the testing is performed within the required time frame.
The Safety Analysis concluded that despite a small deviation above the TS set point tolerances, there would not have been a violation of reactor safety limits on maximum ASME overpressurization, Anticipated Transient Without Scram overpressurization, Reactor thermal limits (Minimum Critical Power Ratio), or loss Of Coolant Accident fuel limits.
LER254197W14.WPF 9705220493 97C3J5 PDR ADOCK 05000254 S
PDR
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev. 2.0 FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3) 0 Year Sequennal Revision Number Number Quad Cities Unit One 0l5l0l0l0l2l5l4 9l7 0l1l4 0l0 2 lOFl 0 l 4 TEXT Energy industry idennfica6on System (EBS) codes are idenufied in the text as (XXj
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power.
EVENT IDENTIFICATION:
Target Rock Safety Relief Valves removed from Unit 2 during Q2R13 and from Unit I during QlR14 did not receive as-found set point testing within 12 months following removal as required by ASME/ ANSI OM-1987 Part I due to a Defective Procedure which failed to provide clear instructions for ensuring prompt testing of Target Rock Safety and Relief Valves.
A.
CONDITIONS PRIOR TO EVENT
Unit:
1 Event Date:
041697 Event Time: 0800 Reactor Mode:
1 Mode Name: Run Power Level: 100%
Power Operation - Mode switch in the RUN position with average reactor coolant temperature at any temperature.
i Unit: 2 Event Date:
041697 Event Time: 0800 Reactor Mode: 0 Mode Name: Refuel Power Level: 00%
None - No Fuel in the Reactor Vessel B.
DESCRIPTION OF EVENT
Technical Specification (TS) 4.0.E.1 states: " Inservice Inspection of ASME Code Class 1,2 and 3 components and Inservice Testing (IST) of ASME Code Class 1,2 and 3 pumps and valves shall be performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code and applicable Addenda as required by 10CFR Part 50, Sections 50.55a(g) and 50.55a(f), respectively, except where specific written relief has been granted by the Commission pursuant to 10 CFR Part 50, Section 50.55a(g)(6)(i) or 50.55a(f)(6)(1),
respectively."
The applicable testing Code for Safety / Relief Valves for Quad Cities Station is ASME/ ANSI OM-1987 Part 1.
Paragraph 1.3.3.1(c)(2) of this Code states: "0wners that satisfy testing requirements by installing a full complement of pretested valves in place of valves that had been in service shall set pressure test the valves which were removed within 12 months of removal from the system."
Contrary to the above, Target Rock Safety Relief Valve (TRSRV)[JE][RV) (Serial Number 224) that was removed from the 2-0203-3A position and replaced during the Q2R13 refueling outage on 060195 under Work Request (WR) 940100493 was not set pressure tested within 12 months of removal.
In addition, TRSRV (Serial Number 225) that was removed from the 1-0203-3A position and replaced during the QlR14 refueling outage on 031596 under WR 950085020 also was not set pressure tested within 12 months of ree <al.
The two TRSRVs along with the TRSRV (Serial Number 171) removed from Unit 2 during the current Q2R14 refueling outage, were sent to Wyle Laboratories for set point testing.
LER254\\97\\014.w?F
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rcn. '2.0 FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
Year Sequential Revision Number Number Quad Cities Unit one 0l5lol0l0l2l5l4 9l7 0l1l4 0l0 3 lOFl 0 l 4' TEXT Engy Indur.<y idenuficanon system (EllSi codes are idanufied m the text as [XXj TRSRV Serial Number 224 was as-found set point tested on 042497 and was found to have an as-found set point of 1148 pounds per square inch gage (psig). This value was outside of the TS 1% acceptance band (1123.7 psig to 1146.4 psig).
TRSRV Serial Number 225 was as-found set point tested on 042597 and was found have an as-found set point of 1095 psig. This value was outside of the TS 1% acceptance band (1123.7 psig to 1146.4 psig) and the ASME OM-1987, Part 1, 3% acceptance band (1101.0 psig to 1169.1 psig).
No sample expansion was necessary since 100% of the sample group for each Unit (consisting of 1 valve) had been tested.
TRSRV Serial Number 171 was as-found set point tested on 042597 and was found to have an as-found set point of 1134 psig. This value was within the TS t 1% acceptance band of 1123.7 psig to 1146.4 psig.
The root cause investigation and safety analysis of the set point failures for TRSRVs serial numbers 224 and 225 are being evaluated separately under Problem Identification Forms (PIFs) 97-2204 and 97-2205.
C.
CAUSE OF THE EVENT
The root cause of the event is due to defective procedures which failed in providing clear instructions for ensuring prompt testing in the Target Rock Removal and Installation Procedure (QCMM 0203-31).
,,ithough there is a provision in the Station's Electronic Work Control System (EWCS) that ensures that the TRSRV is replaced once every refueling outage, a formal trigger and tracking mechanism was not in place to ensure set point testing is performed within the required time frame.
The investigation also revealed that similar trigger and tracking mechanisms were also not included in QCMM 0203-01, " Main Steam Safety Valve Removal and Installation" or in QCMM 0203-04, " Main Steam Valve Testing".
The Main Steam Safety Valves (MSSV), however, were tested within the required time frame (prior to startup) for these valves during the Q2R13, QlR14, and current Q2R14 outages. The Inservice Testing (IST) Coordinator ensured that these valves were tested prior to startup; however the IST Coordinator did not have any provisions made to ensure the tests would have been performed in his absence.
D.
SAFETY ANALYSIS OF EVENT:
The Safety Analysis concluded that despite a small deviation above the TS set point tolerances, there would not have been a violation of reactor safety limits on maximum ASME overpressurization, Anticipated Transient Without Scram (ATWS) overpressurization, reactor thermal limits (Minimum Critical Power Ratio), and Loss Of Coolant Accident fuel limits. Also any as-found set-points below the TS set point tolerances would provide a net benefit to protect the reactor vessel and fuel if analyzed for the ASME and ATWS overpressurization limits.
LER254T97\\014.WPF
-- -_ -~
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev. 2.0 FACILrrY NAME (I)
DOCKET NUMBER (2)
LER NUMBER (6)
PAOE (3)
Year
- - Sequennal Revision Number Number Quad Cities Unit One 0j5l0l0l0l2l5l4 9l7 0l1l4 0l0 4 lOFl 0 l 4 i
TEXT Energy Industry idennficanon System (EUS) coc es are id,anufied in the text as [XX)
)
I i
i E.
CORRECTIVE ACTIONS
CORRECTIVE ACTIONS COMPLETED:
1.
This event was discussed with applicable department personnel.
2.
An EWCS Predefine was implemented to provide a Work Request each refueling outage to track the TRSRV and MSSV testing.
3 CORRECTIVE ACTIONS TO BE COMPLETED:
i 1.
Procedures which govern removal / installation ar.d inspection / repair of TRSRVs and MSSVs will be revised to include all ASME/ ANSI OM-1987 Part 1 Code requirements.
(NTS # 2541809701401)
F.
PREVIOUS EVENTS:
1.
PIF 96-221 (LEVEL III - PIR 2-96-007)
"U-2 DIESEL GENERATOR FUEL OIL TRANSFER RELIEF VALVE INLET CHECK VALVE (2-5299-3) INTERNALS WERE NEVER REMOVED AND THE i
REQUIRED INSPECTION WAS NOT PERFORMED DUE TO INADEQUATE CHANGE MANAGEMENT."
2.
PIF 96-1346 ' LEVEL III - PIR 2-96-023)
" UNIT 2 RX RECIRC SAMPLE (2-0220-45) VALVE IS AN LLRT REQUIRED VALVE, THE AS-FOUND LLRT WAS NOT PERFORMED PRIOR TO UNPACKING VALVE PER QCTP 130-1 ATT. D, REF NWR 960030616-01 DUE TO AN INADEQUATE PROCEDURE.
3.
PIF 96-2325 (LEVEL III - PIR 1-96-167)
"RHR MOV l-1001-47 AND 50 WERE NOT SEAT LEAKAGE TESTED AS REQUIRED PER THE 0Ha-1988 PART 10 DUE TO INADEQUATE CHANGE MANAGEMENT."
4.
PIF 96-2866 (LEVEL III - PIR 2-96-051)
"SB0 DG REMOTE / LOCAL /PLC BYPASS EMERGENCY START TEST HAS NOT BEEN PERFORMED FOR UNIT 2 DUE TO INADEQUATE MANAGERIAL METHODS."
5.
PIF 96-3057 - (LEVEL III - TREND PIR l-96-021)
"12 PIFS HAVE BEEN WRITTEN IN 1996 FOR MISSED SURVEILLANCES/ INSPECTIONS DUE TO INADEQUATE CHANGE MANAGEMENT."
6.
PIF 97-1811 - (LEVEL III - PIR 1-97-032)
"EWCS SURVEILLANCE SCHEDULING PROBLEMS DUE TO THE INTERFACE BETWEEN THE EWCS AND P2 COMPUTERS BEING INADEQUATE."
G.
COMPONENT FAILURE DATA
No Component Failures occurred that resulted in this report.
LER234T9"A014.WPF
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000254/LER-1997-001, :on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed |
- on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed
| 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-001-01, :on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personne |
- on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personnel
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000265/LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-001-07, :on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine |
- on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-002-02, :on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124 |
- on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124
| | | 05000254/LER-1997-002, Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000265/LER-1997-002-05, :on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897 |
- on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897
| | | 05000265/LER-1997-002-01, :on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass |
- on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass
| | | 05000265/LER-1997-002, Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000254/LER-1997-003, Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000265/LER-1997-003-04, :on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten |
- on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-003-05, :on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve |
- on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve
| | | 05000265/LER-1997-003-01, Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-004, Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | 10 CFR 50.73(a)(2) | | 05000265/LER-1997-004-06, :on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed |
- on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-004-03, :on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced |
- on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-005-03, :on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated |
- on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-005, Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000265/LER-1997-005-01, Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-005-02, :on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts |
- on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000265/LER-1997-006, Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000265/LER-1997-006-01, :on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1 |
- on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1
| | | 05000254/LER-1997-006-03, :on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker |
- on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker
| | | 05000254/LER-1997-006, Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-006-06, :on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed |
- on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed
| | | 05000254/LER-1997-007-03, :on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan |
- on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-008, Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-008-01, :on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged |
- on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-008, Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-008-05, :on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable |
- on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-009, Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-009-03, :on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled |
- on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled
| | | 05000265/LER-1997-009-05, :on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas |
- on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(s)(2)(v) | | 05000254/LER-1997-010-02, :on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily |
- on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily
| | | 05000265/LER-1997-010-05, :on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled |
- on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled
| | | 05000265/LER-1997-010, Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-010, Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-011-01, :on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause |
- on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause
| | | 05000254/LER-1997-011, Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-011-05, :on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals |
- on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000265/LER-1997-012-06, :on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted |
- on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted
| | | 05000254/LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000254/LER-1997-013-01, :on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch |
- on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch
| | | 05000254/LER-1997-014, Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-014-01, :on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure |
- on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure
| | | 05000265/LER-1997-015-05, :on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time |
- on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time
| | | 05000254/LER-1997-015, Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | | | 05000254/LER-1997-015-02, :on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test |
- on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test
| | | 05000254/LER-1997-016-01, :on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1 |
- on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1
| | | 05000254/LER-1997-016, Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | 10 CFR 50.73(a)(2)(1) |
|