05000328/LER-1981-134-03, /03L-0:on 811111,relay Contacts for Fire Zone 367 Reactor Coolant Pump 3 Found Wired Normally Closed.Correct Configuration Is Normally Open.Caused by Error in Connection Drawings.Connection Drawings Revised

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/03L-0:on 811111,relay Contacts for Fire Zone 367 Reactor Coolant Pump 3 Found Wired Normally Closed.Correct Configuration Is Normally Open.Caused by Error in Connection Drawings.Connection Drawings Revised
ML20039A565
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 12/10/1981
From: Harding M, Romine W
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20039A561 List:
References
LER-81-134-03L, LER-81-134-3L, NUDOCS 8112180371
Download: ML20039A565 (1)


LER-1981-134, /03L-0:on 811111,relay Contacts for Fire Zone 367 Reactor Coolant Pump 3 Found Wired Normally Closed.Correct Configuration Is Normally Open.Caused by Error in Connection Drawings.Connection Drawings Revised
Event date:
Report date:
3281981134R03 - NRC Website

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