ML20044E507

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Insp Repts 50-413/93-09 & 50-414/93-09 on 930314-0410. Violations Noted.Major Areas Inspected:Review of Plant Operations,Surveillance Observations,Maint Observations,Lers & Follow Up of Previously Identified Items
ML20044E507
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 05/03/1993
From: Hopkins W, Lesser M, William Orders, John Zeiler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20044E484 List:
References
50-413-93-09, 50-413-93-9, 50-414-93-09, 50-414-93-9, NUDOCS 9305250094
Download: ML20044E507 (16)


See also: IR 05000413/1993009

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Report Nos.:

50-413/93-09 and 50-414/93-09

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.: 50-413 and 50-414

License Nos.: NPF-35 and NPF-52

Facility Name:

Catawba Nuclear Station Units 1 and 2

Inspection Conducted: March 14, 1993 - April 10, 1993

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Inspector:

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6AW. T. O ders Senior Re51 den Inspector

Date Signed

Inspector:[

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Inspector:

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fg4 J. Zeiler', Resident Injpector Q

Date Signed

Approved by:

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Mark S. Lesser, Chief

Date Signed

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Projects Section 3A

Division of Reactor Projects

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

review of plant operations, surveillance observations, maintenance

observations, licensee event reports; and follow-up of previously

identified items.

Results:

One violation was identified involving the failure of a qualified

technician to properly supervise a non-qualified individual during

motor maintenance on the 2A Safety Injection pump. The non-

qualified individual reassembled the inboard motor bearing to the

motor incorrectly, resulting in the motor failure when the pump

was operated (paragraph 5.c).

Two Non-Cited Violations were identified involving 1) the failure

to perform two Technical Specification surveillances of available

offsite power sources (paragraph 4.c), and 2) the failure to

perform Technical Specification surveillances of the Containment

Spray system and Phase B Isolation logic circuitry (paragraph 7).

9305250094 93o503

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One licensee weakness was identified in the maintenance area

involving a problem with pre-defined maintenance Work Order

documents not specifying the correct procedures to be used

(paragraph 5.c).

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REPORT DETAILS

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Persons Contacted

Licensee Employees

S. Bradshaw, Shift Operations Manager

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J. Forbes, Engineering Manager

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R. Futrell, Regulatory Compliance Manager

  • T. Harrall, Safety Assurance Manager
  • J. Lowery, Compliance Specialist
  • W. McCollum, Station Manager

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W. Miller, Operations Superintendent

M. Tuckman, Catawba Site Vice-President

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Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

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NRC Resident Inspectors

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W. Orders

P. Hopkins

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  • J. Zeiler

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  • Attended exit interview.

Acronyms and abbreviations used throughout this report are listed in the

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last paragraph.

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2.

Plant Status

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Unit 1 Summary

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Unit 1 operated at or near full power for the entire report period.

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Unit 2 Summary

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Unit 2 began the report period in Mode 5 and day 44 of a planned 65 day

refueling outage. The unit achieved criticality on March 30 and ZPPT

was initiated. Following completion of ZPPT testing, reactor power was

escalated to Mode 1 on April 1, and the main generator was placed on

line that afternoon completing the outage four days early.

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Following the completion of power escalation testing, the unit achieved

100 percent power on the afternoon of April 5 and operated at or near

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full power for the remainder of the report period.

3.

Plant Operations Review (71707)

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a.

General Observations

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The inspectors reviewed plant operations throughout the report

period to verify conformance with regalatory requirements, TS and

administrative controls.

Control Room logs, the Technical

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Specification Action Item Log, and the R&R log were routinely

reviewed.

Shift turnovers were observed to verify that they were

conducted in accordance with approved procedures. The complement

of licensed personnel on each shift inspected, met or exceeded the

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requirements of Technical Specifications.

Further, daily plant

status meetings were routinely attended.

Plant tours were performed on a routine basis. The areas toured

included but were not limited to the following:

Turbine Buildings

Auxiliary Building

Units I and 2 Diesel Generator Rooms

Units 1 and 2 Vital Switchgear Rooms

Units 1 and 2 Vital Battery Rooms

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Standby Shutdown Facility

During the plant tours, the inspectors verified by observation and

interviews that measures taken to assure the physical protection

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of the facility met current requirements. Areas inspected included

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the security organization; the establishment and maintenance of

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gates, doors, and isolation zones; and access control badging.

In addition, the areas toured were observed for fire prevention

and protection activities and radiological control practices. The

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inspectors also selectively reviewed current PIRs to determine if

the licensee was appropriately documenting problems and

implementing corrective actions.

b.

Refueling Outage

The licensee completed the Unit 2, E0C-5 Refueling Outage on April

1, four days ahead of schedule.

The MSR tube bundles were replaced this outage, in preparation for

steam generator replacement. The tubes in the old MSRs had a

constituent of copper which has been shown to cor. tribute to SG

tube degradation. This job was critical path for the outage.

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was scheduled to be accomplished in 40 days but was actually

completed 3 days ahead of schedule. This large modification was

well planned and executed.

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Fourteen RN valves in the shared return header were replaced

during this outage. Complicated, innovative methods of isolating

for this work were necessary which necessitated placing Unit 1 in

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement. The modification was successfully

completed in this time frame, and is considered to have been well

planned and executed. For more details pertaining to the RN work,

refer to NRC Inspection Report Nos. 50-413,414/93-07.

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Additional shutdown risk precautions were implemented during this

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outage which were targeted at minimizing the risk to the plant

during periods of high vulnerability.

For example, the licensee

did not drain the reactor coolant system to mid-loop until the

core was unloaded. The licensee also installed temporary diesel

generators to use as a source of temporary power, along with one

of the permanent D/Gs, to maintain both residual heat removal

trains available when the reactor coolant system was drained to

mid-loop after refueling. These initiatives are notable, and

indicative of safety consciousness.

Overall, this was one of Catawba's better refueling outages,

having been accomplished ahead of schedule, and under the estimate

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for radiation exposure and with minimal rework.

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c.

Control Room Drawing Review

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The inspectors reviewed approximately 200 control room drawings to

verify that they were legible, accurate and to assure that there

was no inordinate backlog of drawing corrections to be made.

Virtually all of the drawings were legible, accurate and current.

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One drawing was illegible, but was immediately replaced.

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If a modification affects VTO drawings, the control room drawing

and aperture card are required to be updated within seven days.

Non-VTO drawing must be updated within 30 days. The inspectors

verified there was no significant backlog of drawing updates for

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either VTO or non-VTO drawings.

No violations or deviations were identified.

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4.

Surveillance Observation (61726)

a.

General

During the inspection period, the inspectors verified that plant

operations were in compliance with various TS requirements.

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Typical of these requirements were confirmation of compliance with

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the TS for reactivity control systems, reactor coolant systems,

safety injection systems, emeraency safeguards systems, emergency

power systems, containment, and other important plant support

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systems. The inspectors verified that:

surveillance testing was

performed in accordance with approved written procedures, test

instrumentation was calibrated, limiting conditions for operation

were met, appropriate removal and restoration of the affected

equipment was accomplished, test results met acceptance criteria

and were reviewed by personnel other than the individual directing

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the test, and any deficiencies identified during the testing were

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properly reviewed and resolved by appropriate management

personnel.

b.

Surveillance Activities Reviewed

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The inspectors witnessed or reviewed the following surveillarm:

PT/0/A/4150/19A

Reactivity Balance Calculation

PT/1/A/4200/06A

Boron Injection Lineup

PT/1/A/4200/06B

ECCS Valve Lineup

PT/1/A/4200/62

NW Surge Chamber IB RN Flow Verification

PT/1/A/4250/06

Unit 1 CA Pump Head and Valve Verification

PT/1/A/4350/02A

Diesel Generator IA Operability Test

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PT/1/A/4450/03B

Anr.ulus Ventilation System Train IB

Operability Test

PT/1/A/4450/13B

Auxiliary feedwater Pump Room C02

Weekly Test

PT/2/A/4000/02C

Mode 3 Periodic Surveillance Item

PT/2/A/4150/01A

NC System Mini Hydro Test

PT/2/A/4150/01B

NC Manual Leakage Calculation

PT/2/A/4150/01D

NC System Leakage Calculation

PT/2/A/4150/02

Visual Inspection Verification of

Radiation

System Outside Containment

PT/2/A/4200/06

Unit 2 CA Pump Head and Valve Verification

PT/2/A/42.50/02B

Weekly Main Turbine Movement Test

PT/2/A/4250/03E

CA System Discharge Control Valve

Throttling Procedure Verification

PT/2/A/4550/04

D/G Fuel Oil Tank Oil / Water Inspection

(Tank 2B1)

PT/2/A/4600/01

RCCA Movement Test

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PT/2/A/4600/02

Periodic Surveillance Test

PT/2/A/4600/02A

Mode 1 Periodic Surveillance

PT/2/A/4600/09

Loss of Operator Aid Computer Check

PT/2/A/4600/19B

Premode 2 Periodic Surveillance Items

PT/2/8/4250/02A

Main Turbine Weekly Trip Test

No discrcpancies were identified.

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c.

Missed Power Availability Technical Specification Surveillances

During this report period, the inspectors reviewed the

circumstances surrounding two separate occasions during the

previous report period, in which the licensee failed to perform a

TS required surveillance to verify the operability of the offsite

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power sources. TS 3.8.1.1 requires that when one or more offsite

power sources or D/Gs become inoperable, appropriate action shall

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be taken to demonstrate the operability of the two offsite power

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sources by performing the surveillance af TS 4.8.1.1.1.a within 1

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hour and at least once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter. Operability of the

offsite power sources is determined by verifying proper breaker

alignments and checking indications of power availability.

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The first missed surveillance occurred on February 25, 1993, after

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Unit 1 entered TS 3.0.3 at 5:45 p.m. due to both trains of the RN

system being inoperable. Since RN is the assured cooling source

for the D/Gs, both Unit 1 D/Gs were also declared inoperable.

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Operations personnel thought that it was not necessary to perform

the power availability surveillance since TS 3.0.3 had been

entered.

Following shift turnover at 6:30 p.m., the oncoming

shift personnel questioned the need to perform the surveillance

and correctly determined that the surveillance was required,

regardless of the fact that TS 3.0.3 had been entered. At 8:35

p.m. the surveillance, confirming that both offsite power sources

had been operable since the entry into TS 3.0.3 was completed.

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Since the surveillance was not performed within the required 1

hour from the time that D/Gs were declared inoperable, this

constituted a missed TS surveillance.

The licensee's corrective action included providing guidance to

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operations personnel on each shift addressing the surveillance

requirements of TS 4.8.1.1.1.a when TS 3.0.3 is entered. A TS

interpretation document is also to be written to clarify these

requirements, and additional training will be performed when the

interpretation is completed. The inspectors concluded that

adequate corrective action was being taken by the licensee.

Therefore, this violation will not be cited because the licensee's

efforts in identifying and correcting the violation meet the

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criteria specified in Section VII.B. of the Enforcement Policy.

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This issue is documented as NCV 413/93-09-01:

Failure to Perform

TS Surveillances of Offsite Power Sources.

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The second missed power availability surveillance occurred on

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March 5, 1993. At 10:01 p.m. that day, the Unit 1 Train A D/G was

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declared inoperable when Train A of the RN system was rendered

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inoperable while conducting an ISI hydro test.

In order to

maintain the Unit 1 Train A D/G available during this testing (but

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not Operable), a contingency plan was implemented f r providing

cooling water to the D/G if a start signal was received. The

contingency plan allowed the D/G to remain in service during the

hydro.

Since the D/G remained in service, it was not necessary

for operations personnel to perform procedure OP/1/A/6350/02 for

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removing the D/G from service.

Steps directing the performance of

TS surveillance 4.8.1.1.1.a are embodied in this procedure. Thus,

since OP/1/A/6350/02 was not performed, operations personnel

failed to recognize the need to perform the surveillance. The

missed surveillance was identified by personnel on the next shift.

At 9:20 a.m. on March 6, the surveillance was completed confirming

that both offsite power sources were operable,

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Since this event, the procedures for removing both the RN system

and D/Gs from service have been revised to ensure that appropriate

actions are taken when a D/G is rendered inoperable.

In addition,

details of the incident were discussed with all operations shifts.

The inspectors determined that adequate corrective action was

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being taken by the licensee. Therefore, this violation will not

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be cited due to the' licensee's efforts in identifying and

correcting the violation met the criteria specified in Section

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VII.B. of the Enforcement Policy. This issue is identified as

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another example of NCV 413/93-09-01:

Failure to Perform TS

Surveillances of Offsite Power Sources.

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One NCV was identified.

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5.

Maintenance Observations (62703)

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a.

General

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Station maintenance activities of selected systems and components

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were observed / reviewed to ensure that they were conducted in

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accordance with the applicable requirements. The inspectors

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verified licensee conformance to the requirements in the following

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areas of inspection:

activities were accomplished using approved

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procedures, and functional testing and/or calibrations were

performed prior to returning components or systems to service;

quality control records were maintained; activities performed were

accomplished by qualified personnel; and materials used were

properly certified. Work requests were reviewed to determine the

status of outstanding jobs and to assure that priority was

assigned to safety-related equipment maintenance which may affect

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system performance.

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Maintenance Activities Reviewed

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The inspectors witnessed or reviewed the following maintenance

activities:

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WO 92079653-01

Install Air Conditioning in D/G Room 2B

(observed hanger installation work)

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WO 92079898-01

Rework / repair Valve 2NRE22

WO 93002516-01

Repair Leak on Valve 2 nil 65

WO 93002517-01

Repair Leak on Valve 2 nil 67

WO 93015229-01

Repair / replace Relay in 2AT62 for VA Buss

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WO 93015238-01

Investigate and Repair Invertor Low

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Voltage on 2EIB

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WO 93021128-01

Inspect Repair VC/YC Chiller

WO 93021188-01

.D/G 1A Oil Condition Inspection Verification

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No discrepancies were identified.

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c.

Inadequate Maintenance on 2A Safety Injection Pump Motor

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On March 23, 1993, with Unit 2-in Mode 5, the 2A NI pump was being

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run in order to fill the Cold Leg Accumulators. The pump was

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being used for this activity even though it was still considered

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inoperable and was awaiting post-maintenance testing as a result

of performing motor bearing maintenance on March 6.

After the

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pump was operated for a short period, a fire detection alarm

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annunciated in the control room indicating a problem in the 2A NI

pump room. An operator was sent to investigate and discovered

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smoke coming from the NI pump motor. The pump was secured and it

was subsequently discovered that the inboard bearing of the motor

had failed due to a lack of adequate lubrication. Since there was

extensive damage to the motor, a decision was made to replace the

motor prior to entering Mode 4.

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When the inboard motor bearing was disassembled, it was discovered

that the cause of the lubrication problem was the incorrect

assembly of the bearing's oil sling ring which provides bearing

lubrication. On March 6, in connection with routine preventative

maintenance, the inboard motor bearing had been disassembled,

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inspected, and then reassembled. During this reassembly, the

technician incorrectly reassembled the oil sling ring such that

lubricating oil was not delivered to the bearing when the pump was

operated.

Following this discovery, licensee management directed

a three-man team to investigate the motor failure. The findings

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from this investigation will be documented in PIR 2-093-213.

The inspectors reviewed the WO package for the March 6 preventive

maintenance, the maintenance procedures governing the work, and

discussed the work with the maintenance supervisor responsible for

the work.

In addition, the preliminary findings from the

licensee's investigation were reviewed to determine if the

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inspector's concerns had been evaluated. A number of problems

were identified pertaining to this maintenance activity.

Several

of the more significant items are discussed below:

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1.

The technician who performed the inboard bearing reassembly

was not qualified via the licensee's ETQS to perform the

task.

The individual was on loan from another department

and was assisting the IAE group during the outage. The

individual was working with a qualified technician who

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failed to properly direct / supervise the non-qualified

individual's activity as required. The inspectors

considered this to be the major deficiency resulting in the

incorrect assembly of the motor bearing.

2.

The procedure used to perform the motor maintenance,

MP/0/A/2002/01, Motor Inspection and Maintenance, lacked

detailed instructions to ensure that the motor bearing was

reassembled properly. Step 11.5 of the procedure stated

that the motor (including the bearings) be reassembled in

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the reverse order of disassembly.

In addition, the

manufacturer's drawings of the motor were not adequately

detailed, nor were there drawings of the bearings for the

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technicians to refer to during reassembly.

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Procedure MP/0/A/2002/001 was revised on December 30, 1992

for motors of this type.

The new procedure, IP/0/A/4974/13,

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Horizontal Split-Sleeve Bearing Motor Inspection and

Maintenance, should have been used for this task. The WO

document incorrectly designated MP/0/A/2002/01 to be used as

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opposed to IP/0/A/4974/13. The inspectors determined that

this was not an isolated case.

It was concluded that there

were numerous other examples in which pre-defined WO

documents specified the use of procedures that had been

deleted and did not specify using a new procedure that had

replaced them. This was identified as a licensee weakness

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in the maintenance area.

4.

Alarms for high bearing temperature were not received in the

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Control Room when the bearing failed. Temperature readings

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from the inboard thermocouple were much lower than expected

temperatures based on the magnitude of bearing damage

observed. The thermocouple was tested following the event

and found to be working properly. This indicated, along

with other problems identified with the spring mechanism of

the thermocouple, that it may not have been making adequate

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contact with the bearing. The inspectors confirmed that one

of the licensee's correction action items was to check the

proper operation of thermocouples of other safety-related

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motors.

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The inspectors reviewed the licensee's ETQS requirements governing

the responsibility of qualified technicians when working with non-

qualified individuals on safety-related tasks. Standard No.

902.0, Employee Qualifications Component, Section 5.1.7, requires

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that when an individual is required to perform a task which he/she

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is not qualified to, then that individual will be

directed / supervised by a qualified individual to ensure that the

task is performed correctly. Contrary to this requirement, a non-

qualified individual was allowed to reassemble the inboard motor

bearing on the 2A Safety Injection pump without adequate

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supervision by a qualified individual. This resulted in the

incorrect reassembly of the bearing by the non-qualified

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individual and the subsequent damage to the motor when the pump

was operated. This issue is documented as Violation 414/93-09-02:

Failure to follow ETQS Requirements during Safety Injection Motor

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Maintenance.

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One violation was identified.

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Review of Licensee Event Reports (92700)

The below listed LERs were reviewed to determine if the information

provided met NRC requirements. The determination included: adequacy of

description; verification of compliance with Technical Specifications

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and regulatory requirements; corrective action taken; existence of

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potential generic problems; reporting requirements satisfied; and the

relative safety significance of each event.

a.

(Closed) LER 413/91-05:

TS 3.0.3 Entry as a Result of Both

Trains of Control Room Ventilation System Being Inoperable due to

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a Possible Design / Installation Deficiency and Inappropriate

Action.

Both trains of the VC/YC system became inoperable on February 12,

1991. The Tra3n "A" YC chiller tripped on low refrigerant

temperature due to a refrigerant leak at the chiller compressor

power terminal box. The Train "B" chiller was placed in service

but the YC chiller tripped on low refrigerant temperature when the

associated condenser water automatic control valve inadvertently

failed open. This placed the plant outside the provisions of TS 3.7.6 and in TS 3.0.3 for approximately I hour and 50 minutes. TS 3.0.3 was exited once the Train "B" condenser water automatic

control valve was restored and the YC chiller was successfully

restarted.

The refrigerant leak on the Train "A" YC chiller was repaired, the

low refrigerant tempereture cutout switch was calibrated and the

YC system was returned to service.

To prevent recurrence, the licensee has completed the following

actions:

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VC/YC system low refrigerant temperature cutout switches

have been included in the stations preventative maintenance

program.

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Maintenance Engineering Services has issued MES Guideline 21

wM ch ider.tifies the independent verification process for

the remov71 and r

toretion of equipment from service. This

includes - Tectrical circuits.

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Bahnson's procedures AFP-CNS-5.019, NH95 and NH96 Hydromotor

Actuators, AFP-CNS-5.020, NH91 ITT Hydromotor Actuators, and

AFP-CNS-5.025, NH92 ITT Hydromotor Actuators, have been

enhanced to ensure that electrical isolation are tagged in

accordance with Station Directive 3.0.12, Electrical Circuit

Isolation Tagging.

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MES evaluated the compressor power terminal box assembly and

found that the terminal box assembly had been modified to

reduce the potential of refrigerant leaks.

b.

(Closed) LER 413/91-18: Unit 1 Essential Bus Blackout due to

Inappropriate Action.

On Sept mber 6, 1991, Unit I was operating in Mode 1.

Diesel

Generatcr IB was being shutdown by a non-licensed operator

following a post maintenance operability test run. The operator

began unloading the diesel per procedure and inadvertently opened

Feeder Breaker IETB-3 ins'aad of IETB-18. This caused the

generator to immediately upply the load to IETB. The operator

attempted to secure the diesel. This caused the sequencer

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circuit, sensing a loss of voltage on the bus, to initiate the

blackout sequence and to restart the diesel. The operator was

unable to stop the diesel using the normal means but was able to

stop the diesel using the emergency stop solenoid. After this

event, the diesel generator was successfully retested.

The licensee evaluated this event and initiated the following

corrective actions to prevent recurrence:

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An " Operator Update" was issued to the operators which

emphasized the importance of self-verification.

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The event was incorporated into the operations training

packages.

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Procedures PT/l(2)/A/4350/02A(B), Diesel Generator

Operability Test, and OP/l(2)/A/6350/2, Diesel Generator

Operation, were revised so that the procedure steps match

actual equipment / panel nomenclature.

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An evaluation was made on the feasibility of assigning

higher priority to the resolution of essential breaker

indication problems.

No changes were deemed necessary.

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A review was made for the identification of the

administrative procedures which employ the use of tags to

identify equipment deficiencies.

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The operators training program has been revised to provide

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specific demonstration and practice in recognizing diesel

generator automatic starts, runaway diesels, and other

failures. Diesel generator restart criteria has also been

included.

c.

(Closed) LER 413/91-26: SSPS TS Violation Due to a Possible

Inappropriate Action.

During the performance of a surveillance test of the SSPS system

on October 17, 1991, a jumper was discovered across two terminals

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inside the Unit 1 SSPS cabinet. This jumper would have prevented

the Train "B" Reactor Trip Breakers from opening during certain

events. The jumper was removed and the Unit I and 2 SSPS cabinets

were inspected to verify that no additional unknown jumpers were

installed.

To prevent recurrence Procedures IP/1(2)/A/3200/03A, Reactor

Protection / Engineered Safeguards Features Response Time Testing,

were revised to clearly specify the installation and removal of

the jumpers required for the tests.

During January - February,

1992, a detailed electrical cabinet inspection was performed by

the Safety Review Group.

Several discrepancies were identified;

however, out of approximately 1100 cabinets inspected, only four

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undocumented jumpers were found. These four jumpers were

installed inside non-safety related cabinets. The licensee

concluded that the current controls for the use of jumpers were

adequate.

d.

(Closed) LER 414/91-13: TS violation Due to Inappropriate Action

Rendering One Train of the BDMS.

With Unit 2 in Mode 6 during a refueling outage, sporadic and

. spurious alarms were received in the control room on November 2,

1991. Subsequent investigation found Valve 2NV252A, Chemical

Volume and Control NV-Pump Suction from Refueling Water Storage

Tank, was red tagged closed and power to the valve was de-

energized.

This valve is required to open on a high flux signal

from the BDMS. Two trains of BDMS are required when the plant is

in Modes 5 and 6.

With Valve 2NV252A closed and power de-

energized, Train "A" of the BDMS was inoperable per TS.

Operability of Train "A" was restored after the breaker which

supplies power to the valve was closed.

This event was evaluated by the licensee but no required revisions

to procedures or other documents were identified.

No violations or deviations were identified.

7.

Followup on Previous Inspection Findings (92701 and 92702)

a.

(Closed) URI 50-413, 414/93-07-04: Review of SSPS and ESFAS

Testing Inaccuracies.

During the previous inspection, two problems involving the SSPS

and ESFAS testing circuitry were reviewed.

One of these problems involved the licensee's failure to properly

test the continuity of the containment spray channel between the

process instrumentation and the ESF actuation and logic circuitry.

A special test circuit had been provided by the vendor to conduct

this continuity check, however, the licensee failed to recognize

the significance of this circuit, and as a result, failed to ever

perform this testing.

Following identification of the problem,

the licensee initiated the continuity testing for both Units and

did not find an operability problem with the Containment Spray

circuitry. Based on these results, the licensee determined that a

past operability problem did not exist. However, this was

considered a missed surveillance and thus a violation of TS 4.3.2.1.

This violation will not be subject to enforcement action

because the licensee's efforts in identifying and correcting the

violation meet the criteria specified in Section VII.B. of the

Enforcement Policy. Thit issue is documented as NCV 413,414/93-

09-03:

Inadequate Surveillance Testing of ESFAS Circuitry.

..

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.

12

As discussed in the previous inspection, a problem was identified

while the licensee was attempting to perform the continuity checks

for the first time on Unit 1.

Two of the four containment spray

channels tested did not exhibit the expected response.

Following

a visual inspection of the test circuitry boards, it was-

discovered that the circuit cards were not wired:according to the

vendor schematics. When the licensee. discussed this problem wi.th

the vendor (Westinghouse), it was learned that an upgrade had.been

made to these circuit cards in 1979, however, due to a problem at

the vendor site, the cards were shipped to Catawba prior to the

modifications being incorporated.

The licensee replaced these cards, retested the circuitry, and

verified that all other spare cards in the warehouse were

correctly wired. No discrepant spare cards were identified.

The second problem reviewed in the previous report irvolved a mis-

wiring error in the SSPS Train "A" Phase B Containtrent Isolation

test circuitry. Because of this wiring discrepancy, when the

monthly SSPS Actuation Logic Surveillance was conducted, the Phase

B Containment Isolation Logic was not tested.

Instead,

Containment Spray Actuation logic was tested twice.~ The wiring

errors were corrected and the circuitry was tested with

satisfactory results.

Based on these results and the fact that

the Phase B isolation circuitry is verified to function every 18

months during ESF Response Time testing, the licensee determined

that past operability was not a concern.

During this inspection, the licensee completed a review of work

performed in the SSPS cabinets and determined that there have been-

no station modifications to these circuits which would have

involved the associated wiring discrepancies. The licensee

discussed with the vendor, the possibility of a manufacturer's

field change that would have. corrected the wiring errors, but,

none have been identified.

Based on this, it appears that a

manufacturer's fabrication deficiency resulted in this mis-wiring

error.

TS 4.3.2 requires that each train of the Phase B Isolation

Automatic Actuation Logic and actuation relays be tested at least

every 62 days on a staggered test basis. The mis-wired. circuitry

~

resulted in the missing of these surveillances since. initial

start-up. However, this violation will not be subject to

enforcement action because the licensee's efforts in correcting.

the violation meet the criteria specified in Section VII.B. of the

Enforcement Policy. This issue is documented as another example

of NCV 413, 414/93-09-03:

Inadequate Surveillance Testing of

ESFAS Circuitry.

One NCV was identified.

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)

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13

8.

Exit Interview

The inspection scope and findings were summarized on April 14, 1993,

with those persons indicated in paragraph 1.

The inspector described

the areas inspected and discussed in detail the inspection findings

listed below. No dissenting comments were received from the licensee.

'

The licensee did not identify as proprietary any of the materials

provided to or reviewed by the inspectors during this inspection.

Item Number

Description and Reference

j

NCV 413/93-09-01

Failure to Perform TS Surveillances of Offsite

Power Sources (paragraph 4.c).

VIO 414/93-09-02

Failure to Follow ETQS Requirements during

Safety Injection Motor Maintenance (paragraph

5.c).

NCY 413, 414/93-09-03

Inadequate Surveillance Testing of ESFAS

,

Circuitry (paragraph 7).

,

9.

Acronyms and Abbreviations

BDMS -

Boron Dilution Mitigation System

CA

-

Auxiliary feedwater

D/G

-

Diesel Generator

.

.

'

ECCS -

Emergency Core Cooling System

EOC-5 -

End-of-Cycle 5

ESFAS -

Engineered Safety Feature Actuation System

ETQS -

Employee Training Qualification System

IAE

-

Instrumentation and Electrical

IP

-

Instrumentation Procedure

ISI

-

Inservice Inspection

4

LER

-

Licensee Event Report

MES

-

Maintenance Engineering Services

MSR

-

Moisture Separator Reheater

NC

-

Reactor Coolant

NCV

-

Non-Cited Violation

NI

-

Safety Injection

,

NV

-

Chemical Volume and Control System

NW

-

Containment Valve Injection Water System

t

OP

-

Operating Procedure

PIR

-

Problem Investigation Report

PT

-

Periodic Procedure

RCCA -

Rod Cluster Control Assembly

RN

-

Nuclear Service Water System

R&R

-

Removal and Restoration

SG

-

Steam Generator

SSPS -

Solid State Protection System

TS

-

Technical Specifications

TSM

-

Temporary Station Modification

.

URI

-

Unresolved Item

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-

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14

VA

-

Auxiliary Building Ventilation System

VC/YC -

Control Room Ventilation and Chill Water System

V10

-

Vital To Operation

WO

-

Work Order

ZPPT -

Zero Power Physics Testing

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