ML20133G753

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Special Rept 85-009:on 850428,30 & 0506,ECCS Actuations Occurred.Caused by Personnel Error & Rate Sensitive Nature of Circuitry.Emphasis Being Placed on Rate Sensitive Nature of Circuitry During Requalification & Hot License Training
ML20133G753
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/16/1985
From: Koester G
KANSAS GAS & ELECTRIC CO.
To: Martin R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
85-009, 85-9, KMLNRC-85-183, NUDOCS 8508090063
Download: ML20133G753 (5)


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KANSAS GAS AND ELECTRIC COMPANY THE ELECTAC COMPANY GLENN L KOESTER veCE pet tiotNT - NUCLE AR July 16, 1985 Mr. R.D. Martin, Regional Administrator U.S. Nuclear Regulatory Comnission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 KMLtGC 85-183 Re: Docket No. STN 50-482 Subj: Special Report 85-009

Dear Mr. Martin:

The enclosed Special Report is submitted pirsuant to Technical Spx:ifications 6.9.2 and 3.5.2.

If you have any questions concerning this matter, please contact ne or Mr. Otto Maynard of my staff.

Yours very truly, Glenn L. Koester

< Vice President - M1 clear Gm: dab Enclosure xc: PO'Connor (2), w/a JCunmins,w/a g- 6M 5 esoso9oo6a eso716 PDR ADOCK 05000402 S PDR

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201 N. Market - Wichita, Kansas - Mail Address: RO. Box 208 I Wichita, Kansas 67201 - Telephone: Area Code (316) 261-6451 l

SPECIAL RITORP 85-009 Bnergency Core Cooling Systen Actuations This Special Report is being subnitted pursuant to Technical Specification 3.5.2 Action Statement b. and Technical Specification 6.9.2. Contained herein are descriptions of the circumstances of three Energency Core Cooling Systen (ECCS) actuations which occurred on April 28, 1985, April 30, 1985, aM May 6,1985. Also included in this report is the total accumulated actuation cycles to date and information on the current value of the Safety Injection nozzle usage factor.

The first ECCS actuation occurred on April 28, 1985, aM is discussed in Licensee Event Report 85-021-00, which was transmitted via KMENRC 85-126, dated May 24, 1985. W is actuation was initiated by a low steamline pressure signal on Stean Generator (S/G) " D" .

At the time of this event, the plant was in Made 3, Hot Standby, prior to initial criticality. The Reactor Coolant System (RCS) was being maintained at 505-510 degrees F and 2100 psig. We pressurizer level was being manually controlled at approximately 27 percent. Pressurizer pressure was also being manually controlled. We steamline pressure was approximately 700 psig, with feedwater being supplied by the Motor Driven Startup Feed Pump, and the Stean Generator (S/G) "C" Power Operated Relief Valve (PORV) was open approximately 25 percent controlling temperature in the RCS.

Testing was being performed on the Main Steamline Isolation Valves (MSLIV's) in accordance with surveillance procedure STS-AB-201, " Main Steam System Inservice Valve Test", and all four MSLIV's were closed. W e MSLIV bypass valves had just been reopened, and the test performer requested that MSLIV AB-IN-ll be opened in order to continue with the surveillance test. We operator initiated the opening of AB-IN-ll and shortly thereafter, at approximately 1550 CDP, the Safety Injection and Main Steanline Isolation occurred due to low steanline pressure.

All Engineered Safety Features equipnent required to actuate responded nroperly, except for the Control Roan Energency Ventilation System which was already in operation due to a Technical Specificat 200 Action Statement regarding an inoperable ra3iation monitor. Thr / ninor equipment problens were noticed. BM-IN-003, a S/G "C" Blowdown M. ion Valve, leaked through following closure at approximately 7000 T r V . le status of SGL15B, a Penetration Roan Cooler in the Auxiliary #_lC , did not display on the ESF status panel, although the cooler did function properly. Also, AL-IN-5, an auxiliary feed regulating valve on S/G "D" did not modulate smoothly.

An Unusual Event was declared and subsequently terminated in accordance with the Energency Plan Implementing Procedures. W e appropriate federal, state, aM local agencies were notified.

Approximately 2000 gallons of water were injected into the RCS from the Refueling Water Storage Tank, causing pressurizer level to increase to approximately 61 percent and RCS pressure to increase to approximately 2340 psig. One Centrifugal Charging Pump was secured during this event in order to limit the RCS pressure transient. Nevertheless, the RCS pressure did reach the set point of the pressurizer Power Operated Relief Valves (PORV's) , and both PORV's did lift. We temperature of the RCS decreased slightly aM the Safety Injection was terminated at approximately 1557 CUP in accordance with plant procedures H4G E-0, " Safety Injection" and B4G ES-03, "SI Termination".

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Page 2 The initiating signal, low steanline pressure, has been attributed to the rate-sensitive nature of the steanline pressure circuitry. The operator opened the MSLIV before the pressure had equalized through the bypass valves aM the result was a rapid decrease in pressure of approximately 10-15 psig in the steamline.

Wis decrease in stean pressure signal was fed into the logic circuits, amplified by a factor of 10, aM was sufficient to reach the low steamline pressure trip setpoint.

Work Requests were initiated to investigate the equipnent problems that were noted during this event. The status of SGL15B did not indicate on the ESF panel due to a warped contact block which has been replaced. BM-HV-003 and AL-HV-5 have been reworked, and demonstrated to stroke aM seat properly.

Although this event has been attributed to a personnel error, the rate sensitive nature of the circuitry contributed substantially to this event. As a result of this event, more emphasis is being placed on the rate-sensitive nature of certain circuitry during Requalification Training and Hot License Trainirg sessions.

This event was the first actuation of ECCS subsystems while the plant was at near normal. operating temperature and pressure.

We second ECCS actuation occurred on April 30, 1985, and is discussed in Licensee Event Report 85-022-00, which was transmitted via KMIRRC 85-132, dated May 30, 1985. %is actuation also occurred due to a low steanline pressure signal.

At the time of this actuation, the plant was in Mode 3, Hot Standby, prior to initial criticality. We RCS was at the normal operating temperature, 557 degrees F, and pressure, 2250 psig. Pressurizer level was beiry manually maintained at approximately 22 percent and pressure was being maintained automatically. We secondary side was being maintained in steMy state conditions by dumpiry steam to the condenser.

When the Safety Injection Signal occurred, all ESF equipment required to actuate with the plant in Mode 3 responded properly. The pressurizer pressure control system limited the pressure transient in the RCS to a maximun of 2328 psig, and the pressurizer level increased to'38 percent. The minimum RCS temperature durirq this event was 551 degrees F. We pressurizer Power Operated Relief Valves did not lift l during this transient.

The operators carried out the appropriate steps of procedure EMG E-0, " Safety l Injection", and when steady state conditions were reached the appropriate steps of the SI recovery procedure ES-03, "SI Termination", were performed. W e Safety Injection was terminated by approximately 1155 cur.

An Unusual Event was declared and terminated. We appropriate federal, state, and local agencies were notified in accordance with the anergency Plan Implementing Procedures.

We Post Trip Review revealed that steanline pressure never reached the trip setpoint for low steamline pressure, although the indications on steam generators "B" and "C" did show a momentary decrease in pressure from 1070.2 and 1065.8 psig to 746.5 and 925.8 psig respectively. Shortly after this pressure dip, the pressure returned to normal. Although the decrease in stean pressure did not reach the low pressure satpoint, the rate sensitive nature of the signal circuit caused an anticipatory trip. %us, the initiating signal of low steanline pressure was due to the step decrease in steamline pressure.

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Page 3 Subsequent investigations into this event co . firmed that the step decrease in the steam pressure signal was caused by interftence from an operator's ham held radio transmission. An operator was standing ia the area of the steamline pressure transmitters aM had keyed his radio just prior to the initiation of this event.

This scenario has been re-enacted with the result being an identical response. At the time of re-enactment, the plant was below the P-ll interlock point, and no actuation of ESP equipnent occurred, but the required logic for a low steanline pressure signal was induced.

As a result of this event, the use of radios within the plant was severely restricted and more stringently controlled.

We third ECCS subsystem actuation occurred on May 6,1985, and is discussed in Licensee Event Report 85-027-00, which was transmitted via KMINRC 85-145, dated May 31, 1985. %is actuation was also initiated by a low steanline pressure signal.

At the time of this event, the plant was in Mode 3, Hot StaMby, prior to initial criticality, and hot, no-flow control rod drop testing on Control Bank "B" was in progress. The Reactor Coolant Pumps (RCPs) and Main Steamline Isolation Valves had been secured to support this testing, aM the average temperature of the RCS was approximately 530 degrees F. The RCS pressure was approximately 2241 psig. The pressurizer level was being controlled manually at approximately 23 percent and pressure was being controlled autanatically. Steam Generators "A" and "C" were being slowly fed via the Main Feedwater Bypass Valves to adjust level. With no significant heat transfer to the Steam Generators fran the RCS, the Mdition of feedwater resulted in cooling the Steam Generators and decreasing the steamline pressure to the trip setpoint for low steamline pressure (615 psig), aM the Safety Injection and Main Steamline Isolation signals occurred.

An Unusual Event was declared aM subsequently terminated. The appropriate federal, state, and local agencies were notified in accordance with the Dnergency Plan Implementing Procedures.

All ESF equignent responded properly. The RCS pressure transient was limited to approximately 2340 psig by the Pressurizer Power Operated Relief Valves.

Pressurizer level increased to 56 percent during this event, and the lowest temperature in the RCS was approximately 500 degrees F.

We Safety Injection was terminated in accordance with plant procedures EMG E-0,

" Safety Injection", and EMG ES-03, "SI Termination", at approximately 1243 CI7r.

The circumstances which led to this event have been discussed with the operating personnel in shift briefings and crew meetings stressing operator awareness of plant status, and particularly early recognition of developing trends. In addition, since the plant conditions allowing no RCS flow through the Steam Generators (minimum or no decay heat present) will only reoccur after subsequent refuelings, the information pertaining to this event has been Mded to a Post-Refueling Action File, maintained by Training, which contains items to be stressed to the operators durire the Requalification Training presented near the time of refueling.

In each of the three actuations at near normal operating temperature and pressure which have occurred, the usage factor for each Safety Injection nozzle was below the 0.70 limit specified by Technical Specification 3.5.2 Action Statement b.

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Page 4 In each instance, the ECCS equipnent performed its intended safety function, no release of radioactivity occurred, ard at no time was there a threat to the health and safety of the public.

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