05000416/LER-1983-190, Updated LER 83-190/03X-1:on 831214,Div 2 Isolation Occurred, Causing Loss of Shutdown Cooling When Pump Suction Valve F009 Isolated.Caused by Temporary Outage Restoration Procedure Error.Procedure retired.W/840321 Ltr

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Updated LER 83-190/03X-1:on 831214,Div 2 Isolation Occurred, Causing Loss of Shutdown Cooling When Pump Suction Valve F009 Isolated.Caused by Temporary Outage Restoration Procedure Error.Procedure retired.W/840321 Ltr
ML20087M627
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 03/21/1984
From: Dale L, Parker J
MISSISSIPPI POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
AECM-84-0167, AECM-84-167, LER-83-190-03X, LER-83-190-3X, NUDOCS 8403300118
Download: ML20087M627 (3)


LER-2083-190, Updated LER 83-190/03X-1:on 831214,Div 2 Isolation Occurred, Causing Loss of Shutdown Cooling When Pump Suction Valve F009 Isolated.Caused by Temporary Outage Restoration Procedure Error.Procedure retired.W/840321 Ltr
Event date:
Report date:
4162083190R00 - NRC Website

text

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Fl MAR 26 A10 : March198421,9 NUCLE AM PRODUCTION DEPARTMENT U.S. Nuclear Regulatory Commission Region 11 101 Marietta St., N.W., Suite 2900 Atlanta, Georgia 30303 Attention: Mr. J. p. O'Reilly, Regional Administrator

Dear Mr. O'Reilly:

SUBJECT:

Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 License No. NPF-13 File: 0260/L-835.0 Update Report - Division 2 Isolation Causes Loss of Shutdown Cooling LER 83-190/03 X-1 AECM-84/0167 This letter submits an update to a previous report submitted on January 13, 1984. The event for which the report was submitted occurred on December 14, 1983, while restoring Division 2 power following a planned maintenance outage, when a Division 2 isolation occurred causing a loss of Shutdown Cooling when pump suction valve F009 isolated. Other actuations included Reactor Water Cleanup isolation and Standby Cas Treatment B initiation. A Limiting Condition for Operation was entered pursuant to Technical Specification 3.4.9.2. The event was reported pursuant to Technical Specification 6.9.1.13.b.

Our investigation into the cause of the event and corrective action to prevent recurrence is complete. Attached is LER 83-190/03 X-1 which is a final report.

Yours truly.

Y trt L. F. Dale Manager of Nuclear Services EBS/SHH:rg Attachment cc: See next page OFFICIAL COPY- i

__ g dp Member Middle South Utilities System

. AECM-84/0167

'~ ** 8 MISSISSIPPI POWER O L12HT COMPANY cc: Mr. J. B. Richard (w/a)

Mr. R. B. McGehee (w/o)

Mr. T. B. Conner (w/o)

Mr. C. B. Taylor (w/o)

Mr. Richard C. DeYoung, Director (w/a)

Office of Inspection & Enforcement U. S. Nuclear Reguintory Commission Washington, D. C. 20555 Document Control Desk (w/a)

U. S. Nuclear Regulatory Commission Washington, D. C. 20555 1