ML20045C114

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Insp Repts 50-266/93-09 & 50-301/93-09 on 930401-0524. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint & Surveillance & Emergency Preparedness
ML20045C114
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 06/11/1993
From: Jackiw I
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20045C107 List:
References
50-266-93-09, 50-266-93-9, 50-301-93-09, 50-301-93-9, NUDOCS 9306220091
Download: ML20045C114 (19)


See also: IR 05000266/1993009

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION III

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Report Hos. 50-266/93009(DRP); 50-301/93009(DRP)

Docket Nos. 50-266; 50-301

License No. DPR-24; DPR-27

Licensee: Wisconsin Electric Company

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231 West Michigan

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Milwaukee, WI 53201

Facility Name: Point Beach Units 1 and 2

Inspection At:

Two Rivers, Wisconsin

Dates: April 1 through May 24, 1993

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Inspectors:

K. R. Jury

J. Gadzala

T. Kobetz-

G. F. O'Dwyer

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Approved By:

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I, K. Jac @ , Chief

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Reactor Biojects Section 3A

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inspection Summarv

Jnspection from April 1 throuah May 24, 1993

.(Reports No. 50-266/93009(DRP): No. 50-301/93009(DRP)

Areas Inspected: Routine, unannounced inspection by resident inspectors of

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corrective actions on previous findings;. plant operations; radiological

controls; maintenance and surveillance; emergency preparedness; security;

engineering and technical support; and safety assessment / quality verification.

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Results: A violation of NRC requirements was cited for inadequate corrective

action (Paragraphs 2.d, 5.a, and 6.d) and three non-cited violations were

identified (Paragraphs 4.a and 6.a).

A summary follows.

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Plant Operations

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A pressurizer level instrument bistable failed low resulting in a plant

transient. Operators took prompt and appropriate _ corrective actions, but

management appeared slow in communicating guidance to the control room.

Improperly stowed equipment was identified, presenting potential seismic

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hazards. The repetitive nature of this concern makes it appear .that the plant

inspection program has not been effective.

9306220091 930611-

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During surveillance test performance, a poor operating practice was identified

regarding operator alarm acknowledgement without verification.

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Radioloaical Control

An operator's exemplary actions allowed identification of a highly

contaminated filter prior to its being handled.

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A non cite'd violation was identified for not' posting a high radiation area.

Maintenance / Surveillance

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A step in the master copy of a procedure was found to be already initialed to

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signify completion of that step.

This occurred because of a weakness in the

temporary procedure change process which the licensee was addressing.

As stated in the violation, no condition report was generated to document a

fault that occurred on the fuel oil sump level control switches which caused

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the diesel to be declared inoperable. Despite extensive troubleshooting, this

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fault could not be identified and therefore the switches were left as found

and the diesel was declared operable.

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Two different type oils for a safety injection pump were inadvertently

switched during maintenance, resulting in both pump and motor being filled

with the wrong type oil. During the subsequent return to service test, the

motor bearings failed. However, no determination could be made regarding

whether the failure was due to the incorrect oil or inadequate prelubrication

of the motor bearings during maintenance. This item remains unresolved.

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Good coordination was observed in the conduct of two unrelated surveillance

tests to assure that they did not interfere with each other. . Good

communication was also noted between test personnel and the control operator.

Safety Assessment /0uality Verification

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The licensee instituted corrective actions in response to a determination that

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low temperature overpressure protection setpoints 'were inadequate.

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A non-cited violation was identified for a containment isolation valve not

being included in a leak testing program.

Enforcement discretion was granted for delaying performance of the monthly

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surveillance for Unit 2 reactor protection-instrument functions-due to plant

conditions. This prevented a potential degraded grid voltage condition.

The third door to the Unit I containment personnel _ hatch was found blocked

open.

Implementation of corrective actions for previous violations of this

third door being blocked.open were inadequate to prevent recurrence.

This is

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one of two examples of a violation for inadequate corrective action,

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DETAILS

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1.

Persons Contacted (71707) (30702)

  • G. J. Maxfield, Plant Manager
  • T. J. Koehler, Site Engineering Manager

R. D. Seizert, Training Manager

  • J. F. Becka, Regulatory Services Manager

J. G. Schweitzer, Maintenance Manager

J. C. Reisenbuechler, Manager - Operations

N. L. Hoefert, Manager - Production Planning

J. J. Bevelacqua, Manager - Health Physics

F. P. Hennessy, Manager - Chemistry

J. A. Palmer, Manager - Maintenance

G. R. Sherwood, Manager - Instrument & Controls

W. B. Fromm, Sr. Project Engineer - Plant' Engineering

T. G. Staskal, Sr. Project Engineer - Performance Engineering

W. J. Herrman, Sr. Project Engineer - Construction Engineering

  • F. A. Flentje, Administrative Specialist

Other company employees were also contacted including members of the

technical and engineering staffs, and reactor and auxiliary operators.

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  • Denotes the personnel attending the management exit interview for

summation of preliminary findings.

2.

Corrective Action on-Previous Inspectiou Findinas (92701) (92702)

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a.

(Closed) Violation (266/91025-02: 301/91025-02):

Failure to

Effectively Correct Main Steam Isolation Valve Deficiencies.

This violation, .for which a civil penalty was issued, concerned

ineffective corrective action of past main steam isolation valve

(MSIV) failures. The inspector reviewed the company's response

dated February 5, 1992, and verified that the described actions

regarding changes to correct the problems had been taken.

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Modifications were completed on the MSIVs for~both units to'

improve the reliability of the valve operators. A larger air

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cylinder was installed to increase the amount of closure' force

available to shut the valve. One side of the valve disk pivot

arm was enclosed to allow removal of packing material and thereby

reduce the amount of friction to oppose valve movement. A bellows

assembly was'added over the operator piston rod to prevent' entry

of moisture into the operator. Actions taken to improve MSIV

testing were also reviewed. Operating Procedure OP-13A,

" Secondary Systems Startup" had been revised to eliminate the-

requirement for cycling the.MSIVs prior to operability tests.

.In addition significant additional MSIV testing was included to

provide additional assurance of MSIV operability.

These. actions

were considered adequate and no additional concerns were

identified in this area. This item is closed.

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b.

(Closed) Violation (301/92018-03): One Train of the Containment

Recirculation Mode of Safety Injection Inoperable.

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During the 1991 Unit 2 refueling outage, the licensee installed

modification IWP 88-098 to allow full flow testing of containment

spray, safety injection (SI), and residual heat removal (RHR)

systems as recommended by NUREG 0578.

On September 17, 1992,

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during the subsequent refueling outage, the licensee discovered

that a foam disk wrapped in duct tape had been inadvertently left

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inside this piping during installation of the full flow test

modification. This disk had likely been used as a foreign

material exclusion plug during the modification work.

It had been

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swept out of the piping and lodged in the containment spray pump

impeller during testing. As a result, the piping associated with

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one train of the containment recirculation made of safety

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injection had been rendered inoperable.

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The licensee was cited for this violation and an associated civil

penalty was assessed. As corrective action, the plug was removed

and the system retested. A detailed inspection was then performed

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on the Unit 2 containment spray, RHR, and SI systems to identify

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any additional foreign material in these systems. The inspections

included portions of the systems affected by the modification as

well as piping dead legs and flow restrictions, and were performed

using a combination of boroscopic examinations and radiography.

Only minor amounts of foreign material were found, none of which

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was determined to pose any hazard to the equipment involved.

During the subsequent Unit I refueling outage, a similar

inspection was performed on the Unit I systems affected by this

modification.

No debris was found in any of the piping sections

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examined.

The inspector monitored the licensee's corrective

actions in this area, reviewed the results of the system

inspections, and had no further concerns. This item.is closed.

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c.

L0 pen) Violation (301/92018-04):

Inadequate Ac:eptance Criteria

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for Cleanliness Control.

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The cause of the foreign material exclusion plug, discussed in

paragraph 2.b above, being left inside the containment

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recirculation piping was due to inadequate cleanliness control.

Procedure QAP-105-PB, " Cleanliness Inspection of Fluid Systems and

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Components", Revision 1, did not include appropriate acceptance

criteria to ensure that debris was not left inside the piping.

The licensee was cited for this violation and an associated civil

penalty was assessed.

Corrective actions to prevent recurrence included a revision of

the foreign material exclusion procedure, an' assessment of

contractor controls, and a performance based surveillance of

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activities performed by onsite contractors.

The revision to the

foreign material exclusion procedure consisted of replacing the

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maintenance instruction with Point Beach administrative procedure

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PBNP 3.4.25, " Exclusion of Foreign Material From Plant Components

and Systems".

The inspector reviewed the new procedure and

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discussed its implementation with maintenance planners and system

engineers.

Several concerns were identified with this procedure.

Steps 7.3.2

and 7.3.5 provided no guidance to the planner on what criteria to

use for determining the extent of cleanliness controls required.

By the inspector's observations, the material controls of step

7.3.4 were sparsely implemented around the reactor cavity during

Unit I refueling operations. An incident involving a bag of

booties and gloves being left inside the IWlA containment accident

fan following maintenance demonstrated that the new procedure was

not being effectively utilized.

Following discussions with the

inspector, plant management indicated that additional changes were

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being considered to the foreign material exclusion procedure to

improve the guidance provided regarding the extent of controls

needed and the applicability of these controls. This item will

remain open pending additicnal progress of corrective actions and

subsequent review by the inspector.

d.

(Closed) Unresolved item (266/93002-02: 301/93002-02):

Emergency

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Diesel Generator Glycol Water Mixture.

This issue involved the use of a glycol water mixture in the

licensee's two (G01 and G02-) emergency diesel generators (EDGs).

On January 18, 1993, the EDG vendor notified the licensee that the

use of glycol as an engine coolant would result in derating of the

EDGs by five percent. The licensee reevaluated the loads for' EDGs

G01 and G02 and found that the worst case loading of EDG G01 was

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not substantially affected by the derating. However, the licensee

determined that the half-hour design basis accident (DBA) load

requirement of 2909 KW was 11 KW above the derated capacity of

2898 KW for EDG G02. The licensee removed 239 KW of load from EDG

G02 and thereby restored the operability of G02. On January 25,

1993, the licensee replaced the glycol mixture in the G02 EDG with

the required treated water.

The inspector determined that since original installation in 1970,

the engine coolant has been a glycol water mixture instead of

treated water as recommended by the vendor. The concern was that

the glycol mixture would not provide adequate cooling if the EDG

was fully loaded.

However, the original and existing EDG vendor

and maintenance instruction manuals specified water and a

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corrosion inhibitor for the engine coolant.

The inspector found-

that revisions to the maintenance instruction manuals were issued

to file and not reviewed by plant personnel. This was considered

a weakness.

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10 CFR Part 50, Appendix B, Criterion III, " Design Control,"

requires that design measures provide for the selection and review

for suitability of materials and processes that are essential to

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the safety-related functions of the structures, system, and

components. The failure to install the appropriate EDG engine

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coolant was a violation of Criterion III.

However, the violation

was not cited because the criteria specified in Section VII.B.2 of

the " General Statement of Policy and Procedures for NRC

Enforcement Actions," (Enforcement Policy, 10 CFR Part 2,

Appendix C, were met.

Specifically, when the vendor notified the

licensee, prompt corrective action was taken. Additionally, the

worst case loading of 2909 KW for the first half-hour following a

DBA was only 11 KW or 0.38% above the manufacturer's EDG rating

and, therefore, the safety significance was minimal.

Furthermore,

since the DBA load requirements drop off after the first half-

hour, the actual seven day kw loads of 2584 were well within the

200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> EDG rating. Moreover, in 1970 the G01 EDG was tested at

3053 KW for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> followed by load cycling between 2850 and

3053 KW for an additional 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />.

Based on the above

information, this item is closed.

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No violations or deviations were identified.

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3.

Plant Operations (71707) (71710) (93702)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

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facility tours, interviews and discussions with plant personnel and

management, verification of safety system status, and review of facility

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records.

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To verify equipment operability and compliance with technical

specifications (TS), the inspectors reviewed shift logs, Operations'

records, data sheets, instrument traces, and records of equipment:

malfunctions. Through work observations and discussions'with Operations

staff members, the inspectors verified the staff was knowledgeable of

plant conditions, responded promptly and properly to alarms, adhered to

procedures and applicable administrative controls, was cognizant of in

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progress surveillance and maintenance activities, and was aware of

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inoperable equipment status. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS.

Shift changes were observed,

verifying that system status continuity was maintained and that proper

control room staffing existed. Access to the control room was

restricted and operations personnel carried out their assigned duties in

an effective manner. The inspectors noted professionalism in most

facets of control room operation.

Plant tours and perimeter walkdowns were conducted to verify equipment

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operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controir, physical

protection controls, and equipment tag out procedures were properly

implemented.

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a.

Unit 1 Operational Status

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The unit commenced this period in refueling outage 20.

This

40 day outage was completed three days early. The reactor was

restarted on May 4 and the unit was placed on line May 6.

Full

power was reached on May 10.

b.

Unit 2 Operational Status

Power was reduced to 60 percent on April 1 to isolate two of the

four main condenser water boxes and search for a suspected tube

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leak.

Sodium levels had increased in the steam generators and

condenser inleakage was suspected.

No leak could be found and

sodium levels subsequently returned to normal even though all the

condenser water boxes were returned to service the next day.

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cause of the elevated sodium levels was attributed to chemical

hideout return in the steam generators.

On April 5, pressurizer level instrument bistable 2LC-4280 failed

low. This caused all pressurizer heaters to deenergize and

primary coolant letdown to isolate as designed. The inspector

responded to the control room and noted that operators took prompt

and appropriate immediate corrective actions. Charging flow was

minimized to reduce the rate of level rise in the pressurizer due

to letdown flow being isolated. The rising pressurizer level

compressed the bubble sufficiently to counter the effects of

pressure drop due to the loss of pressurizer heaters. Operators

were dispatched to manually shut pressurizer heater supply

breakers but the failed bistable was identified as the cause of

the event and was replaced before level departed the normal band.

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This restored normal control of pressurizer heaters and coolant

letdown flow. Although the technical staff was assembled to

determine a course of response to the event, management appeared

slow in communicating guidance to the control room.

The unit operated at full power during the remainder of this

period with the exception of requested load following power

reductions,

c.

Enaineered Safeauards Features System Walkdown (71710)

The inspectors performed a detailed walkdown of portions of the

auxiliary feedwater system in order to independently verify

operability.

The auxiiiary feedwater system walkdowns included

verification of the following items:

  • Inspection of system equipment conditions.
  • Confirmation that the system check-off-list and operating

procedures were consistent with plant drawings.

  • Verification that system valves, breakers, and switches were

properly aligned.

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  • Verification that instrumentation was properly valved in and

operable.

  • Verification that valves required to be locked had appropriate

locking devices.

  • Verification that control room switches, indications, and

controls were satisfactory.

  • Verification that surveillance test procedures properly

implemented the TS's surveillance requirements.

A minor deficiency was identified. Chemical addition tank outlet valve

AF-85A was a normally shut valve that was found open.

The valve did not

affect the safety function of the auxiliary feedwater system. This

deficiency was communicated to plant management for correction.

The

inspector observed that the attached funnels for the chemical addition

tanks did not have covers to prevent foreign material entry and were

significantly corroded. This presented the potential to transfer these

corrosion products to the steam generators.

Licensee management was

reviewing the observation.

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d.

Eauipment Stowaae

During various vital area tours, the inspectors noticed equipment that

was neither properly stowed nor restrained, presenting potential seismic

hazards. The inspectors discussed with plant management the repetitive

nature of this concern and that it appeared the plant inspection program

had not been effective. Additionally, the inspectors were concerned

that a violation was recently issued for inadequate equipment stowage

and that the licensee responded that they were in compliance with

equipment stowage requirements.

The licensee committed to revise their

docketed response to the Notice of Violation (92024-01), to address

these additional concerns. Corrective action adequacy will be monitored

on a continuing basis and documented when the violation is closed.

No violations or deviations were identified.

4.

Radioloaical Controls (71707)

The inspectors routinely observed the plant's radiological controls and

practices during normal plant tours and the inspection of work

activities.

Inspection in this area included direct observation of the

use of Radiation Work Permits (RWPs); normal work practices inside

contaminated barriers; maintenance of radiological barriers and signs;

and health physics (HP) activities regarding monitoring, sampling, and

surveying. The inspectors also observed portions of the radioactive

waste system controls associated with radwaste processing.

From a radiological standpoint the plant was in good condition, allowing

access to most sections of the facility. When discrepancies were

identified, the HP staff responded quickly.

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a.

Hiah Radiation Area not Posted

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On May 6 a plant health physics technician identified a high

radiation area in the auxiliary building that was not posted.

The technician immediately posted the area as required and HP

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management initiated a review of- the change in radiological

conditions. This review revealed that the area had been surveyed

and identified as meeting the conditions for posting as a high

radiation area during the two previous weekly surveys.

The

failure to post the area was immediately recognized by plant

personnel, a condition report was generated, and an investigation

initiated. The licensee's corrective actions were prompt and

thorough.

Their investigation included performing a Human

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Performance Enhancement System (HPES) evaluation of this event and

others involving personnel errors and/or inattention to detail.

The failure to post the area after it was identified as-a high

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radiation area is a violation of Technical Specification 15.6.11.

However, this violation was not cited because the identification

and corrective actions satisfy the criteria specified in Section.

VII.B of the " General Statement of Policy and Procedure for NRC

Enforcement Actions", (Enforcement Policy 10 CFR Part 2,

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Appendix C).

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Hiah Radiation Levels on Filter

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On April 15, while preparing to change a filter. downstream of a

liquid radioactive waste holding tank, an operator noted that

radiation levels were about 5 rem /hr on contact with the filter

housing and 400 mrem /hr at 30 cm from the surface. Although there

was no specific procedural requirement directing the operator to

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check radiation levels prior to attempting replacement of that

filter, he was following standard plant precautions for such

operations. Since these high levels were unexpected, the operator

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did not attempt to replace the filter but instead contacted health

physics for assistance. His exemplary actions prevented

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unnecessary exposures to radiation and a potential-overexposure.

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The area was subsequently surveyed, posted, and the filter was

removed and placed in an appropriate storage location.

Additionally, the licensee performed dosimetry review and

determined no inadvertent exposures had occurred prior to the area

being posted.

Based on an isotopic analysis of the filter

entrapment, the licensee determined that the likely source of the

high activity was residue from cleaning of several highly

contaminated valves. The decontamination room sink where the

cleaning was done drained into the liquid waste tank and the job

had been done the day before the activity on the filter was found.

The licensee evaluated their procedures and precautions for

changing potential radioactive filters and determined that

additional precautions were warranted.

Filter change procedure

and task sheet changes and operator aids were among the controls

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considered. An area radiation monitor was installed on the

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laundry / chem tank outlet filter to alert operators to abnormal

radiation levels.

No violations or. deviations were identified; however, one non-cited

violation was identified.

5.

Maintenance / Surveillance Observation (62703) (61726)

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Maintenance

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The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards._ The inspectors

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determined that these activities did not violate limiting

conditions for operation (LCOs) and that required redundant

components were operable.

The inspectors verified that required

administrative, material, testing, radiological, and fire

prevention controls were adhered to.

Specifically, the inspectors observed / reviewed the following

maintenance activities:

RMP 96 (Revision 9), Reactor Head and Upper Internals

Removal and Installation

During a review of procedure RMP 96, the. inspector noted

that step 3.3.1 of the master copy, which was marked up to

incorporate several temporary changes, was already initialed

to signify completion of that step. This occurred because

the person making the temporary changes.used a photostatic

copy of the procedure that had been in use at the time the

need for the temporary changes was identified. Although

this was the method directed by plant instructions, the

intent was that initials be removed from those pages being

entered into the master procedure.

Preexistent initials on

a procedure create the potential to omit performance of the

initialled step.

Following discussions with the inspector, plant management

reviewed their temporary change process to determine

appropriate revisions to prevent recurrence. A proposed

revision to this procedure to address the deficiency was

scheduled for review by the Manager's Supervisory Staff on.

June 1.

The inspector discussed the proposed changes with

plant management.

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IWP 91-209*A-01 (Revision 0), Modification of Main Steam

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Isolation Valve IMS-2017, Unit 1

This modification completes the physical corrective action

implemented by the company to address design deficiencies in

the main steam isolation valves that had contributed to

numerous past failures of the valves to close upon demand.

The most significant of these had occurred September 29,

1991, and is documented in Inspection Report 266/301/91025.

MWR 931852, Troubleshooting and Repair of G-01 Fuel Oil Sump

Level High/ Low Switches

While manually filling the G-01 emergency diesel generator

fuel oil sump, a fault occurred with the fuel oil sump level

control switches which caused the diesel to be declared

inoperable and required entry into a seven day limiting

condition for operation. During normal operation, these

mercury switches control transfer of fuel oil from the day

tank to the engine sump. Although extensive engineering

support of the ensuing evaluation of this problem was

observed by the inspector, no cause for the fault was

identified.

All attempts to recreate the faulty indication were

fruitless and the level control switches operated properly

during ensuing diesel runs.

Consequently, the switches were

left as found and the diesel was declared back in service.

A modification had previously been scheduled to change the

location of these switches due to vibration concerns during

diesel operation.

Although the licensee had a condition report system to

document conditions that might appear to be adverse to the

safe conduct of operation, including events or conditions

that might provide data to the operating experience review

program, no condition report was generated to document this

event. This is one of two examples of a violation for

inadequate corrective action (266/93009-01A).

MWR 932349 SI pump oil change and inspection

On April 12, the oil in Unit I safety injection pump 1-P15f

was replaced. The motor also had its oil replaced and its.

bearings removed and inspected.

During the ensuing return

to service test, the motor bearings failed.

The reactor was

in a refueling outage at the time and therefore'the pump was

not required to be operable.

An evaluation of the cause and

discussion with the mechanic performing the work, indicated

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that the bearings had not been adequately lubricated prior

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to reassembly. The motor was replaced with a refurbished

motor and both-pump and motor were satisfactorily tested and

returned to service. The reactor was subsequently started

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up following completion of the refueling outage.

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As a matter of routine, the old motor bearing oil was sent

offsite for analysis. The pump and motor used different

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types of oil for lubrication of their bearings, Rykon #32

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and #68, respectively.

During interviews, the mechanic

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stated that the labels on the portable containers used to

these containers and had fallen off.

Believing he

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transport the oil to the job site did not adhere properly to

remembered which oil was in each hand and by performing a

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color comparison, he filled the pump and motor with the oil

he believed to be correct. After the motor bearings failed,

he informed his supervisor that he may have put the wrong

oil in each component.

The motor oil analysis results were received May 12 and

indicated that, based on measured viscosity, the wrong oil

had been used in the motor bearings.

At this time, the

plant contacted the pump vendor who initially stated that

improper viscosity oil in the pump would have-little effect

on operability.

Based on this information, the plant deemed

that the pump had remained operable. A followup contact by

the vendor indicated that the higher viscosity oil did

present a concern to pump operation.

This concern was.due-

to potential inadequate pump bearing lubrication.

Based on

this new information, the plant declared the pump inoperable

and changed the oil in the pump to assure that it contained

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the proper oil. The old pump oil was also sent for analysis

to verify its type and.the pump was inspected for abnormal

indication of bearing or- oil slinger ring wear.

Analysis of the old pump oil was-received May 24 and it also

was determined to have been the wrong type.

This verified

that the pump and motor oils had been switched during the

maintenance evolution.

This. item remains unresolved pending

the licensee's root cause determination and subsequent

evaluation by the inspector (266/93009-02).

b.

Surveillance

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The inspectors- observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with. license requirements.

For the surveillance test procedures listed below, the inspectors

determined that-precautions and LCOs were adhered to, the required

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administrative approvals and tag-outs were obtained prior to test

initiation, testing was accomplished by qualified ~ personnel in

accordance with an approved test procedure, test instrumentation

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was properly calibrated, the tests were completed at the required

frequency, and that the tests conformed to TS requirements.

Upon

test completion, the inspectors verified the recorded test data

was complete, accurate, and met TS requirements; test

discrepancies were properly documented and rectified; and that

the systems were properly returned to service.

Specifically, the inspectors witnessed / reviewed selected portions

of the following test activities:

ORT 3 (Revision 25), Safety Injection Actuation with Loss of

Engineered Safeguards AC, Unit 1

During performance of this test the inspector identified a

weakness in the way operators were acknowledging alarms.

This test induced numerous alarms which required

acknowledgement by one of several operators either

performing the test or whom were on watch. The inspector

observed operators who were inducing alarms during the test,

and acknowledging alarms without visually verifying which

alarms were actually being acknowledged.

This was observed

during portions of the test which required securing the

emergency diesel generators. The electrical distribution

system control board and annunciators were part of Unit 2's

control board, the unit that was operating during the test.

The inspector questioned the operators (including a senior

reactor operator) about this practice and was told that the

operator on watch was responsible for ensuring other alarms

were not present. The inspector considered acknowledgement

of alarms without verification to be a weakness and a poor

operating practice. The concern was disseminated to each

shift and the operations manager will reinforce proper alarm

acknowledgement practices during future shift meetings.

ORT 17 (Revision 0), Containment Integrated Leak Rate Test,

Unit 1

TS-1 (Revision 37), Emergency Diesel Generator G-01 Biweekly

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TS-2 (Revision 37), Emergency Diesel Generator G-02 Biweekly

TS-10 (Revision 12), local Leak Test of Containment Hatches

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The inspector observed testing of the Unit 2 containment

upper personnel airlock and questioned certain aspects of

the plant's local leak rate test methodology.

This will be

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reviewed as an inspector follow item in a future inspection

(301/93009-03).

TS-30 (Revision 12), High and Low Head Safety injection

Check Valve Leakage Test (Cold Shutdown), Unit 1

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ICP 5.22 (Revision 11), Feedwater Control

The technician performing the work was very knowledgeable of

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the system being worked on and of the conduct of the test.

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A completed data sheet from the previous performance of this-

annual test was used by the technician to assist him in

evaluating test results. The inspector observed good

coordination between this test and .an unrelated test being.

performed on other control circuitry to assure that the

tests did not interfere with each other.

IT-4 (Revision 31), Low Head Safety Injection Pumps and

Valves (Monthly), Unit 2

Ultrasonic testing of the reactor vessel nozzles.

No deviations were identified; however, one example of a violation was -

identified.

6.

Safety Assessment /0uality Verification (40500) (90712) (927001

Wisconsin Electric's quality assurance programs were inspected to assess

the implementation and effectiveness of programs associated with

management control, verification, and oversite activities.

Special

consideration was given to issues which may be indicative of overall

management involvement in quality matters such as self improvement

programs, response to regulatory and industry initiatives, the frequency

of management plant tours and control room observations, and management

personnel's attendance at technical and planning / scheduling meetings.

a.

Licensee Event Report (LER) Review

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The inspector reviewed LERs submitted to the NRC to verify that'

the details were clearly reported, including accuracy of the

description and corrective action taken. -The inspector determined

whether further information was required, whether generic

implications were indicated, and whether the event warranted

onsite follow up. The inspector also verified that appropriate

corrective action was taken or responsibility was assigned and

that continued operation of the facility was conducted in

accordance with Technical Specifications and did not constitute an

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unreviewed safety question as defined in 10 CFR 50.59. The

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following LERs were reviewed and closed:

266/301/93-003

Nonconservative Setpoints for the Low

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Temperature Overpressure System

This report described a condition t.here the setpoints for the low

temperature overpressure (LTOP) system were nonconservative.

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This information was provided to the licensee from Westinghouse

Electric Corporation in a letter dated March 15, 1993. The

location of the reactor coolant system pressure transmitters was

not considered in the LTOP setpoint development analysis. With

reactor coolant pumps running and developing a differential

pressure across the core, the reactor vessel pressure is greater

than that seen by pressure transmitters. 'As a result, the LTOP

setpoint is about 34 psig too high to operate both reactor coolant

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pumps throughout the entire temperature range during the worst

case mass input transient.

As corrective action, the licensee considered several options.

Changes were made to procedures OP-1A, " Cold Shutdown.to Low Power

Operation" and OP-3C, " Hot Shutdown to Cold Shutdown" to ensure

that one reactor coolant pump was secured when cold leg

temperature was below 160' F and to require that the control

switch for the idle pump be red-tagged out.

Restricting operation.

to one reactor coolant pump would reduce the differential pressure

across the core sufficiently that the maximum allowable vessel

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pressure would not be exceeded even with the existent LTOP

setpoints and pressure transmitter locations. At temperatures

above 152

F, the maximum allowable pressure would be sufficiently

high to permit unrestricted coolant pump operations under the

existent configuration,

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The licensee had submitted an exemption request with respect to

this issue to allow use of recently approved American Society of

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Mechanical Engineers (ASME) Code Case N-514.

Plant management

stated that they intended to withdraw this specific exemption

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request and instead await conclusion of the routine ASME code

approval process before proceeding. Any additional compensatory

measures were to be included in the follow on correspondence.

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This item is being tracked by' Unresolved Item 266/93006-01;.

301/93006-01.

301/93-003 Monthly Reactor Protection and Safeguards and Nuclear

Instrumentation Systems Testing Not Performed Within

Required Periodicity

This report described the event where portions of the monthly

reactor protection system and safeguards and nuclear

instrumentation system tests required by plant technical

specifications were not performed within their required

periodicity. A notice of enforcement discretion was granted by

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the NRC for this occurrence due to the extenuating circumstances.

Details appear in paragraph 6.c below. The licensee had

previously submitted a change to their technical specifications to

increase the periodicity of these tests based upon observed

acceptable instrument drift data.

266/93-004 Containment Hatch Temporary Third Door Tied Open

During Refueling Operations

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This report described the tying open of the temporary third door

of a containment personnel hatch during refueling operations.

Details appear in paragraph 6.d below. The plant was cited for

this violation due to inadequate implementation of corrective

action for a previous similar event.

266/93-005 Inadvertent Engineered Safety Feature Actuation

This report described the inadvertent actuation of.an engineered

safety feature while adjusting the time delay relay setpoint for a

containment accident fan. On April 15, while adjusting time delay

relays for Unit I containment' accident fans, service water

isolation valve ISW-2880 inadvertently stroked shut.

The licensee

considered this an actuation of an engineered safety feature and

the NRC was notified via the emergency notification system. This

valve supplied Unit 1 turbine building auxiliaries and its

function was to automatically isolate nonessential loads during a

safety injection event if at least four service water pumps were

not running 30 seconds after the pumps received a start signal.

This automatic isolation had no adverse consequences since Unit I

was shutdown for refueling at the time and the emergency cooling

systems were not required to be operational. Additionally, only

non-essential loads were isolated by this valve.

If this event

had occurred during power operation, it would not have been safety

significant. The cause of this event was a-minor equipment

configuration difference between Units 1 and 2 actuation circuitry

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for this function. Unit 2 circuitry utilized separate relays for

controlling containment fan . starting and service water isolation;

however, Unit 1 circuitry had both these functions on two contacts

off the same relay. The Unit 2 containment accident fan relays

had been adjusted earlier that day without incident.

Later, while

adjusting Unit I relay time delays, the service water isolation

occurred because the requisite time interval had elapsed following

relay actuation.

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To prevent recurrence of this event, the configuration of Unit I

relays was changed to correspond to that of Unit 2 with the

different actuation functions being controlled by separate relays.

The inspector discussed this event with plant personnel and had no

further concerns.

266/301/93-006

Containment Isolation Valve not Leak Tested in

Accordance with Technical Specification

Requirements

This report described discovery of a containment isolation valve

which was not included in a leak testing program as required by

Technical Specification 15.4.4.III, " Type C Tests".

Containment

isolation valve CV-369A, for the chemical and volume control

system and RHR cross connect line, had not been leak tested on

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either unit. CV-369A was the first isolation valve located

outside containment.

This condition was identified while investigating a boric acid

buildup on the socket weld between the pipe and valve, which was

due to a crack in the weld.

During the ensuing engineering

evaluation, it was identified that CV-369A was a containment

isolation valve subject to required leak testing, but was not

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included in the testing program.

However, this violation was not

cited because the identification and corrective actions satisfy -

the criteria specified in Section VII.B of the " General Statement

of Policy and Procedure for NRC Enforcement Actions", (Enforcement

Policy 10 CFR Part 2, Appendix C). The licensee's investigation

of the cause determined that the valve was incorrectly classified

during a review of containment penetrations conducted in 1984 to

determine which valves should be subject to testing.

As

corrective action, the piping associated with CV-369A was modified

during the recent Unit I refueling outage to permit leak testing

of this valve.

The valve was subsequently leak tested with

acceptable results.

A similar modification was scheduled for Unit

2 during its next refueling outage in the fall of 1993.

b.

Manaaer's Supervisory Staff Meetina

The inspector observed sessions 93-08, 93-09 and 93-10 of the

Manager's Supervisory Staff meetings.

Issues discussed included a

request for enforcement discretion to postpone required testing,

as built walkdowns of control board wiring, low temperature

overpressure protection setpoints, seismic mounting of post

accident instrumentation, and crossover steam isolation valves.

c.

Enforcement Discretion for Testina

On April 9, the NRC informed the licensee that enforcement of

requirements to perform monthly surveillance of certain reactor

protection instrument functions would be waived for up to 30 days.

This was in response to the licensee's request to postpone

performance of those tests that increased the probability of a

Unit 2 scram while both Unit I and the Kewaunee Nuclear Plant were

both shut down for refueling outages.

Loss of Unit 2 under these

conditions could result in a degraded grid voltage condition as

discussed in Inspection Report 50-266/93006;50-301/93006.

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The surveillances involved were monthly reactor protection and.

safeguards circuit testing. All these tests, with the exception

of reactor trip breaker testing, had already been reviewed for

testing at a quarterly interval and a technical specification

change request was in the final stage of being issued by the NRC.

The company analyzed reactor trip breaker performance data to

verify that instrument setpoints would not drift beyond setpoint

limits and thereby justified extending the test interval.

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The enforcement discretion was also predicated on the testing

being performed within two weeks following return to service of

either Unit 1 or Kewaunee.

The Kewaunee plant was started up

April 16 and Point Beach completed the deferred tests April 28.

This ended the requirement for the enforcement discretion. The

inspector observed portions of this testing and no unexpected

conditions were noted.

d.

Temocrary Third Door to Containment Blocked Open Durina Refuelino

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On April 8, with refueling operations in progress, the licensee

discovered the temporary third door to the Unit I containment

personnel hatch secured open.

Technical Specification 15.3.8.1

required a temporary third door on the outside of the personnel

lock be in place whenever both doors in a personnel lock were open

during refueling operations. The door was immediately secured by

the individual that discovered it open. A sign had been posted on

both sides of the door stating " Refueling In Progress, Keep This

Door Closed, Do Not Block Open".

The licensee conducted an evaluation of this event and determined

the door was open for 15 minutes or less. A HPES evaluation was

also performed to determine root causes and contributing factors.

While the individual responsible for this event could not be

determined, the licensee did identify that the security guard-

stationed at the entrance to containment was not notified that

refueling activities were in progress and that the door was to

remain closed.

Security guard notification and control of the temporary third

door were actions that had been committed to in response to a

previous occurrence of this door being open on October 10, 1991.

Additionally, a violation was issued for this door being blocked

open during refueling operations in 1989 (see Inspection Report

50-301/88022). Hovrave", implementation of corrective actions for

the previous violations were inadequate to prevent recurrence.

This is one of two examples of a violation for inadequate

corrective action (266/93009-01B).

No deviations were identified; however, an example of a violation and a

non-cited violation were identified.

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7.

Outstandina Items (92701)

Inspection Follow Up Items

Inspection follow up items are matters which have been discussed with

Wisconsin Electric management, will .be reviewed further by the

inspector, and involve some action on the part of the NRC, company or

both. A follow up item disclosed during the inspection is discussod in

paragraph 5.b.

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Unresolved Items

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Unresolved . items are matters about which more information is required in

order to ascertain whether they are acceptable items, items of

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noncompliance, or deviations. An unresolved item identified during the

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inspection is discussed in paragraph 5.a.

8.

Non-cited Violations

During this inspection, certain of your activities, as described above

in Paragraphs 2.d, 4.a, and 6.a, appeared to be in violation of NRC

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requirements. However, these violations were categorized at Severity

Level TV or V and they are not being cited because they meet the

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criteria specified in Section VII.B of the " General Statement of

Policy and Procedures for NRC Enforcement Actions", (10 CFR Part 2,

Appendix C)'.

9.

Exit Interview (71707)

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A verbal summary of preliminary findings was provided to the Wisconsin

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Electric representatives denoted in Section 1 on May 26, at the

conclusion of the inspection. No written inspection material was

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provided to company personnel during the inspection.

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The likely informational content of the inspection report with regard to

documents or processes reviewed during the inspection was also

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discussed.

Wisconsin Electric management did not identify any documents

or processes that were reported on as proprietary.

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