/03L-0 on 781018:isolation Valve V-7-31 Had Damaged Rubber Seat & Drain Valve V-7-29 Obstructed by Piece of Cork & Filter F-1-58 Medium Disintegrated.Cause of V-7-31 & F-7-58 Degradations Due to Detonations in SysML20064F069 |
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Site: |
Oyster Creek |
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Issue date: |
11/16/1978 |
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From: |
Ross D JERSEY CENTRAL POWER & LIGHT CO. |
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To: |
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Shared Package |
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ML20064F067 |
List: |
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References |
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LER-78-024-03L, LER-78-24-3L, NUDOCS 7811280196 |
Download: ML20064F069 (3) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000219/LER-1990-0081990-07-23023 July 1990 LER 90-008-00:on 900625,reactor Scram Occurred on Low Condenser Vacuum.Caused by Failure of Backwash Outlet Valve to Open,Causing Loss of Circulating Water to Condenser A. Plant Stabilized & Taken to Cold shutdown.W/900723 Ltr 05000219/LER-1984-020, Errata to LER 84-020-01,consisting of Page 4 Re Corrective Actions.Preventive Maint Request Initiated to Store Overload Devices in Vertical Position1985-09-23023 September 1985 Errata to LER 84-020-01,consisting of Page 4 Re Corrective Actions.Preventive Maint Request Initiated to Store Overload Devices in Vertical Position 05000219/LER-1982-0261982-06-0707 June 1982 LER 82-026/03L-0:on 820507,thermocouple for Safety Valve NR28J Found Open During Surveillance Testing.Caused by Broken Lead Wire at Thermocouple.One of Adjacent Valve Acoustic Monitor Setpoints Reduced.Thermocouple Replaced 05000219/LER-1981-061, Updated LER 81-061/03X-1:on 811223,of 11 Deficient Hydraulic Snubbers,Nine Found to Be Inoperable During Functional Testing.Caused by Seal Degradation &/Or Worn Poppet Valves. Snubbers Replaced W/Operable Spares1982-05-25025 May 1982 Updated LER 81-061/03X-1:on 811223,of 11 Deficient Hydraulic Snubbers,Nine Found to Be Inoperable During Functional Testing.Caused by Seal Degradation &/Or Worn Poppet Valves. Snubbers Replaced W/Operable Spares ML20064J2011978-12-22022 December 1978 /03L-0 on 781126:during Testing Containment Spray Pumps 51C & 51A Failed to Start on Signal Due to Excess Friction in Circuit Breaker Trip Bar Bearings.Bearings Were Cleaned & Lubricated ML20147H5331978-12-21021 December 1978 /03L-0 on 781125:switch RE03C Was Found to Trip at Pressure Less conservative(1075 Psig)Than Specified in Tech Specs 2.3.3.Cause of Pressure Switch Tripping Is Attributed to Sensor Repeatability ML20064H3441978-12-14014 December 1978 /01T-0 on 781129:during Test,Noted That Containment Leakage Rate Greater than Allowable.Discovered That Vent Valves Were Leaking.Caused by Leakage Past the Seating Surfaces ML20064H1871978-12-13013 December 1978 /01T-0 on 781129:during Test,Main Steam Line Drain Valve V-1-106 Did Not Close 2 Incore Probes,Did Not Fully W/Draw & Reactor Coolant Valve Did Not Indicate Closed.Due to Jammed Armature,Faulty Fuse Holder & Incorrect Settings ML20064F0691978-11-16016 November 1978 /03L-0 on 781018:isolation Valve V-7-31 Had Damaged Rubber Seat & Drain Valve V-7-29 Obstructed by Piece of Cork & Filter F-1-58 Medium Disintegrated.Cause of V-7-31 & F-7-58 Degradations Due to Detonations in Sys ML20064E7071978-11-15015 November 1978 /03L-0 on 781019:IRM 12 Became Inoperative While Cable to IRM 14 Was Disconnected.Irm 12 Failure Attributed to Maint Activities Under Vessel.Subesquent Inspec Showed IRM 12 Cable Damaged ML20064E5561978-11-15015 November 1978 /03L-0 on 781017:during Routine Surveillance Test of Standby Gas Treatment Sys,The Sys II Discharge Valve Failed to Open,Due to Stuck Solenoid in Control Air Supply to Operator for V-28-30 ML20064C2501978-10-12012 October 1978 /03L-0:on 780914,circuit Breaker for motor- Operated Valve Tripped When Valve Closed by Isolation Signal.Caused by Component Failure Allowing Switch Setting to Shift.Setting Corrected & Set Screw Tightened ML20064B7391978-09-29029 September 1978 /01T-0 on 780916:3 MSIVs(NS03A,NS04A,NS04B) Had Leakage Rates in Excess of Maximum Allowable Due to Stem Packing,Cracked Stellite Weld & Failure of Main Poppet to Seat Properly.Msiv Failures Being Investigated 1990-07-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
Text
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7 8 61 ET NUVS E R 69 REPORT DATE EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 l While performing maintenance on the Off Gas System to satisfy a commit- l l o 13 ] I ment made in R.O. No. 50-219/77-21, it was discovered that isolation !
l o 141 I valve V-7-31 had a damaged rubber seat which affected its capability to l 10151 I seal, and drain valve V-7-29 was obstructed by a piece of cork like ma- l 1016 I I terial which most_likely was in the pipe from plant const ruct ion. In I l o 17 l l addition. the absolute filter F-1-58 medium was found disintegrated. l 8F . 9 I
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35 36 31 40 41 42 43 44 47 CAusE DESCRIPTION AND CORRECTIVE ACTIONS h l i 101 l The cause of the V-7-31 and F-1-58 dearadations is attributed to the 1 li li j l detonations that occurred in the system during operation of the AuOment- l ed Off Gas System. A new seat was installed in V-7-31 and the blockage
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Iil3l l was removed from V-7-29 Both valves were cleaned, lubricated, tested, l
[ i 14 l l and reinstalled. A new absolute filter cartridge was installed in F-1-58. I 7 8 9 80 ST % POWER OTHER STATUS DISCO RY Of SCOVERY DESCRIPTION 32 1119 l l H Ih l0 l010 ]@l NA l l A l@l Routine Maintenance Activities l 0
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(201)4554200 OYSTER CREEK NUCLEAR GENERATING STATION
- Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/78-24/3L-0 Report Date November 16, 1978 Occurrence Date October 18, 1978 4 .
Identification of Occurrence Degradation of the Off Gas System capability to properly isolate and filter the gaseous effluent from the plant. As a result, the radioactive off gases could not have been fully contained in the off gas piping. This event is considered to be a reportable occurrence as defined in the T-chnical Specifi-cat ions, paragraph 6.9.2.b. (4) .
Conditions Prior to Occurrence The plant was shut down for a scheduled refueling / maintenance outage.
Reactor subcritical.
Reactor mode switch locked in refuel.
All control rods fully inserted, i Source range monitors <40 cps. ,
Cavity flooded.
Reactor coolant 93*F.
Description of Occurrence During the period of October 18, 1978, through October 24, 1978, while per-forming maintenance on the Off Gas System, it was discovered that:
(1) The off gas isolation valve V-7-31 had a damaged rubber seat which affected the capability of the valve to obtain a leak tight seal.
Signs of discoloration and " wire drawing" type damage were observed.
A new seat ring was Installed in V-7-31.
(2) The off gas drain valve V-7-29 was found obstructed with a piece of cork type material which most likely was in the pipe as a result of plant construction. This obstruction prevented the full closure of I
the valve. The blockage was removed from V-7-29.
Both valves V-7-31 and V-7-29 were cleaned, lubricated, tested and reinstalled.
Jersey Central Power & Light Company rs a Member of the General Pub'. Utilit es System
1 f- s :
Reportable Occurrence No. 50-219/78-24/3L-0 Page 2 November 16, 1978 All (3) The off gas abolute filter F-1-58 medium was found disintegrated.
that remained of the filter material was a small layer of ashes in the filter housing. A new absolute filter cartridge was installed in F-1-58. .
Apparent Cause of Occurrence The cause of the V-7-31 and F-1-58 degradations are attributed to the detonations that occurred in the system as a result of the Augmented Off Gas System oper-ation. The first detonation occurred at 4:40 p.m. on August 9, 1977; the second occurred at 2:03 a.m. on March 17, 1978. The cause of the V-7-29 obstruction is attributed to maisrlal lef t in the pipe during the construction phase of the plant.
Analysis of Occurrence The safety significance of this event is considered to be minimal. Signals which would call for the automatic closure of these two valves, namely high radiation in the main steam line or high radiation in the air ejector off gas, have not been r'eceived during the time interval between the first det-onation and the discovery of damage. The quantity of off gas leaking past V-7-31, in the event of an isolation, would have been considerably less than that released during normal operations. The failure of V-7-29 to close would result in leakage of off gas into the vicinity of the 1-12 sump. An~ explosive gas monitor is installed at this sump and would instantly alarm such leakage.
Also, the atmosphere in this sump area is processed through the radwaste ventilation system, whereby, it passes through roughing and absolute filters prior to exhausting to the stack which is monitored. Stack particulate samples, which are obtained and analyzed twice weekly, Indicate that the filter damage occurred in the detonation on August 3, 1977 Although the
- subsequent stack particulate release rate increased an order of magnitude
( over that observed during normal operation, no violations of release limits resulted from the damage to F-1-58.
Corrective Action At present, modifications are being incorporated into the new Augmented Off Gas System which will include a hydraulic flane arrester.. These changes, a result of an investigation into the cause of the detonations, are hoped to be effective in precluding future malfunctions in this system.
Failure Data Previous Reportable Occurrence No. 50-219/77-21/3L, September 23, 1977, (corrective action outlined in that reportable occurrence to disassemble and repair V-7-29 and V-7-31 as appropriate.)
.