ML20134E378

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Insp Rept 50-333/96-08 on 961117-970104.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20134E378
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 01/30/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20134E364 List:
References
50-333-96-08, 50-333-96-8, NUDOCS 9702060188
Download: ML20134E378 (25)


See also: IR 05000333/1996008

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U.S. NUCLEAR REGULATORY COMMISSION

Region I

License No.: DPR-59

Report No.:

96-08

Docket No.:

50-333

Licensee:

New York Power Authority

Post Office Box 41

Scriba, New York 13093

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Facility Name:

James A. FitzPatrick Nuclear Power Plant

Dates:

November 17,1996 through January 4,1997

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inspectors:

G. Hunegs, Senior Resident inspector

R. Fernandes, Resident inspector

R. Skokowski, Resident inspector

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D. Dempsey, Reactor Engineer

Approved by:

Curtic J. Cowgill Ill, Chief

Projects Branch 2

Division of Reactor Projects

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EXECUTIVE SUMMARY

James A. FitzPatrick Nuclear Power Plant

NRC Inspection Report 50-333/96-08

Ooerations

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The reactor startup following the refueling outage was performed in a safe and

prudent manner. The post refueling outage startup training was well presented and

comprehensive,

Operators demonstrated conservative decision making by directing a manual scram

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to be inserted when an electro-hydraulic control (EHC) system leak was identified on

a turbine bypass valve. In addition, operators demonstrated excellent control of the

plant transient.

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Auxiliary operators performed watchstanding duties in an acceptable mmer. Good

radiological control practices were observed and operators demonstrated

attentiveness by identifying and documenting rninor equipment deficiencies. Minor

logkeeping discrepancies as well as some equipment storage discrepancies were

noted and were addressed by operations management.

o

An unresolved item (URI 50-333/95021-01) involving extended operation of all four

residual heat removal system pumps in the suppression pool cooling mode was

closed. Failure to perform a safety evaluation prior to performing this evolution

resulted in a violation of 10 CFR 50.59. (VIO 50-333/96008-01)

Maintenance

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The approach to maintenance activities on the bypass valves was not rigorous and

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contributed to bypass valve hydraulic actuator seal failures and in one case resulted

in a manual reactor scram to be required. The licensee's equipment failure

evaluation was thorough and corrective actions well developed to address

maintenance practices for the bypass valves.

Personnel error by technicians during surveillance testing on reactor water level

instrumentation resulted in automatic reactor protection and primary containment

isolation actuation. Since the plant was shutdown at the time of the event, there

was no effect on plant operation. The inspector noted that this event contained

similarities with the September 16,1996, scram described in NRC inspection report

50-333/96-06 in that technicians proceeded with work without fully recognizing the

potential to cause a plant transient. The condition [a valve packing leakl was not

reported to supervision; thus the decision to proceed with the packing adjustment

was not challenged.

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Configuration control for reinstallation of tubing for the HPCI governor hydraulic

control system was lost during maintenance when tags used to label components

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Executive Summary (cont'd)

became illegible. Although efforts were made to regain configuration control for the

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tubing, the licensee failed to ensure that installation was proper. The problem was

identified during HPCI post work testing.

Enaineerina

Primary containment leakage rate testing was well conducted by the

operations staff. The program was properly implemented and the as-left

testing data met the requireinents for plant start-up following the refueling

outage.

The equipment failure evaluation for the local leak rate testing (LLRT) failures

was comprehensive with appropriate corrective actions completed or planned

for completion. The licensee's decision to replace several poor performing

valves was warranted based on the testing history. The LLRT results over

the past several refueling cycles have shown continuous improvement in the

number of as found failures. However, since the as-found totalleakage rate

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based on Type B and C LLRT results was greater than the technical

specification (TS) limits, a violation of NRC requirements occurred. This

violation will not be cited in accordance with Section Vll.B.1 of the NRC

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Enforcement Manual as the violation was non-recurring, promptly corrected

and of low safety significance (50-333/96008-02).

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Plant Suocort

There were several radiological control barriers and radiation worker practices which

were not adhered to by two workers which resulted in one worker becoming

contaminated. These requirements which were not met included the failure to

obtain a radiation control brief, not adhering to the radiation work permit, wearing

inadequate anti-contamination clothing, disregarding radiological posting

requirements and improper use of the portal monitor. The results were that an

individual became contaminated and the potential existed for the spread of

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contamination. The issue is unresolved item (URI 50-333/96008-03).

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TABLE OF CONTENTS

E X EC UTIV E S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TA B LE O F C O NT E NT S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

Sum m a ry of Plant Statu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. O p e ra ti o n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Cond uct of Operation s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 R e a cto r St a rt u p . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.2 Manual Reactor Scram . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

O2

Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 2

O2.1 Engineered Safety Feature System Walkdowns

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Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 3

04.1 Observations of Auxiliary Operator Watchstanding . . . . . . . . . . . 3

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Operator Training and Qualification . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

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05.1 Post refueling outage (RFO) startup training . . . . . . . . . . . . . . . . 4

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Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

08.1 (Closed) LER 5 0-3 3 3 /9 6007 . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

08.2 (Closed) Unresolved item 50-333/95021-01

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11. M a i nt e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M1

Conduct of Maintenance

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M 1.1 General Comments

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M1.2 General Comments on Surveillance Activities . . . . . . . . . . . . . . . 6

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M1.3 Conclusions on Conduct of Maintenance . . . . . . . . . . . . . . . . . . 6

M2

Maintenance and Material Condition of Facilities and Equipment

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M2.1 Turbine Bypass Valve Actuator Seal Leak

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Maintenance Staff Knowledge and Performance . . . . . . . . . .

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M4.1 Reactor Protection System Actuation Error Caused By

Personnel Error

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M4.2 High Pressure Coolant injection incorrect Tubing Installation . . . . 8

111. Engineering

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Conduct of Engineering

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E1.1

Primary Containment Leakage Rate Testing Program . . . . . . . . . . 9

E1.2 (Closed) LER 96-012, Primary Containment Leakage Exceeding

Technical Specifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

IV. Plant Support . . . . . . . . . . . . . . . .

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Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 12

R1.1

Personnel Contam' nation Identified at the Security Building

Radiation Monitor

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Table of Contents (cont'd)

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V. Ma nagement Meeting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

X1

Exit Meeting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

X2

Review of UFS AR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

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ATTACHMENT

Attachment 1 - TlA Regarding Design Basis Functionality of FitzPatrick RHR System When

Operated in the Suppression Pool Cooling Mode (TAC No. M94319)

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Report Details

Summarv of Plant Status

The unit began this inspection period in cold shutdown with the refueling outage in

progress. The control rod drive change out was completed on November 19 the core was

reloaded on November 27 and reactor vessel pressure testing was completed on December

3. On December 6, the licensee implemented technical specification amendment No. 239.

This amendment increased the steady state reactor core power levellimit from 2436 to

2536 megawatts (thermal). The licensee had to complete several actions as conditions for

the approval of this power uprate license amendment. These actions included monitoring

the recirculation pump motor vibrations during initial power ascension, performance of a

startup test program and incorporation of any potential effects of operation at an increased

power level into operator training.

On December 7, at 10:28 p.m., a reactor startup was commenced and the reactor was

critical on December 8 at 12:36 a.m. On December 15, operators identified an electro-

hydraulic control (EHC) system leak from the turbine bypass valve (BPV) actuator seal and

manually scrammed the reactor from 36% reactor power. Following repairs to the BPV,

the reactor was restarted and was critical on December 18. At the end of the inspection

period, the reactor was at 96% power and power uprate testing was in progress.

l. Operations

01

Conduct of Operations'

01.1 Reactor Startuo

a.

Inspection Scope

The inspectors observed portions of the reactor startup conducted on December 7,

1996, inspector attention was focused on reactivity control, operator procedure

use and communications.

b.

Observations and Findings

The startup was characterized by clear operator communications and procedure use,

attentive management oversight, and effective control by shift supervision. Shift

turnover meetings were performed in a controlled manner and crew briefings were

good. Senior operations management personnel were designated to provide

continuous oversight. Training was conducted for operations personnel to cover

operating parameter changes which had been made as a result of the power uprate.

' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized

reactor inspection report outline. Individual reports are not expected to address all outline

topics.

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c.

Conclusions

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The reactor startup following the refueling outage was performed in a safe and

prudent manner.

01.2 Manual Reactor Scram

a.

Inspection Scoce

On December 15, at 1:00 a.m., operators inserted a manual reactor scram following

the identification of an electro-hydraulic control (EHC) fluid leak from the number

four turbine bypass valve. The inspectors reviewed the post transient evaluation

including logs and operator actions. The plant operating review committee (PORC)

which was conducted to review the event was also observed. In addition, the

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inspectors verified that the action commitment tracking system (ACTS) items which

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were generated from the event were appropriately addressed.

b.

Observations and Findinas

On December 15, an operator was performing turbine building rounds and identified

one to two gallon per minute (GPM) electro-hydraulic control (EHC) system leak

from the turbine bypass valve (BPV) actuator seal. Based on the system engineer's

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recommendation and the potential for the leak to increase substantially and possibly

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lose EHC pressure control, shift management determined that insertion of a manual scram was a prudent course of action. Control room operators were briefed and

stationed at a.5 signed panels and a manual scram was inserted from 36% reactor

power. All required actions occurred and plant response to the transient was

normal. Operators stabilized reactor pressure and level and commenced a normal

reactor cooldown. The EHC leak was stopped by securing the operating EHC pump.

c.

Conclusions

Operators demonstrated conservative decision making by directing a manual scram

to be inserted when an EHC leak was ideritified, in addition, operators

demonstrated excellent control of the plant transient.

O2

Operational Status of Facilities and Equipment

O2.1 Enaineered Safetv Feature System Walkdowns

The inspectors performed a walk down of accessible portions of the following

systems and performed general area tours:

oresidual heat removal service water system

semergency diesel generator

oprimary containment

salternate decay heat removal system

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Equipment operability and material condition were good. Housekeeping conditions

were acceptable. Some outage related equipment was not stored prior to plant

operation. For example, some small tools and tubing were found unattended and

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severalladders in both the reactor and turbine buildings were not secured. The

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licensee addressed these issues.

04

Operator Knowledge and Performance

04.1 Observations of Auxiliary Operator Watchstandina

a.

Scope

The inspectors observed auxiliary operators (AOs) during reactor and turbine

building watchstanding. The inspectors assessed the performance of the AOs, and

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the material and housekeeping conditions of the plant. Additionally, the inspectors

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reviewed applicable site procedures, and held discussions with operations

department personnel, including AOs, shift managers, and the operations

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department manager.

b.

Observations and Findinas

The inspectors observed AOs on the December 11,1996, day shift rounds of the

reactor building, and the December 12 day shift rounds of the turbine building. The

rounds were completed in accordance with Operations Department Standing Order

(ODSO) 17, " Auxiliary Operator Plant Tours and Operating Logs," Revision 59. The

AOs demonstrated good radiological controls practices in the performance of their

duties. The inspector identified some minor logkeeping discrepancies which were

appropriately addressed by operations management. The inspector noted that AOs

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identified some minor equipment deficiencies and appropriately documented the

deficiencies using the Problem Identification (PID) process. The operators wiped up

small amounts of oil under several components including the condensate booster

pumps, the rer.ctor recirculation system (RCS) pump motor generator (MG) sets and

the hydrogen seal oil pumps.

c.

Conclusions

The AOs performed watchstanding duties in an acceptable manner. Good

radiological control practices were observed and operators demonstrated

attentiveness by identifying and documenting minor equipment deficiencies. Minor

logkeeping discrepancies were noted and were addressed by operations

management.

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Operator Training and Qualification

05.1 Post refuelina outaae (RFO) startuo trainina

a. Inspection Scope

Post refueling outage (RFO) startup training was conducted 'o cover the power

uprate technical specification amendment. The inspector observed portions of

power uprate training and discussed the content of training with the Operations

manager.

b. Observations and Findinas

Training included power uprate training, operating experience, changes in plant

system parameters, operations management expectations and an overview of

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special uprate test procedures including sequence of testing. The inspector noted

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good participation from operators that were attending the training.

c. Conclusions

The post refueling outage startup training was well presented and comprehensive.

08

Miscellaneous Operations issues

08.1 (Closed) LER 50-333/96007 Engineered Safety Feature Activation Due to False

High Radiation isolation Signal. On May 22,1996, the reactor building ventilation

exhaust radiation monitor spiked. Automatic actions including reactor building

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ventilation system isolation, standby gas treatment system initiation, and closure of

primary containment atmosphere sample system isolation valves occurred as

required. The redundant ventilation radiation monitor showed no change in radiation

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levels.

Subsequent trouble; Joting determined that the Geiger-Muller type radiation

detector had failed

nich generated the signal spike. The detector was replaced

and the system re

ned to operation.

Operator response to the ESF actuation was appropriate.

08.2 (Closed) Unresolved item 50-333/95021-01: Operation of all residual heat removal

(RHR) pumps in the suppression pool cooling mode for extended periods of time.

On November 7,1995, the licensee operated all four RHR pumps for ten hours in

the suppression pool cooling mode. The operation wm conducted in response to

NRC Bulletin 95-02, " Unexpected Clogging of a Resic.ual Heat Removal Pump

Strainer While Operating in Suppression Pool Cooling Mode," using normal operating

procedures. The licensee did not perform a safety evaluation pursuant to 10 CFR 50.59, " Changes, tests, and experiments," prior to performing the evolution.

Subsequently, the licensee determined that a safety evaluation had not been

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required, but, nonetheless, completed a formal evaluation to ensure that no safety

inues had been overlooked.

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Due to the potential for water hammer should a design-basis accident occur while

both RHR trains are aligned for suppression pool cooling, NRC Region I referred the

issue to the NRC Office of Nuclear Reactor Regulation (NRR) for evaluation. In a

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memorandum dated October 30,1996 (attached to this report), the NRC concluded

that infrequent operation of both RHR trains in the suppression pool cooling mode,

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such as on November 7,1995, was not an unreviewed safety question. However,

frequent, long-term operation of the RHR system either in the suppression pool

cooling or test modes would constitute an unreviewed safety question (per 10 CFR 50.59) due to the increased likelihood of a malfunction due to a water hammer

event. The inspector concluded that the licensee's failure to perform a safety

evaluation prior to operating both trains of the RHR system in the suppression pool

cooling mode on November 7,1995, was a violation of 10 CFR 50.59. (VIO 50-

333/96008-01)

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11. Maintenance

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M1

Conduct of Maintenance

M1.1 General Comments

a.

Insoection Scope

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The inspectors observed all or portions of the following work activities:

eWR 96-06652-01 Inspect condenser thermowells for cracks and determine the

extent of identified crack

eWR 96-06703-04 Post modification testing of off-gas system check valve for the

steam packing exhauster drip pot drain line

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eWR 95-08324

Perform inspection of scram discharge header isolation valve

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disk in accordance with maintenance procedure

b.

Observations and Findinas

The inspectors found the work performed under these activities to be professional

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and thorough. All work observed was performed with the work package present

and in active use. Technicians were experienced and knowledgeable of their

assigned task. The inspectors frequently observed supervisors and system

engineers monitoring job progress, and quality control personnel were present when

required. - When applicable, appropriate radiation control measures were in place.

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M1.2 General Comments on Surveillance Activities

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a.

Inspection Scoce

The inspectors observed selected surveillance tests to determine whether approved

procedures were in use, details were adequate, test instrumentation was properly

calibrated and used, technical specifications were satisfied, testing was performed

by knowledgeable personnel, and test results satisfied acceptance criteria or were

properly dispositioned.

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The inspectors observed portions of the following surveillance activities:

  • ST 20K

control rod withdrawal checks

  • ST 39Q

drywell inspection

  • ST 4N

high pressure coolant injection (HPCI)

  • ST 24Q

reactor core isolation cooling (RCIC) turbine slow roll and overspeed

test

  • ST 4K

HPCI turbine slow roll and overspeed test

  • TST 55

feedwater level control power uprate startup test

  • TST 56

feedwater level control power uprate startup test

b.

Observations and Findinas

The licensee conducted the above surveillance activities appropriately end in

accordance with procedural and administrative requirements. Good coordination

and communication were observed during performance of the surveillance.

M1.3 Conclusions on Conduct of Maintenance

Overall, maintenance and surveillance activities were well conducted, with good

adherence to both administrative and maintenance procedures.

M2

Maintenance and Material Condition of Facilities and Equipment

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M 2.1 Turbine Bvoass Valve Actuator Seal Leak

a.

Inspection Scope

On December '.'5, the number four turbine bypass valve actuator seal was observed

to be leaking at a rote of one to two gallons per minute. Operators inserted a

manual reactor scram to address the hydraulic oilleak.[see section 01.2] The

inspectors reviewed the equipment failure evaluation, reviewed material history and

discussed the seal failure with the maintenance engineer.

b.

Observations and Findinas

The piston, piston rod and rod seal for the number four turbine bypass valve had

recently been replaced during the refueling outage. The seal package consists of a

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lip seal which is the primary pressure retaining device, a backup seal which

supports the primary seal and a wiper seal which prevents external contamination

from the seal area. It appears that the primary seal was damaged during

installation. The damage to the primary seal provided a leakage path for the high

pressure fluid (approximately 1600 psig) to leak past the seal. This caused

pressurization of the wiper seal which is not designed to retain pressure.

On November 24, the number one bypass valve hydraulic actuator piston seal failed

and approximately 50 gallons of EHC fluid leaked from the system. The EHC

system had been restored to operation following preventive and corrective

maintenance activities. The piston seal had been replaced earlier in the outage.

The licensee performed equipment failure evaluations for the seal failures which

included a review of their maintenance practices. In the case of the number one

seal failure, the piston stem had some coating degradation which caused the seal to

wear during operation. The number one seal had exhibited excessive oscillation

during the plant shutdown for the refueling outage and the licensee elected to

replace the seal but did not inspect the piston stem, in the case of the number four

seal, a small burr on the piston damaged the seal during installation. There is a

starting sleeve to facilitate seal replacement which was not used because the

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licensee was not aware of the availability of the tool.

The licensee developed corrective actions to improve maintenance practices

associated with seal replacement.

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c.

Conclusions

The approach to maintenance activities on the bypass valves was not rigorous and

contributed to bypass valve hydraulic actuator seal failures and, in one case,

resulted in the need to insert a manual reactor scram. The licensee's equipment

failure evaluation was thorough and corrective actions well developed to address

maintenance practices for the bypass valves.

M4

Maintenance Staff Knowledge and Performance

M4.1 Reactor Protection System Actuation Error Caused By Personnel Error

a.

Inspection Scope

The inspector reviewed Licensee Event Report (LER)96-013, Reactor Protection and

Primary Containment isolation System Actuation on False Low Reactor Water Level

Due to Personnel Error, and various procedures associated with the event and

discussed the issue with licensee personnel.

b.

Observations and Findinas

On November 16,1996, an automatic reactor protection and primary containment

isolation system actuation occurred on a f alse low reactor water level signal.

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During surveillance testing of reactor water level instrumentation, technicians noted

and attempted to correct an instrument isolation valve stem packing leak which

caused a pressure transient in the level sensing lines and resulted in the instruments

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sensing a false low reactor water level. Systems which were in service

automatically isolated and there was no negative effect on the plant.

The licensee determined that the technician attempted to tighten the valve stem

packing nut while holding the valve handwheel. When the packing nut was turned,

a reactor scram signal and primary containment isolation signal occurred. It appears

that when the packing nut was turned, the technician slightly opened the isolation

valve which resulted in a pressure decrease in the reactor water level variable leg

sensing lines.

The licensee determined that the event was caused by personnel error. The

procedure, IMP-G17, " Whitey Valve Packing Adjustments", which had been

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developed to adjust packing was not used nor was supervision informed of the

packing leak. Use of the procedure would have resulted in a different system

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configuration which would essentially isolate the valve being worked on from the

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system.

c.

Conclusions

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Personnel error by technicians during surveillance testing on reactor water level

instrumentation resulted in automatic reactor protection and primary containment

isolation actuation. Since the plant was shutdown at the time of the event, there

was no effect on plant operation. The inspector noted that this event contained

similarities with the September 16,1996 scram described in NRC inspection report

50-333/96-06 in that technicians proceeded with work without fully recognizing the

potential to cause a plant transient. The condition la valve packing leak] was not

reported to supervision and the decision to proceed with the packing adjustment

was not challenged.

Based on this review, LER 50-333/96-013 is closed.

M4.2 Hiah Pressure Coolant Iniection incorrect Tubina Installation

a.

Insoection Scope

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On December 9,1996, the high pressure coolant injection (HPCI) turbine would

not roll during ST 4K, HPCI Turbine Slow Roll and overspeed Test, conducted at

150 PSIG reactor pressure. The surveillance test was conducted, in part, as post

work testing. The licensee identified that tubing connecting ports on the governor

hydraulic control system was installed incorrectly. The inspector reviewed the

maintenance procedure, the deviation and event report (DER) response and

discussed the event with the system engineer, in addition, the inspector observed

the performance enhancement review committee (PERC) meeting during which the

personnel error was discussed.

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b.

Observations and Findinas

During maintenance performed on the HPCl turbine, all piping was identified in

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accordance with MP 23.14, Turbine Maintenance. However, the method used to

identify components was to use duct tape and a magic marker. The identification

subsequently became illegible. The tubing was reassembled using the procedure

and the tubing was walked down by the system engineer to verify correct

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installation. Due to the configuration, the walkdown verification failed to identify

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that the tubing was installed incorrectly. The problem was subsequently identified

during post work testing.

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As part of their corrective actions, the licensee initiated ACTS items to provide

better labels for the tubing and connection ports and provided additional

maintenance procedure enhancements.

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c.

Conclusions

Configuration control for reinstallation of tubing for the HPCI governor hydraulic

control system was lost during maintenance when tags used to label components

became illegible. Although efforts were made to regain configuration control for the

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tubing, the licensee failed to ensure that installation was proper. The problem was

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identified during HPCI post work testing.

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E1

Conduct of Engineering

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E1.1

Primarv Containment Leakaae Rate Testina Proaram

a.

Insoection Scone

The licensee submitted and received approval for Technical Specification

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Amendment No. 234 last cycle which allowed the licensee to implement

10 CFR Part 50, Appendix J, Option B, " Performance Based Containment Leakage

Testing", during the refueling outage. The licensee's program is based on Nuclear

Energy Industry NEl 94-01, "Inductry Guidelines For Implementing Performance

Based Option of 10 CFR Part 50, Appendix J, Revision 0, dated July 26,1995.

This document is endorsed by the NRC, with certain industry wide exceptions, in

USNRC Regulatory Guide 1.163. The technical methods utilized by the licensee for

performing Type A, B, and C test are contained in ANSl/ANS-56.8-1994,

Containment System Leakage Testing Requirements. The actual implementation of

the program is conducted in accordance with the licensee's surveillance testing

program. The inspector observed testing, reviewed the program plan and the

results of the localleak rate testing conducted during the refueling outage.

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10

b.

Observations and Findinas

The inspector observed the LLRT performed on penetration X7A in

accordance with ST-398-X7A, Type C Leak Test Main Steam Line A MSIVs.

The test was conducted by a group of auxiliary operators and supervised by

a senior reactor operator. During the outage, testing was conducted on both

shifts with oversight and coordination of the testing being directed from the

work control center. The inspector noted that the operators were

knowledgeable and experienced with the test equipment, procedures were in

use and good communications were noted between operators in the field.

The inspector reviewed the Primary Containment Leakage Rate Testing

Program against the requirements and noted the following:

The licensee's Primary Containment Leakage Rate Testing Program

,

was consistent with 10 CFR 50 Appendix J, Regulatory Guide 1.163

,

and NEl-94-01 Revision O.

Regulatory Guide 1.163, Performance-Based Leak Rate Test Program,

requires that if the test interval for the Type A test is being extended

for 10 years, then at least two refueling outages have to include a

visual examination of accessible portions of the containment. The

licensee completed two consecutive Type A test successfully and is

extending the interval; however a visual examination was not

j

performed as a part of the recent outage. The licensee has developed

and assigned an ACTS item to write a procedure to perform this for

the next outage. The next Type A test is due March 7,2005.

The program allows for reduced testing on good performing valves

and increased test frequency for the poor performers. The inspector

reviewed ST-39B, Type B and C LLRT of Containment Penetrations,

and the licensee's Appendix J Option B Test Program Baseline

j

Evaluation and concluded that all the penetrations which required

LLRT were performed during the last outage or where within current

testing periodicity.

The inspector reviewed the test data and calculations for the as left

minimum and maximum pathway penetration leakage rate and

concluded the calculations were correct. The requirement is for both

values to be less than 63.182 standard liters per minute (SLM). The

minimum pathway was determined to be 16.6764 SLM and the

maximum was 31.9627 SLM.

The inspector reviewed the test data and calculations for the total as

found minimum pathway leakage rate and concluded that the

calculations were correct. The total as found minimum pathway was

determined to be 311 SLM, exceeding the limit of 63.182 SLM. This

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was reported to the NRC in accordance with 10 CFR 50.73 in

Licensee Event Report LER-96-012 and is discussed in section E.1.2.

c.

Conclusions

1

The inspector concluded that the testing was well conducted by the

1

operations staff and the as-left testing data met the requirements for plant

start-up following the refueling outage. The inspector determined that the

Primary Containment Leakage Rate Testing Program was in accordance with

the regulatory requirements and being properly implemented,

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E1.2 (Closed) LER 96-012. Primary Containment Leakaae Exceedina Technical

Soecifications

a.

insoection Scope

j

On November 11,1996, the licensee determined that the as found running total

primary containment leakage rate was in excess of the TS limit of 105.3 SLM and

reported the event in accordance with 10 CFR 50.72. The licensee determined the

as-found running totalleakage rate to be 122 SLM. At the conclusion of the as-

found minimum pathway localleak rate testing conducted during the refueling

outage, the licensee determined the total as found minimum pathway to be 311

SLM, exceeding the limit of 63.182 SLM. The inspector reviewed the LER as part

of the primary containment leakage rate program review.

b.

Observations and Findinas

The licensee processed an equipment failure evaluation (EFE) for each of the LLRT

failures which discusses the causes and corrective actions for each of the failures.

Five of the eight main steam isolation valves (MSIVs) failed to pass testing. The

EFE concluded that this was attributed to normal wear occurring during the closing

stroke of the valve. The licensee utilized a separate vendor supplied valve team

with special tooling to repair the valves. All valves passed the subsequent retests.

The mean time between failures of the MSIVs is about 5 years. The MSIVs are

required to be tested every two years. The corrective actions appear to be

adequate with respect to the MSIV failures.

Three valve failures were Anchor Darling double disk gate valves, which the

licensee determined to be a poor design for steam applications. All three valves

were reworked and subsequently passed the retesting. The EFE resulted in the

generation of problem identification entries (PlDs) to track the replacement of two of

the valves. The inspector noted that the mean time between failures for these

valves was approximately a cycle, in discussion with the licensee's engineering

staff, the inspector learned that the valves were replaced several cycles ago and

albeit the valves have a long history of LLRT failures, the more recent failures are

attributed to the design of the replacement valves. The inspector concluded that

the corrective actions for these valves were adequate.

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One feedwater system non-return valve,34 NRV-111B also has a history of

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LLRT failures while its matching valve, 34 NRB-111 A ht : very good LLRT

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history. The licensee attributed this to a disc to seat misalignment during

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manufacture of the valve. The valve was repaired and subsequently retested

satisfactorily. The long term corrective action for this valve included a PID to

replace the valve or have a field service repair team correct the misalignment

problem. The inspector concluded that the corrective actions were

adequate. The remainder of the failures were attributed to normal wear,

system particle accumulation, and corrosior products.

c.

Conclusions

The inspector concluded that the EFEs for the LLRT faiiures were

comprehensive with appropriate corrective actions completed or planned for

completion. The licensee's decision to replace several poor performing

valves was warranted based on the testing history. The LLRT results over

,

the past several refueling cycles have shown improvement in the number of

as found failures. However, since the as-found running total leakage rate,

based on Type Band C LLRT results was greater than the TS limit, a violation

l

of NRC requirements occurred. This violation will not be cited in accordance

with Section Vll.B.1 of the NRC Enforcement Manual as the violation was

non-recurring, prompt:y corrected and of low safety significance (50-

333/9608-02). Licensee event report LER-96-012, is closed.

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IV. Plant Support

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R1

Radiological Protection and Chemistry (RP&C) Controls

R 1.1 Personnel Contamination Identified at the Security Buildina Radiation Monitor

a.

Insoection Scope

On December 7, a non-licersed operator leaving to go home was identified as

contaminated at the security building radiation monitor. The inspector reviewed the

licensee's followup corrective actions including surveys, portal monitor testing, and

discussed the event with licensee management. Additionally, radiological control

procedures pertinent to the event were reviewed.

b.

Observations and Findinas

On December 7, a non-licensed operator leaving to go home was identified as

contaminated at the security building radiation monitor. A health physics technician

escorted the individual back to the radiation protection office and performed a

whole body count and decontaminated the worker's face and hands. The workers

clothing, including shoes, socks, trousers and outer coat were contaminated up to

12,000 cpm and removed. Following decontamination activities, the worker was

allowed to go home. The worker's egress route was surveyed and no

contamination was found. Additional subsequent surveys identified some

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paperwork located in the control room that the operator had been in contact with

had some detectable contamination, but was less than release limits.

4

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The licensee's review showed that, during the week of December 1, various repairs

l

were being performed on condensate demineralizer valves located in a contaminated

,

area in the turbine building. On December 7, the operators involved were tasked

j

with clearing a protective tagging request (PTR) associated with the system. The

i

first operator did not obtain the required radiation protection briefing prior to-

4'

entering the contaminated area. A second operator entered the area without a brief

because he believed that the shift meeting brief covered the activity and the first

i

!

operator had informed him that the required anti-contamination clothing was booties

f

and gloves. NRC and NYPA review of the event is continuing; this is unreso!ved

item (URI 50-333/96008-03) pending additional review.

1

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c.

Conclusions

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A radiation worker had performed some tasks in a contaminated area and had

!

improperly exited the radiologically controlled area. In addition, the radiation

workers involved did not take proper radiological precautions while performing

I

work.

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t

There were several radiological controls barriers and radiation worker practices

which were not adhered to by the workers involved. These requirements included

the failure to obtain a radiation control brief, not adhering to the radiation work

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permit, wearing inadequate anti-contamination clothing, disregarding radiological

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posting requirements and improper use of the portal monitor. The results were that

'

an individual became contaminated and the potential existed for the spread of

contamination.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of the licensee management at

{

the conc usion of the inspection on January 14,1997. The licensee acknowledged the

>

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

X2

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary to the Updated

Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused

review that compares plant practices, procedures and/or parameters to the UFSAR

description. While performing the inspections discussed in this report, the inspector

reviewed the applicable portions of the UFSAR that related to the areas inspected. The

inspector verified that the UFSAR wording was consistent with the observed plant

practices, procedure and/or parameters.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. Colomb, Plant Manager

R. Locy, Operations Manager

D. Ruddy, Director, Design Engineering

J. Maurer, General Manager, Support Services

NB.G

C. Cowgill, Chief, Projects Branch 2

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INSPECTION PROCEDURES USED

37550

Engineering

37551

Onsite Engineering

62703

Mrintenance Observations

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61726

Surveillance Observations

,

71707

Plant Operations

,

71750

Plant Support

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92903

Followup - Engineering

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ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

,

50-333/96008-01

VIO

failure to perform a 50.59 safety evaluation

1

50-333/96008-02

NCV primary containment leakage exceeding technical specifications

,

50-333/96008-03

URI

improper radiation worker practices by a non-licensed operator

Closed

50-333/96008-02

NCV primary containment leakage exceeding technical specifications

!

50-333/96007

LER

Engineered Safety Feature Activation Due to False High

Radiation Isolation Signal.

50-333/96012

LER

Primary Containment Leakage in Excess of TS Limits

50-333/96013

LER

Reactor Protection and Primary Containment isolation System

Actuation on False Low Reactor Water Level Due to Personnel

Error

50-333/95021-01

URI

residual heat removal pump operation

Discussed

None

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LIST OF ACRONYMS USED

ALARA

As Low As Reasonably Achievable

ASME

American Society of Mechanical Engineers

BWR

Boiling Water Reactor

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

DAW

Dry Active Waste

DP

differentia; pressure

dpm

disintegrations per minute

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

ESF

Engineered Safety Feature

,

FME

Foreign Material Exclusion

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FR

Federal Register

FWLCS

Feedwater Level Control System

,

HCU

Hydraulic Control Unit

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HPCI

High Pressure Coolant injection

IFl

Inspection Followup Item

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IPE

Individual Plant Evaluation

IR

Inspection Report

ISEG

Independent Safety Engineering Group

ISI

Inservice inspection

IST

Inservice Testing

LER

Licensee Event Report

)

LSA

Low Specific Activity

MSIV

Main Steam Isolation Valves

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

NRC

Nuclear Regulatory Commission

OSHA

Occupational Safety and Health Administration

PEP

Performance Enhancement Program

)

ppm

parts per million

PSA

Probabilistic Safety Assessment

j

psig

pounds per square inch gage

QA

Quality Assurance

QC

Quality Control

RCA

Radiological Controlled Area

RCIC

Reactor Core Isolation Cooling

RHR

Residual Heat Removal

RP

Radiation Protection

RP&C

Radiological Protection and Chemistry

RWCU

Reactor Water Clean-Up

RWP

Radiation Work Permit

SCO

Surface Contaminated Objects

SRV

Safety Relief Valve

TS

Technical Specification

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UE

Unusual Event

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UFSAR

Updated Final Safety Analysis Report

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VIO

Violation

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ATTACHMENT 1

r.t

.

UNITED STATES

g

j

NUCLEAR REGULATORY COMMISSION

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WASHINGTON, D.C. 20555 @ 01

% , j ,o

October 30, 1996

MEMORANDUM T0:

Curtis Cowgill

Division of Reactor Projects, Region I

FROM:

S. Singh Bajwa, Acting DirectorgAy4/p 7//M

.

Project Directorate I-l

Division of Reactor Projects - I/II

Office of Nuclear Reactor Regulation

SUBJECT:

TIA REGARDING DESIGN BASIS FUNCTIONALITY OF FITZPATRICK RHR

SYSTEM WHEN OPERATED IN THE SUPPRESSION POOL COOLING MODE

(TAC N0. M94319)

By letter dated December 12, 1995, the Region raise / concerns regarding water

hammer issues and extended operation of the residual heat removal (RHR) system

in the Suppression Pool Cooling (SPC) mode.

The memorandum in particular

stated a position that the regional staff considers that operation of the RHR

system in secondary modes of operation for extended periods of time without

consideration of the inherent susceptibility to water hammer is unacceptable.

NRR is in agreement with the Region's position. We consider that frequent

long-term operation of RHR in the SPC mode constitutes an unreviewed safety

question (USQ).

For example, when operating in the SPC mode, the RHR system

is more likely to undergo a water hammer event should there be a loss of

station power. Hence, the probability of a water hammer event is increased in

direct proportion to the amount of time the system is operated in the SPC.

Furthermore, the likelihood of a malfunction of the RHR system is increased

when subjected to a water hammer event. Therefore, an increase in the

likelihood of a water hammer increases the likelihood of a malfunction of a

system important to safety. This meets the criterion for an USQ per 10 CFR 50.59(a)(2)(i).

We also believe that long-term operation of the RHR in the SPC mode

constitutes a modification to the facility which should be (and should have

been) subject to a 10 CFR 50.59 evaluation. We will recommend to the Generic

Communications Branch to send a generic letter to all the BWR licensees

stating our position.

The staff has previously evaluated the water hammer issue on a generic basis.

In Table 3-1 of NUREG-0927, BWR system water hammer causes are listed and

CONTALT:

George Thomas, SRXB/DSSA

415-1814

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the frequency of operation of RHR in the SPC mode.

Licensees typically have

'

administrative controls in place to limit the use of RHR system in the SPC

mode and, thereby, reduce the potential for water hammer of the RHR system.

We believe that similar controls should be in place at FitzPatrick.

Finally, the Region provided four specific questions regarding SPC operation

at FitzPatrick, they are addressed in the attachment.

Attachment: As stated

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Response to Reaion I TIA reaardina

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Suporession Pool Coolina Mode of

j

Operation at FitzPatrick

i

Q 1.

Was the operation of both RHR loops for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> on November 10, 1995,

at Fitzpatrick an unreviewed safety question (USQ)?

No.

We do not believe that an isolated instance of both RHR loops in SPC

such as the operation on November 10, 1995, constitutes an USQ. We believe

that such infrequent operation is included in the system design basis as

described in the FSAR which includes both periodic short-term operation as

well as long-term post accident operation.

Q 2.

Should RHR be considered inoparable for purposes of ECCS when run in the

SPC mode?

No.

RHR is considered operable for purposes of ECCS when run in the SPC mode

or in the test mode.

The RHR system is designed for automatic alignment to

the LPCI mode if the system is in the SPC mode or in the test mode.

The

cumulative running time must be considered in light of maintenance

specifications and pump maintenance and pump testing programs. As long as the

pump is maintained in accordance with these programs, the RHR pumps are

considered operable for purpose of ECCS.

Q 3.

Is extended use of RHR in the SPC mode (viz., one pump more than 2

hours, both loops simultaneously, or cumulative run time in excess of 100

hours annually) beyond the licensing basis?

Yes. We believe that extended use (increased frequency and long duration) of

RHR system in the SPC mode is beyond the licensing basis.

Frequent use of the

RHR system in the SPC mode changes the original design basis analysis (iOCA)

assumptions.

For example, in the original design of the RHR system, the

closing speeds of the valves in the system cooling / test lines were specified

as standard speed (12 inches / minute) and not fast closing valves such as the

LPCI injection valves.

Since the cooling / test return valves take longer to

close than the LPCI injection valves take to open, there is a potential for

the core injection flow to be diverted to the suppression pool. The ECCS

performance analysis does not include the longer closing time of the test line

vales since they are assumed to be normally closed. As the amount of time

(the time the test valves are kept open) increases, the assumption is

invalidated resulting in an unanalyzed condition.

Q 4.

Should E0Ps be reevaluated with respect to the meaning "----operate all

available torus cooling?" Should torus cooling be optimized along a

divisional basis until the need to maximize torus cooling is demonstrated?

Should a caution statement concerning the potential water-hammering a voided

system be considered?

The FitzPatrick E0P for torus cooling states the following:

" Operate all

available torus cooling, use only RHR pumps which do not have to be run

continuously in the LPCI mode for core cooling." This is in agreement with

the EPG, Rev.4 SER which states:

"The EPGs are based upon maintaining core

cooling and primary containment integrity.

In all but a few cases the EPG

Attachment

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I

emphasize core cooling.

But in a few specific situations, when a decision

between a possible loss of adequate core cooling and a loss of primary

containment integrity must be made, the EPGs preferentially choose to maintain

primary containment integrity in order to protect against the uncontrolled

release of radioactivity to the general public from a degraded core

l

condition." The LPCI mode of operation supersedes all other modes of RHR

except for scenarios where the containment integrity is in danger. This

philosophy should be taught to the operators during the training process.

Therefore, unless, it is found that the licensee's training program is

deficient with regard to emphasizing the primacy of the LPCI mode of

operation, or if the E0P fail to caution the operator in this regard, there is

,

no need to modify the E0P for torus cooling optimization along a divisional

basis.

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