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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20116B4391996-07-24024 July 1996 Special Rept 96-003:on 960617 Declared Reactor Vessel Level Indicating System B Train Inoperable.Determined Probable Cause to Be within Resistance Temp Detector (Rtd).Tagged RTD out-of-service & Performed Further Troubleshooting ML20107M3571996-04-25025 April 1996 Special Rept 96-002:on 960327,RCS Pressure Exceeded Setpoint of 445 Psig for PORV 455A When Cooler,Denser Water,In Vessel Warmed & Expanded,But Did Not Approach TS Limit of 485 Psig. RCS Pressure Subsequently Stabilized at Approx 335 Psig ML20091L0931995-08-22022 August 1995 Special Rept 95-002:on 950727,valid Failure of EDG B Occurred.Util Believes Overspeed Plunger Partially Extended & Repositioned Overspeed Trip Lever.Adjusted Governor to Reduce Max Frequency Experienced by EDG B During Startup ML20086B8271995-06-28028 June 1995 Special Rept 95-001:on 950531,output Breaker for B EDG Tripped During Performance of Routine Monthly Testing.Ega Replaced & EDG B Was Evaluated & Determined to Be Operable ML20078B9401994-10-21021 October 1994 Special Rept 94-003,providing Info Re Number of Tubes Plugged in Each SG as Required by TS 4.4.5.5 ML20071L5211994-07-29029 July 1994 Special Rept 94-002:on 940701 & 08,reported to CR That Net Refill Vols of Sheathing Filler Matl Exceeded 5 Percent of Net Duct Vol for Tendons V39 & 25CB.Voids Filled by Addl Grease Pumped Into Tendon Ducts ML20070N7031994-05-0303 May 1994 Special Rept 94-001:on 940329,seismic Monitoring Channel Declared Inoperable Due to Location on Exterior Reactor Cavity West Wall within Biological Shield Wall.Entire Accelermeter Package to Be Replaced ML20127G2021993-01-12012 January 1993 Special Rept 93-001:on 921229,10-60 Meter Elevation Delta Temp Indication for Meteorological Tower Declared Inoperable Due to Erratic Indications.Ice Shields Installed to Minimize Recurrence ML20101P9731992-07-0808 July 1992 Special Rept 92-002:on 920608,valid Failure of EDG B Occurred Due to Failure to Temp Control Valve.Caused by Failure of Two Out of Three Power Pills.Power Pills Replaced & EDG Testing Frequency Increased ML20097A2831992-05-29029 May 1992 Special Rept 91-007,reporting Results of Fourth SG Tube Inservice Insp Completed by Westinghouse on 911024 of SGs a & C ML20098D6951992-05-26026 May 1992 Special Rept 92-001:on 920422,invalid Failure of EDG a Occurred When Output Breaker Tripped on Reverse Power.Caused by Megawatt Meter Used to Load EDG Reading 0.2 MW W/Edg in Standby.Meters Rezeroed to Ensure Proper Load Applied ML20086P8301991-12-20020 December 1991 Special Rept 91-006:on 911121,operators Depressed Test Button to Energize Relay K615 But EDG a Would Not Start. Caused by Incomplete Description of Initial Conditions in Surveillance Procedure.Statement Added to Procedure ML20086L8151991-12-12012 December 1991 Special Rept 91-005:on 911112,invalid Failure of Emergency Diesel Generator B Occurred During Train a Safeguards Actuation Test.Caused by Binding of Temporary Test Flag in Alternate Supply Breaker Cubicle.Test Flags Modified ML20079L9871991-11-0101 November 1991 Special Rept 91-004:all Inconel 600 Mechanical Tube Plugs in Steam Generators a & C Removed During Fourth Steam Generator Inservice Insp from 911016-24.Tubes Replugged W/Inconel 690 Except for Tubes R28C56 & R28C76 in Steam Generator C ML20082U0911991-09-16016 September 1991 Special Rept 91-003:on 910819,invalid Failure of EDG B. Caused by Unit Parallel Relay.Hermetically Sealed Relay Being Evaluated as Means to Prevent Similar Failures of Relay ML20070U0031991-04-0202 April 1991 Special Rept 91-002:on 910304,invalid Failure of Emergency Diesel Generator a Occurred.Caused by Failure of Operator to Verify That Correct Switch Adjusted Before Adding Load to Diesel Generator.Operator Counseled ML20155J1691988-10-17017 October 1988 Suppl 1 to Special Rept 85-011 Re Inoperable Loose Part Detection Sys Channel.On 850912,Channel 10 of Loose Part Detection Sys Declared Inoperable.Caused by Faulty Preamplifier Charge Converter.Converter Replaced ML20154M0571988-05-27027 May 1988 Special Rept 87-015-01:on 871211,failure of Emergency Diesel Generator a Occurred When Cracked Lube Oil Line Fitting Caused Excessive Leakage.Procedure Initiated That Will Require Use of Vendor Recommended Heavier Grade Oil ML20154M0181988-05-27027 May 1988 Special Rept 87-016-01:on 871219,diesel Generator B Failed When Generator Could Not Be Synchronized to Bus.Caused by Potential Transformer Fuse Knives Not Inserting Fully Into Fuse Stabs.Insp Windows on Each Cubicle Recommended ML20148A4081988-01-14014 January 1988 Special Rept 87-016:on 871219,failure of Emergency Diesel Generator B Occurred When Generator Not Synchronized W/Bus. Caused by Repeated Opening & Closing of roll-out Potential Transformer.Engineering Evaluation in Progress ML20147C1741988-01-0808 January 1988 Special Rept 87-015:on 871211,failure of Emergency Diesel Generator a Occurred Due to Excessive Leakage.Caused by Cracked Lube Oil Line Fitting.Fitting Replaced & Retested for Leakage.Cause of Cracking Not Determined ML20149F8141988-01-0707 January 1988 Special Rept 87-013:on 871109,discovered Low Level Radioactive Matl Delivered to Coffey County Land Fill.Caused by Nonlicensed Util Personnel Error.Procedure for Release of Radioactive Matl Revised ML20238C7871987-12-24024 December 1987 Special Rept 87-10,Suppl 2:voids in Tendon Sheathing Attributed to Listed Additive Factors,Quality Program Described,Grease Installation & Insp Discussed & Audits & Surveillance of Const Operations Conducted ML20237E6311987-12-18018 December 1987 Special Rept 87-014:on 871014,hydrogen Pressurizer Ignited. Caused by Inadequate Pressurizer Draining & Depressurizing Procedure.Procedure Review & Rev & Control Room Personnel Training Planned ML20195K3281987-11-16016 November 1987 Reportable Event 10691:on 871116,trash Bag Containing Low Level Contamination Found During Survey of Coffee County Landfill as Followup to Reportable Event 10646.Contaminated Rag Returned to Plant.Survey Continuing ML20195K3171987-11-11011 November 1987 Reportable Event 10646:on 871109,discovered That Low Level Radioactive Sheets of Metal Removed from Site & Delivered to Coffee County Landfill.All But Three Pieces Recovered.Search for Remaining Pieces Continuing ML20235K4511987-09-28028 September 1987 Suppl 1 to Special Rept 87-10:third Yr Tendon Surveillance on 870801-0914 Indicated That Net Refill Vols of Sheathing Filler Grease Exceeded 5% of Net Duct Vol for Tendons. Investigation Being Performed to Determine Causes of Voids ML20238F7771987-09-11011 September 1987 Special Rept 87-010:inservice Tendon Surveillance Voids in Excess of 5% of Net Duct Vol Discovered.Cause Not Stated. Prevention of Tendon Corrosion Assured by Adequately Coating Tendon Wires & Anchorage ML20214U0691987-06-0505 June 1987 Special Rept 87-006:on 870429,seismic Monitoring Instrumentation Channel Declared Inoperable & Remained Out of Svc for More than 30 Days.Caused by Faulty Voltage Regulating Printed Circuit Board.Board Will Be Replaced ML20207E8721986-12-24024 December 1986 Special Rept 86-011:on 861201,failure of Emergency Diesel Generator a Occurred.Caused by Faulty Speed Switch.Switch Replaced.Faulty Switch Returned to Vendor for Failure Analysis & Repair ML20212D9601986-12-22022 December 1986 Suppl 1 to Special Rept 85-010:on 851001,two Failures of Diesel Generator a Occurred.Caused by Mild Fluctuations in Engine Speed & Output Breaker Trip on Reverse Power.Oil Added to Correct Fluctuations ML20214K2831986-11-18018 November 1986 Special Rept 86-005:on 861018,19 & 31,ESF Switchgear Rooms I & II Exceeded Max Temp Limit Specified in Tech Specs. Caused by Inoperability of Cooling Unit ML20198E4531986-05-12012 May 1986 Special Rept 86-002:on 860412,invalid Failure of Emergency Diesel Generator B Occurred During Surveillance Procedure STS KJ-001B.Caused by Malfunctioning Unit Parallel Relay. Relay Replaced ML20154N3591986-03-0606 March 1986 Special Rept 86-001:on 860127,net Refill Vols of Sheathing Filler Grease Exceeded 5% of Net Duct Vol for Listed Tendons.Caused by Physical Characteristics of Sheathing Filler Matl & Industry Std Installation Techniques ML20140D2741986-01-14014 January 1986 Special Rept 85-015:on 851215,diesel Generator B Output Breaker Tripped on Reserve Power.Caused by Operator Error. Operator Reclosed Output Breaker & Successfully Paralleled & Loaded Unit ML20138P1731985-12-0909 December 1985 Special Rept 85-014:on 851029,Channel 8 of loose-part Detection Sys Declared Inoperable.Cause Believed to Be in Either Charge Converter or Accelerometer.Investigations Underway ML20136G0331985-11-0101 November 1985 Special Rept 85-012:on 851003,invalid Failure of Diesel Generator B Occurred.Possibly Caused by Vent Petcocks Vibrating Open.Precautions Added to Procedures STS KJ-005B & STS KJ-005A to Ensure Petcocks Fully Closed ML20136C7651985-10-31031 October 1985 Special Rept 85-010:on 851001,two Failures of Diesel Generator a Occurred.Caused by Closed Governor Needle Valve. Valve Opened Slightly & Procedure Sys KJ-121, Diesel Generator NE01 & NE02 Lineup for Automatic... Revised ML20198B2731985-10-22022 October 1985 Special Rept 85-011:on 850912,Channel 10 of Loose Part Detection Sys Declared Inoperable During Surveillance Procedure.Investigation Conducted to Discover Root Cause & Plans for Restoring Inoperable Channel to Svc ML20133G7531985-07-16016 July 1985 Special Rept 85-009:on 850428,30 & 0506,ECCS Actuations Occurred.Caused by Personnel Error & Rate Sensitive Nature of Circuitry.Emphasis Being Placed on Rate Sensitive Nature of Circuitry During Requalification & Hot License Training ML20129A4011985-06-28028 June 1985 Special Rept 85-006:on 850601,during Periodic Surveillance Testing of Diesel Generator A,Generator Secured Prematurely Due to Erratic Low Jacket Water Pressure Indication & Alarm. Caused by Use of Valve Lineup to Test Starting Air Sys ML20140F4381985-06-24024 June 1985 Special Rept 85-008:on 850415,containment Base Slab Seismic Monitor Declared Inoperable Due to Failed Power Supply.Cause Unknown.New Power Supply Ordered.Temporary Power Supply Installed ML20127N4841985-06-10010 June 1985 Special Rept 85-007 Re Positive Moderator Temp Coefficient for Withdrawn Control Rods.Hot Zero Thermal Power Condition within Tech Spec 3.1.1.3a Limit.Control Rod Withdrawal Limits Incorporated Into Operating Procedures ML20126J2921985-05-30030 May 1985 Special Rept 85-005:on 850502,invalid Failure of Diesel Generator a Occurred Due to Personnel Oversight in Restoring Diesel to Svc After Planned Outage.On 850501,diesel Generator a Taken Out of Svc for Insp of Welds ML20128E6631985-05-17017 May 1985 Special Rept 85-004:on 850419,invalid Failure of Diesel Generator Occurred.Caused by Operating Error.Rept Will Be Added to Operations Required Reading to Emphasize Importance of Close Adherence to Procedural Steps ML20128B6281985-05-0909 May 1985 Special Rept 85-003:on 850409,black Smoke Observed Coming from Manifold of Diesel Generator B When Generator Started After Hot Web Deflection.Caused by Failure to Close Cylinder Petcocks.Petcocks Closed ML20117G0411985-05-0101 May 1985 Special Rept 85-002:on 850401,during Periodic Testing,Diesel Generator a Failed Due to Restrictive Acceptance Criteria & Personnel Error.Procedure STS KJ-0054A Revised & Personnel Instructed on Importance of Following Procedures ML20117G1621985-04-29029 April 1985 Special Rept 85-001:on 850330,invalid Failure of Diesel Generator A,NE01,occurred.Caused by Personnel Oversight Resulting in Inadequate Venting of Fuel Oil Lines After Maint.Work Request Procedure Revised 1998-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
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KANSAS GAS AND ELECTRIC COMPANY THE ELECTAC COMPANY GLENN L KOESTER veCE pet tiotNT - NUCLE AR July 16, 1985 Mr. R.D. Martin, Regional Administrator U.S. Nuclear Regulatory Comnission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 KMLtGC 85-183 Re: Docket No. STN 50-482 Subj: Special Report 85-009
Dear Mr. Martin:
The enclosed Special Report is submitted pirsuant to Technical Spx:ifications 6.9.2 and 3.5.2.
If you have any questions concerning this matter, please contact ne or Mr. Otto Maynard of my staff.
Yours very truly, Glenn L. Koester
< Vice President - M1 clear Gm: dab Enclosure xc: PO'Connor (2), w/a JCunmins,w/a g- 6M 5 esoso9oo6a eso716 PDR ADOCK 05000402 S PDR
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201 N. Market - Wichita, Kansas - Mail Address: RO. Box 208 I Wichita, Kansas 67201 - Telephone: Area Code (316) 261-6451 l
SPECIAL RITORP 85-009 Bnergency Core Cooling Systen Actuations This Special Report is being subnitted pursuant to Technical Specification 3.5.2 Action Statement b. and Technical Specification 6.9.2. Contained herein are descriptions of the circumstances of three Energency Core Cooling Systen (ECCS) actuations which occurred on April 28, 1985, April 30, 1985, aM May 6,1985. Also included in this report is the total accumulated actuation cycles to date and information on the current value of the Safety Injection nozzle usage factor.
The first ECCS actuation occurred on April 28, 1985, aM is discussed in Licensee Event Report 85-021-00, which was transmitted via KMENRC 85-126, dated May 24, 1985. W is actuation was initiated by a low steamline pressure signal on Stean Generator (S/G) " D" .
At the time of this event, the plant was in Made 3, Hot Standby, prior to initial criticality. The Reactor Coolant System (RCS) was being maintained at 505-510 degrees F and 2100 psig. We pressurizer level was being manually controlled at approximately 27 percent. Pressurizer pressure was also being manually controlled. We steamline pressure was approximately 700 psig, with feedwater being supplied by the Motor Driven Startup Feed Pump, and the Stean Generator (S/G) "C" Power Operated Relief Valve (PORV) was open approximately 25 percent controlling temperature in the RCS.
Testing was being performed on the Main Steamline Isolation Valves (MSLIV's) in accordance with surveillance procedure STS-AB-201, " Main Steam System Inservice Valve Test", and all four MSLIV's were closed. W e MSLIV bypass valves had just been reopened, and the test performer requested that MSLIV AB-IN-ll be opened in order to continue with the surveillance test. We operator initiated the opening of AB-IN-ll and shortly thereafter, at approximately 1550 CDP, the Safety Injection and Main Steanline Isolation occurred due to low steanline pressure.
All Engineered Safety Features equipnent required to actuate responded nroperly, except for the Control Roan Energency Ventilation System which was already in operation due to a Technical Specificat 200 Action Statement regarding an inoperable ra3iation monitor. Thr / ninor equipment problens were noticed. BM-IN-003, a S/G "C" Blowdown M. ion Valve, leaked through following closure at approximately 7000 T r V . le status of SGL15B, a Penetration Roan Cooler in the Auxiliary #_lC , did not display on the ESF status panel, although the cooler did function properly. Also, AL-IN-5, an auxiliary feed regulating valve on S/G "D" did not modulate smoothly.
An Unusual Event was declared and subsequently terminated in accordance with the Energency Plan Implementing Procedures. W e appropriate federal, state, aM local agencies were notified.
Approximately 2000 gallons of water were injected into the RCS from the Refueling Water Storage Tank, causing pressurizer level to increase to approximately 61 percent and RCS pressure to increase to approximately 2340 psig. One Centrifugal Charging Pump was secured during this event in order to limit the RCS pressure transient. Nevertheless, the RCS pressure did reach the set point of the pressurizer Power Operated Relief Valves (PORV's) , and both PORV's did lift. We temperature of the RCS decreased slightly aM the Safety Injection was terminated at approximately 1557 CUP in accordance with plant procedures H4G E-0, " Safety Injection" and B4G ES-03, "SI Termination".
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Page 2 The initiating signal, low steanline pressure, has been attributed to the rate-sensitive nature of the steanline pressure circuitry. The operator opened the MSLIV before the pressure had equalized through the bypass valves aM the result was a rapid decrease in pressure of approximately 10-15 psig in the steamline.
Wis decrease in stean pressure signal was fed into the logic circuits, amplified by a factor of 10, aM was sufficient to reach the low steamline pressure trip setpoint.
Work Requests were initiated to investigate the equipnent problems that were noted during this event. The status of SGL15B did not indicate on the ESF panel due to a warped contact block which has been replaced. BM-HV-003 and AL-HV-5 have been reworked, and demonstrated to stroke aM seat properly.
Although this event has been attributed to a personnel error, the rate sensitive nature of the circuitry contributed substantially to this event. As a result of this event, more emphasis is being placed on the rate-sensitive nature of certain circuitry during Requalification Training and Hot License Trainirg sessions.
This event was the first actuation of ECCS subsystems while the plant was at near normal. operating temperature and pressure.
We second ECCS actuation occurred on April 30, 1985, and is discussed in Licensee Event Report 85-022-00, which was transmitted via KMIRRC 85-132, dated May 30, 1985. %is actuation also occurred due to a low steanline pressure signal.
At the time of this actuation, the plant was in Mode 3, Hot Standby, prior to initial criticality. We RCS was at the normal operating temperature, 557 degrees F, and pressure, 2250 psig. Pressurizer level was beiry manually maintained at approximately 22 percent and pressure was being maintained automatically. We secondary side was being maintained in steMy state conditions by dumpiry steam to the condenser.
When the Safety Injection Signal occurred, all ESF equipment required to actuate with the plant in Mode 3 responded properly. The pressurizer pressure control system limited the pressure transient in the RCS to a maximun of 2328 psig, and the pressurizer level increased to'38 percent. The minimum RCS temperature durirq this event was 551 degrees F. We pressurizer Power Operated Relief Valves did not lift l during this transient.
The operators carried out the appropriate steps of procedure EMG E-0, " Safety l Injection", and when steady state conditions were reached the appropriate steps of the SI recovery procedure ES-03, "SI Termination", were performed. W e Safety Injection was terminated by approximately 1155 cur.
An Unusual Event was declared and terminated. We appropriate federal, state, and local agencies were notified in accordance with the anergency Plan Implementing Procedures.
We Post Trip Review revealed that steanline pressure never reached the trip setpoint for low steamline pressure, although the indications on steam generators "B" and "C" did show a momentary decrease in pressure from 1070.2 and 1065.8 psig to 746.5 and 925.8 psig respectively. Shortly after this pressure dip, the pressure returned to normal. Although the decrease in stean pressure did not reach the low pressure satpoint, the rate sensitive nature of the signal circuit caused an anticipatory trip. %us, the initiating signal of low steanline pressure was due to the step decrease in steamline pressure.
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Page 3 Subsequent investigations into this event co . firmed that the step decrease in the steam pressure signal was caused by interftence from an operator's ham held radio transmission. An operator was standing ia the area of the steamline pressure transmitters aM had keyed his radio just prior to the initiation of this event.
This scenario has been re-enacted with the result being an identical response. At the time of re-enactment, the plant was below the P-ll interlock point, and no actuation of ESP equipnent occurred, but the required logic for a low steanline pressure signal was induced.
As a result of this event, the use of radios within the plant was severely restricted and more stringently controlled.
We third ECCS subsystem actuation occurred on May 6,1985, and is discussed in Licensee Event Report 85-027-00, which was transmitted via KMINRC 85-145, dated May 31, 1985. %is actuation was also initiated by a low steanline pressure signal.
At the time of this event, the plant was in Mode 3, Hot StaMby, prior to initial criticality, and hot, no-flow control rod drop testing on Control Bank "B" was in progress. The Reactor Coolant Pumps (RCPs) and Main Steamline Isolation Valves had been secured to support this testing, aM the average temperature of the RCS was approximately 530 degrees F. The RCS pressure was approximately 2241 psig. The pressurizer level was being controlled manually at approximately 23 percent and pressure was being controlled autanatically. Steam Generators "A" and "C" were being slowly fed via the Main Feedwater Bypass Valves to adjust level. With no significant heat transfer to the Steam Generators fran the RCS, the Mdition of feedwater resulted in cooling the Steam Generators and decreasing the steamline pressure to the trip setpoint for low steamline pressure (615 psig), aM the Safety Injection and Main Steamline Isolation signals occurred.
An Unusual Event was declared aM subsequently terminated. The appropriate federal, state, and local agencies were notified in accordance with the Dnergency Plan Implementing Procedures.
All ESF equignent responded properly. The RCS pressure transient was limited to approximately 2340 psig by the Pressurizer Power Operated Relief Valves.
Pressurizer level increased to 56 percent during this event, and the lowest temperature in the RCS was approximately 500 degrees F.
We Safety Injection was terminated in accordance with plant procedures EMG E-0,
" Safety Injection", and EMG ES-03, "SI Termination", at approximately 1243 CI7r.
The circumstances which led to this event have been discussed with the operating personnel in shift briefings and crew meetings stressing operator awareness of plant status, and particularly early recognition of developing trends. In addition, since the plant conditions allowing no RCS flow through the Steam Generators (minimum or no decay heat present) will only reoccur after subsequent refuelings, the information pertaining to this event has been Mded to a Post-Refueling Action File, maintained by Training, which contains items to be stressed to the operators durire the Requalification Training presented near the time of refueling.
In each of the three actuations at near normal operating temperature and pressure which have occurred, the usage factor for each Safety Injection nozzle was below the 0.70 limit specified by Technical Specification 3.5.2 Action Statement b.
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Page 4 In each instance, the ECCS equipnent performed its intended safety function, no release of radioactivity occurred, ard at no time was there a threat to the health and safety of the public.
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