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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20116B4391996-07-24024 July 1996 Special Rept 96-003:on 960617 Declared Reactor Vessel Level Indicating System B Train Inoperable.Determined Probable Cause to Be within Resistance Temp Detector (Rtd).Tagged RTD out-of-service & Performed Further Troubleshooting ML20107M3571996-04-25025 April 1996 Special Rept 96-002:on 960327,RCS Pressure Exceeded Setpoint of 445 Psig for PORV 455A When Cooler,Denser Water,In Vessel Warmed & Expanded,But Did Not Approach TS Limit of 485 Psig. RCS Pressure Subsequently Stabilized at Approx 335 Psig ML20091L0931995-08-22022 August 1995 Special Rept 95-002:on 950727,valid Failure of EDG B Occurred.Util Believes Overspeed Plunger Partially Extended & Repositioned Overspeed Trip Lever.Adjusted Governor to Reduce Max Frequency Experienced by EDG B During Startup ML20086B8271995-06-28028 June 1995 Special Rept 95-001:on 950531,output Breaker for B EDG Tripped During Performance of Routine Monthly Testing.Ega Replaced & EDG B Was Evaluated & Determined to Be Operable ML20078B9401994-10-21021 October 1994 Special Rept 94-003,providing Info Re Number of Tubes Plugged in Each SG as Required by TS 4.4.5.5 ML20071L5211994-07-29029 July 1994 Special Rept 94-002:on 940701 & 08,reported to CR That Net Refill Vols of Sheathing Filler Matl Exceeded 5 Percent of Net Duct Vol for Tendons V39 & 25CB.Voids Filled by Addl Grease Pumped Into Tendon Ducts ML20070N7031994-05-0303 May 1994 Special Rept 94-001:on 940329,seismic Monitoring Channel Declared Inoperable Due to Location on Exterior Reactor Cavity West Wall within Biological Shield Wall.Entire Accelermeter Package to Be Replaced ML20127G2021993-01-12012 January 1993 Special Rept 93-001:on 921229,10-60 Meter Elevation Delta Temp Indication for Meteorological Tower Declared Inoperable Due to Erratic Indications.Ice Shields Installed to Minimize Recurrence ML20101P9731992-07-0808 July 1992 Special Rept 92-002:on 920608,valid Failure of EDG B Occurred Due to Failure to Temp Control Valve.Caused by Failure of Two Out of Three Power Pills.Power Pills Replaced & EDG Testing Frequency Increased ML20097A2831992-05-29029 May 1992 Special Rept 91-007,reporting Results of Fourth SG Tube Inservice Insp Completed by Westinghouse on 911024 of SGs a & C ML20098D6951992-05-26026 May 1992 Special Rept 92-001:on 920422,invalid Failure of EDG a Occurred When Output Breaker Tripped on Reverse Power.Caused by Megawatt Meter Used to Load EDG Reading 0.2 MW W/Edg in Standby.Meters Rezeroed to Ensure Proper Load Applied ML20086P8301991-12-20020 December 1991 Special Rept 91-006:on 911121,operators Depressed Test Button to Energize Relay K615 But EDG a Would Not Start. Caused by Incomplete Description of Initial Conditions in Surveillance Procedure.Statement Added to Procedure ML20086L8151991-12-12012 December 1991 Special Rept 91-005:on 911112,invalid Failure of Emergency Diesel Generator B Occurred During Train a Safeguards Actuation Test.Caused by Binding of Temporary Test Flag in Alternate Supply Breaker Cubicle.Test Flags Modified ML20079L9871991-11-0101 November 1991 Special Rept 91-004:all Inconel 600 Mechanical Tube Plugs in Steam Generators a & C Removed During Fourth Steam Generator Inservice Insp from 911016-24.Tubes Replugged W/Inconel 690 Except for Tubes R28C56 & R28C76 in Steam Generator C ML20082U0911991-09-16016 September 1991 Special Rept 91-003:on 910819,invalid Failure of EDG B. Caused by Unit Parallel Relay.Hermetically Sealed Relay Being Evaluated as Means to Prevent Similar Failures of Relay ML20070U0031991-04-0202 April 1991 Special Rept 91-002:on 910304,invalid Failure of Emergency Diesel Generator a Occurred.Caused by Failure of Operator to Verify That Correct Switch Adjusted Before Adding Load to Diesel Generator.Operator Counseled ML20155J1691988-10-17017 October 1988 Suppl 1 to Special Rept 85-011 Re Inoperable Loose Part Detection Sys Channel.On 850912,Channel 10 of Loose Part Detection Sys Declared Inoperable.Caused by Faulty Preamplifier Charge Converter.Converter Replaced ML20154M0571988-05-27027 May 1988 Special Rept 87-015-01:on 871211,failure of Emergency Diesel Generator a Occurred When Cracked Lube Oil Line Fitting Caused Excessive Leakage.Procedure Initiated That Will Require Use of Vendor Recommended Heavier Grade Oil ML20154M0181988-05-27027 May 1988 Special Rept 87-016-01:on 871219,diesel Generator B Failed When Generator Could Not Be Synchronized to Bus.Caused by Potential Transformer Fuse Knives Not Inserting Fully Into Fuse Stabs.Insp Windows on Each Cubicle Recommended ML20148A4081988-01-14014 January 1988 Special Rept 87-016:on 871219,failure of Emergency Diesel Generator B Occurred When Generator Not Synchronized W/Bus. Caused by Repeated Opening & Closing of roll-out Potential Transformer.Engineering Evaluation in Progress ML20147C1741988-01-0808 January 1988 Special Rept 87-015:on 871211,failure of Emergency Diesel Generator a Occurred Due to Excessive Leakage.Caused by Cracked Lube Oil Line Fitting.Fitting Replaced & Retested for Leakage.Cause of Cracking Not Determined ML20149F8141988-01-0707 January 1988 Special Rept 87-013:on 871109,discovered Low Level Radioactive Matl Delivered to Coffey County Land Fill.Caused by Nonlicensed Util Personnel Error.Procedure for Release of Radioactive Matl Revised ML20238C7871987-12-24024 December 1987 Special Rept 87-10,Suppl 2:voids in Tendon Sheathing Attributed to Listed Additive Factors,Quality Program Described,Grease Installation & Insp Discussed & Audits & Surveillance of Const Operations Conducted ML20237E6311987-12-18018 December 1987 Special Rept 87-014:on 871014,hydrogen Pressurizer Ignited. Caused by Inadequate Pressurizer Draining & Depressurizing Procedure.Procedure Review & Rev & Control Room Personnel Training Planned ML20195K3281987-11-16016 November 1987 Reportable Event 10691:on 871116,trash Bag Containing Low Level Contamination Found During Survey of Coffee County Landfill as Followup to Reportable Event 10646.Contaminated Rag Returned to Plant.Survey Continuing ML20195K3171987-11-11011 November 1987 Reportable Event 10646:on 871109,discovered That Low Level Radioactive Sheets of Metal Removed from Site & Delivered to Coffee County Landfill.All But Three Pieces Recovered.Search for Remaining Pieces Continuing ML20235K4511987-09-28028 September 1987 Suppl 1 to Special Rept 87-10:third Yr Tendon Surveillance on 870801-0914 Indicated That Net Refill Vols of Sheathing Filler Grease Exceeded 5% of Net Duct Vol for Tendons. Investigation Being Performed to Determine Causes of Voids ML20238F7771987-09-11011 September 1987 Special Rept 87-010:inservice Tendon Surveillance Voids in Excess of 5% of Net Duct Vol Discovered.Cause Not Stated. Prevention of Tendon Corrosion Assured by Adequately Coating Tendon Wires & Anchorage ML20214U0691987-06-0505 June 1987 Special Rept 87-006:on 870429,seismic Monitoring Instrumentation Channel Declared Inoperable & Remained Out of Svc for More than 30 Days.Caused by Faulty Voltage Regulating Printed Circuit Board.Board Will Be Replaced ML20207E8721986-12-24024 December 1986 Special Rept 86-011:on 861201,failure of Emergency Diesel Generator a Occurred.Caused by Faulty Speed Switch.Switch Replaced.Faulty Switch Returned to Vendor for Failure Analysis & Repair ML20212D9601986-12-22022 December 1986 Suppl 1 to Special Rept 85-010:on 851001,two Failures of Diesel Generator a Occurred.Caused by Mild Fluctuations in Engine Speed & Output Breaker Trip on Reverse Power.Oil Added to Correct Fluctuations ML20214K2831986-11-18018 November 1986 Special Rept 86-005:on 861018,19 & 31,ESF Switchgear Rooms I & II Exceeded Max Temp Limit Specified in Tech Specs. Caused by Inoperability of Cooling Unit ML20198E4531986-05-12012 May 1986 Special Rept 86-002:on 860412,invalid Failure of Emergency Diesel Generator B Occurred During Surveillance Procedure STS KJ-001B.Caused by Malfunctioning Unit Parallel Relay. Relay Replaced ML20154N3591986-03-0606 March 1986 Special Rept 86-001:on 860127,net Refill Vols of Sheathing Filler Grease Exceeded 5% of Net Duct Vol for Listed Tendons.Caused by Physical Characteristics of Sheathing Filler Matl & Industry Std Installation Techniques ML20140D2741986-01-14014 January 1986 Special Rept 85-015:on 851215,diesel Generator B Output Breaker Tripped on Reserve Power.Caused by Operator Error. Operator Reclosed Output Breaker & Successfully Paralleled & Loaded Unit ML20138P1731985-12-0909 December 1985 Special Rept 85-014:on 851029,Channel 8 of loose-part Detection Sys Declared Inoperable.Cause Believed to Be in Either Charge Converter or Accelerometer.Investigations Underway ML20136G0331985-11-0101 November 1985 Special Rept 85-012:on 851003,invalid Failure of Diesel Generator B Occurred.Possibly Caused by Vent Petcocks Vibrating Open.Precautions Added to Procedures STS KJ-005B & STS KJ-005A to Ensure Petcocks Fully Closed ML20136C7651985-10-31031 October 1985 Special Rept 85-010:on 851001,two Failures of Diesel Generator a Occurred.Caused by Closed Governor Needle Valve. Valve Opened Slightly & Procedure Sys KJ-121, Diesel Generator NE01 & NE02 Lineup for Automatic... Revised ML20198B2731985-10-22022 October 1985 Special Rept 85-011:on 850912,Channel 10 of Loose Part Detection Sys Declared Inoperable During Surveillance Procedure.Investigation Conducted to Discover Root Cause & Plans for Restoring Inoperable Channel to Svc ML20133G7531985-07-16016 July 1985 Special Rept 85-009:on 850428,30 & 0506,ECCS Actuations Occurred.Caused by Personnel Error & Rate Sensitive Nature of Circuitry.Emphasis Being Placed on Rate Sensitive Nature of Circuitry During Requalification & Hot License Training ML20129A4011985-06-28028 June 1985 Special Rept 85-006:on 850601,during Periodic Surveillance Testing of Diesel Generator A,Generator Secured Prematurely Due to Erratic Low Jacket Water Pressure Indication & Alarm. Caused by Use of Valve Lineup to Test Starting Air Sys ML20140F4381985-06-24024 June 1985 Special Rept 85-008:on 850415,containment Base Slab Seismic Monitor Declared Inoperable Due to Failed Power Supply.Cause Unknown.New Power Supply Ordered.Temporary Power Supply Installed ML20127N4841985-06-10010 June 1985 Special Rept 85-007 Re Positive Moderator Temp Coefficient for Withdrawn Control Rods.Hot Zero Thermal Power Condition within Tech Spec 3.1.1.3a Limit.Control Rod Withdrawal Limits Incorporated Into Operating Procedures ML20126J2921985-05-30030 May 1985 Special Rept 85-005:on 850502,invalid Failure of Diesel Generator a Occurred Due to Personnel Oversight in Restoring Diesel to Svc After Planned Outage.On 850501,diesel Generator a Taken Out of Svc for Insp of Welds ML20128E6631985-05-17017 May 1985 Special Rept 85-004:on 850419,invalid Failure of Diesel Generator Occurred.Caused by Operating Error.Rept Will Be Added to Operations Required Reading to Emphasize Importance of Close Adherence to Procedural Steps ML20128B6281985-05-0909 May 1985 Special Rept 85-003:on 850409,black Smoke Observed Coming from Manifold of Diesel Generator B When Generator Started After Hot Web Deflection.Caused by Failure to Close Cylinder Petcocks.Petcocks Closed ML20117G0411985-05-0101 May 1985 Special Rept 85-002:on 850401,during Periodic Testing,Diesel Generator a Failed Due to Restrictive Acceptance Criteria & Personnel Error.Procedure STS KJ-0054A Revised & Personnel Instructed on Importance of Following Procedures ML20117G1621985-04-29029 April 1985 Special Rept 85-001:on 850330,invalid Failure of Diesel Generator A,NE01,occurred.Caused by Personnel Oversight Resulting in Inadequate Venting of Fuel Oil Lines After Maint.Work Request Procedure Revised 1998-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
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W$LF CREEK NUCLEAR OPERATING CORPORATION Neil S. " Bun" Carns Chairman, President and Chief Emecutwo Officer Augu5t 22, 1995 WM 95-0124 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station P1-1 37 Washington, D. C. 20555
Subject:
Docket No. 50-482: Special Report 95-002 Gentlemen The attached Special Report is being suomitted in accordance with Wolf Creek Generating Station Technical Specification 4.8.1.1.3 concerning a valid failure of Emergency Diesel Generator "B" and an invalid failure of Emergency Diesel Generator "B."
If you should have any questions regarding this response, please contact me at (316) 364-8831, extension 4000, or Mr. William M. Lindsay at extension 8760.
Very truly yours,
~
. W Neil S. Carns NSC/jad Attachment cc: L. J. Callan (NRC), w/a D. F. Kirsch (NRC), w/a J. F. Ringwald (NRC), w/a J. C. Stone (NRC), w/a 9508280295 950822 PDR ADOCK 05000482 S PDR PO. Box 411/ Burlington, KS 66839 / Phone: (316) 364-8831 l j
An Equal opportunity Employer M T/HC/ VET l
- 9. .
o 18 Attcchment to WM 95-0124
-page 1 of 4 I i
, Special Report 95-002 (Part 1) '
Valid Failure of "--raaney Diasal n===rator *B" This report describes a valid failure of Emergency Diesel Generator (EDG) "B" -
which occurred on July 27, 1995. This report is being submitted in accordance ,
with Wolf Creek Generating Station (WCGS) Technical Specification 4.8.1.1.3. ,
Background Tnformations On June .28, 1995, Wolf Creek Nuclear Operating Corporation (WCNOC) ~ issued '
Special Report 95-001, by letter Irr 95-0064. .This letter documented an Jinvalid failure of EDG "B." Corrective actions for this event included replacement of the EDG "B" Governor. ,
'At the time of this event the "A" EDG was administratively declared inoperable
- to maximize personnel safety during the replacement of its lube oil. keepwarm pump. WCGS had conservatively entered Technical Specification Action Statement 3. 8.1.1 (a) . t Technical Specification Action Statement 3 . 8 .1.1 (a) defines the actions WCGS must implement when one EDG is inoperable, Technical Specification Action Statement 3. 8.1.1 (b) defines the actions WCGS i must implement when two EDGs are inoperable.
i Description of Events:
On July 27, 1995, at approximately 2121 hours0.0245 days <br />0.589 hours <br />0.00351 weeks <br />8.070405e-4 months <br /> CDT, WCGS performed Surveillance Test STS KJ-005B, Revision 22, " Manual / Auto Start, Synchronization & Loading Of Emergency D/G NE02." This test was performed to demonstrate operability of Emergency Diesel Generator "B," in accordance with the testing requirements specified in the Wolf Creek Generating Station Technical Specifications. This !
test' implements a fast start and load of the EDG "B". ;
During the performance of this test, the unit experienced an initial frequency peak of about 64 cycles before stabilizing at 60 cycles. Upon completion of the test, the EDG "B" was shutdown in accordance with the guidance contained in STS.KJ-005B. During the EDG "B" coast-down, the unit tripped on mechanical overspeed. WCGS declared the unit " Administratively" inoperable at 2132 hours0.0247 days <br />0.592 hours <br />0.00353 weeks <br />8.11226e-4 months <br /> CDT on July 27, 1995, entered WCGS Technical Specification Action Statement ,
3.8.1.1(b), and began an investigation to determine the cause of the EDG's trip. Both EDGs remained simultaneously inoperable for approximately 4.8 ,
. hours. WCGS declared an unusual event at 2211 hours0.0256 days <br />0.614 hours <br />0.00366 weeks <br />8.412855e-4 months <br /> CDT, on July 27, 1995, and notified the NRC at 2308 hours0.0267 days <br />0.641 hours <br />0.00382 weeks <br />8.78194e-4 months <br /> CDT, on July 27, 1995.
( ,At approximately 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> CDT, on July 28, 1995, WCGS started the "A" EDG to warm the unit and thus restore the lube oil to the required temperature band. ,
Subsequently WCGS declared the "A" EDG operable, on July 28, 1995, at 0218 !
hoursfCDT, and WCGS Technical Specification Action Statement 3.8.1.1(b) was l exited and Technical Specification Action Statement 3. 8.1.1 (a) , was entered j
- due to the inoperability of the EDG "B". ;
l 5
l
l
Tbisevent occurred while the EDG "B" was in the standby mode. The EDG "B" f was administratively inoperable for approximately 70 hours8.101852e-4 days <br />0.0194 hours <br />1.157407e-4 weeks <br />2.6635e-5 months <br />, of which it was ;
available for use and would have functioned correctly in an emergency for all but 20 of the 70 hours8.101852e-4 days <br />0.0194 hours <br />1.157407e-4 weeks <br />2.6635e-5 months <br />. During the 20 hour2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> time period the unit. was tagged ,
out to facilitate replacement of the mechanical overspeed trip mechanism. t Root cause mad Corrective Actions !
Root ("luse r WCGS believes that when the EDG *B" frequency peaked at approximately .64 ,
cycles, during startup of the EDG "B", the mechanical overspeed plunger l partially extended and repositioned the overspeed trip lever. The movement of j the overspeed trip level was not enough to result in an immediate trip of the
- EDG "B". However it is believed that, during the coast down process, the overspeed trip lever vibrated into the full trip position resulting in a ;
mechanical trip signal.
Immediate Corrective Actions i
The unit was tested in an effort to determine the exact cause of the trip.
This troubleshooting determined that the most likely cause of the mechanical overspeed trip was the overspeed trip lever, which had been repositioned during the EDG "B" startup, and vibrated into the " Tripped" position.
WCGS performed an evaluation and determined that this failure could have f adversely affected the function of the EDG "B" when in the isochronous (emergency) mode.
To prevent recurrence of this action, WCGS adjusted the governor to reduce the maximum frequency experienced by the EDG "B" during startup to 62 cycles.
WCGS has determined that this frequency is sufficiently low enough to prevent the overspeed trip switch from being repcsitioned during the initial startup of the EDG "B", and the subsequent vibration of the overspeed trip switch into the " Tripped" positioned.
Future Corrective Actioni The above discussed action has been determined to be appropriate to prevent recurrence of this problem. ;
Failure Classification ,
In the event of an emergency, EDG "B" would have started and supplied power to [
its emergency bus as required. The repositioned overspeed trip switch could have prevented the EDG "B" from assuming the necessary emergency house loads.
Therefore, this failure is classified as an valid failure in accordance with Position C.2.e (2) , Regulatory Guide 1.108, Revision 1. ;
i
(;
.- special Report 95-002 (Part 2)-
' Invalid Failure of *-roancy Dianal annarator *B"
-This report describes an invalid failure of Emergency Diesel Generator (EDG) ,
Descrintion of Eventar On August 3, 1995, at approximately 0905 hours0.0105 days <br />0.251 hours <br />0.0015 weeks <br />3.443525e-4 months <br /> CDT, the "B" emergency diesel {
generator was started in accordance with Surveillance Test Procedure STS KJ-005B, Revision 22, ' Manual /-Auto Start, Synchronization & Loading Of Emergency l D/G NE02." This . test was performed to meet monthly testing requirements specified in the WCGS Technical Specifications. The emergency diesel l generator was successfully started and loaded. The "B" emergency diesel !
generator operated normally for approximately 27 minutes. At 0932 hours0.0108 days <br />0.259 hours <br />0.00154 weeks <br />3.54626e-4 months <br /> CDT,. ;
on August 3, 1995, a "Hi Lube Oil Sump Level" Alarm was received. The l validity of the alarm was evaluated by Operations and System Engineering personnel. At 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> CDT, the "B" emergency diesel generator was secured, :
j the unit was declared 4noperable, and WCGS entered Technical Specification Action Statement 3.8.1.. s).
WCGS personnel immediately began an investigation into the cause of the high lube oil sump level. This investigation determined that lube oil, contained in the lube oil makeup tank, was leaking past the automatic lube oil makeup valve. This leakage resulted in the emergency diesel generator lube oil sump level increase and caused the lube oil sump high level alarm to actuate. WCGS ,
manually isolated the automatic makeup valve and returned the emergency diesel generator lube oil sump to the correct level. The emergency diesel generator I was retested and demonstrated operable at approximately 0439 hours0.00508 days <br />0.122 hours <br />7.258598e-4 weeks <br />1.670395e-4 months <br />, on August j 4, 1995.
l This event occurred during routine testing, as required by the WCGS Technical Specification 4 . 8 .1.1. 2 ( f ) . The EDG *B" was unavailable for approximately j 28.5' hours. During this time period, the cause of the problem was determined i and corrected. I Root canna and Corrective Actiona l
. Jtoot Caune:
l WCGS determined that oil, contained in the lube oil makeup tank, was leaking l past the automatic lube oil makeup valve. This leakage resulted in the level l in the emergency diesel ' generator lube oil sump increasing to the high level alarm setpoint. i l
l
.-*- Attechment to WM 95-0124 Pega 4'of 4
-Immad'inte corrective Action WCGS secured the "B" emergency diesel generator and declared it inoperable until the lube oil sump level could be returned to the manufacturer's specified level.
WCGS manually isolated the automatic lube oil makeup va;ve and returned the emergency diesel' generator lube oil sump to the correct level. The automatic lube oil makeup valve will remain isolated until repairs can be effected.
This action was determined to be acceptable, based on the ability of the EDG "B" to operate continuously for a minimum of 10 days without the addition of-oil, as discussed below.
Future corrective Actions The above discussed corrective actions are adequate to prevent recurrence of ,
this problem. WCGS will repair the automatic lube oil makeup valve during a l future emergency diesel generator outage. The oil contained in the lube oil ;
. storage tank is not necessary because the capacity of the engine lube oil sump l provides a sufficient volume of oil, so that the engine can operate at the nameplate continuous rating for at least seven days without replenishing the oil in the sump. When operating at nameplate continuous rating, engine oil ,
consumption is approximately 60 gallons per day. At full capacity, the engine l oil sump contains 1200 gallons of oil. The engine sump is considered empty at !
300 gallons. This provides 900 gallons of oil that can be consumed which represents between 14 and 15 days ci continuous operation without replenishment. At the low sump level alarm point, there is approximately 963 1 gallons in the sump which provides 663 gallons of consumable oil or approximately 11 days continuous operation without replenishment. If !
continuous operation starts when the oil level was at the add oil level (approximately 948 gallons), there is 648 gallons of consumable oil which represents a 10 day supply.
Failura Classificationt In the event of an emergency, EDG "B" would have started and supplied power to its emergency bus as required. The high level in the sump and the subsequent isolation of the automatic makeup valve would not have prevented the emergency diesel generator from ptrforming its designed function. Therefore, this failure is classified ca an invalid failure in accordance with Position C.2.e (2 ) , Regulatory Guide 1.108, Revision 1.
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