LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Submitted |
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e COOPER NUCLE AR STATION hNjeg Nebraska Public Power District
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CNSS820444 August 5, 1982 hhfbf
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i U} r-Mr. John T. Collins, Regional Administrator
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U.S. Nuclear Regulatory Commission Region IV
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611 Ryan Plaza Drive
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l' Suite 1000 Arlington, Texas 76011
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Dear Sir:
This report is submitted in accordance with Section 6.7.2.B.2 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occurrence that was determined during leak rate testing.
A licensee event report form is also attached.
Report No.:
50-298-82-15 Report Date:
August 5, 1982 Occurrence Date: July 6, 1982 Facility:
Cooper Nuclear Station Brownville, Nebraska 68321 During the Spring 1982 Refueling Outage all primary containment double "0" ring seals, testable expansion bellows, electrical penetrations, and testable isolation valves were tested in accordance with Technical Specifications Section 4.7.A.2.f and Tables 3.7.2 through 3.7.4.
This report describes a condition which may have resulted in failure to meet the limiting condition for operation established in Section 3.7. A.2 of the Technical Specifications. There were a total of 47 Type "B" pene-trations and 46 Type "C" penetrations tested. There were seven Type "C" penetrations that were found to be leaking above established limits which necessitated repair and retest.
Leak rate limits for each penetration are arbitrary limits established from the preoperational local leak rate test results. No electrical penetrations, double "0" ring seals, or testable bellows were leaking excessively. Listed below is a summary of each primary containment penetration which was repaired due to a high leakage rate.
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4 V
8208160173 820805 PDR ADOCK 05000298 S
PDR
Mr.' John T. Collins August 5, 1982 Page 2.
- - X-10 RCIC Turbine Steam Supply Line, RCIC-MO-15 (inboard-isolation valve) and RCIC-MO-16 (outboard isolation valve)
Initial leakage was found to be 17.79 cfh. The established limit is 2.0 scfh. RCIC-MO-15 was disassembled and the gate was lapped. After repair, the leakage was reduced to 1.87 cfh.
RCIC-M0-15 and MO-16 are Anchor 3" gate valves with Limitorque motor operators.
X-14 RWCU, Inlet to RWCU System, RWCU-M0-15 (supply inboard isolation) and RWCU-MO-18 (supply outboard isolation)
Initial leakage was found to be 75.38 cfh.. The established limit is 2.0 scfh. RWCU-MO-15 was removed and replaced with a new valve identical to the original. After the new valve was installed,'the leakage was.99 scfh. RWCU-MO-15 and MD-18 are Anchor 6" gate valves.
X-210B & 211B RHR to Suppression Pool, RHR-MO-34B (suppression pool cooling inboard isolation valve) RHR-MO-38B (suppression pool inboard. spray isolation valve) and RHR-MO-39B (suppression' pool cooling and spray outboard isolation valve)
Initial leakage was found to be 126.12 cfh. The established limit is-8.0 scfh. RHR-M0-34B was disassembled, the seat was lapped, the~ disc seating surface was cut down on a lathe,'and a new bonnet. gasket in--
stalled.
RHR-MO-38B was disassembled, the seat and plug were cleaned,.
and a new bonnet gasket installed'.
RHR-MO-39B was disassembled,.the seat was lapped, and a new bonnet gasket' installed'.- After repairing these valves, the leakage was 13.0 cfh..
Even though the leakage was above the established limit, further repair was not initiated because of
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the safety margin in the established ~ limits.
RHR-M0-34B is an Anchor 18" globe valve, RHR-MO-38B is an Anchor 6" globe valve, and RHR-MO-39B-is an Anchor 18" gate valve.
X-212 RCIC Turbine Exhaust to the Suppression Chamber, RCIC-15CV and RCIC-37
Mr. John T. Collins
' August 5, 1982 Page 3.
Initial leakage was found to be 9.87 cfh. The established limit is 1.0 scfh. RCIC-15CV was disassembled, the seat was lapped, the disc was cleaned, and a new gasket was installed.
RCIC-37 was disassembled, the 4
seat and disc were cleaned, and a new bonnet gasket was installed.
After repairs, the leakage was reduced to 2.47 cfh.
Even though this value was above the established limit, further repair was not initiated because of the safety margin in the established limit.
RCIC-15CV is an Anchor 8" check valve and RCIC-37 is an Anchor 8" globe valve.
X-214 HPCI Turbine Exhaust to the Suppression Chamber, HPCI-15CV and HPCI-44 Initial leakage was found to be 10.11 cfh. The established limit is 2.0 scfh. HPCI-15CV was disassembled and the disc and seat were lapped.
After repair, the leakage was 2.89 scfh. Even though the leakage was above the established limit, further repair was not initiated because of the safety margin in the established limits. HPCI-15CV is an Anchor 20" check valve.
X-220 Primary Containment Purge and Vent Exhaust from Suppression Chamber, PC-M0-230 (inboard isolation valve), PC-AO-245 (outboard isolation valve),
PC-M0-305 (inboard isolation bypass), and ACAD-1308MV (ACAD torus vent)
The initial leakage was too rapid to determine an initial leak rate.
The established limit is 5.0 scfh.
PC-AO-245 was disassembled and the rubber seating ring replaced. After repair, the leakage was 2.84 scfh.
PC-M0-230 and PC-M0-305 were not repaired or adjusted. Therefore, primary containment would have been maintained by the' inboard isolation valves.
PC-A0-245 is an Allis-Chalmers 24" butterfly valve.
X-226 HPCI Pump Suction from the Suppression Chamber, HPCI-M0-58 Initial leakage was found to be 15.96 cfh. The established limit is 3.0 scfh. HPCI-M0-58 was disassembled, the seat and gate were lapped, and a new bonnet gasket installed. After repair, the leakage was 3.755 cfh.
Even though the leakage was above the established limit, further repair was not initiated because of the safety margin in the established limits. HPCI-MO-58 is an Anchor 16" gate valve.
o Mr. John T. Collins August 5, 1982 Page 4.
A review was conducted of the local leak rate test from 1980 through 1982 to determine penetrations that repetitively exceeded established limits each year. Due to this review, additional corrective actions are being done on the following penetrations.
X-210B & 211B New valves have been on order since November 1981 for RHR-M0-34B and RHR-M0-39B. A new seat and disc have been on order since November 1981 for RHR-MO-38B.
X-212 A new valve is in the warehouse for RCIC-37.
Engineering is conducting an evaluation on the best location for the new valve because of the very close location of the existing valve and the ceiling which makes this valve very difficult to repair. A new valve has been on order since November 1981 for RCIC-15CV.
X-220 Engineering is exploring the possibility of developing a procedure to verify PC-AO-245 is seating properly.
In accordance with Section 4.7.A.2.a of the Technical Specifications, the total leakage rate shall not exceed the equivalent of 0.6 La (189 scfh) of the primary containment volume per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 58 psig.
All valves were tested at >58 psig with the exception of the MSlV's as prescribed in Section 4.7.A.2.f.
Pressure decay or water collection was used to determine the leakage. The total as-found leakage was approx-imately 1640 cfh. The actual leakage would have been approximately 222 l
cfh because in 5 of the 7 penetrations that required repair, only one valve had to be repaired to decrease the leakage. Therefore, the other isolation valve in each of the penetrations would have maintained the primary containment. After repair of the leaking valves, the' leak rate was reduced to less than 108 scfh.
Sincerely, m
L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:cg Attach.
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| 05000298/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-001-03, /03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed | /03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed | | | 05000298/LER-1982-002-03, /03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced | /03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced | | | 05000298/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1982-003-03, /03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily | /03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily | | | 05000298/LER-1982-004, Forwards LER 82-004/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-004/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-004-03, /03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised | /03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised | | | 05000298/LER-1982-005, Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested | Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested | | | 05000298/LER-1982-005-03, /03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position | /03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position | | | 05000298/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-006/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-006-03, /03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established | /03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established | | | 05000298/LER-1982-007-03, /03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modif | /03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified | | | 05000298/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-008-03, /03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair | /03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair | | | 05000298/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-009-03, /03L-0:on 820428,suppression Chamber Level Instrument PC-LI-13 Failed full-scale.Caused by Personnel Error.Ref Water Leg Drained While Collecting Torus Water Sample.Level Transmitter Replaced.Sampling Valve Tagged | /03L-0:on 820428,suppression Chamber Level Instrument PC-LI-13 Failed full-scale.Caused by Personnel Error.Ref Water Leg Drained While Collecting Torus Water Sample.Level Transmitter Replaced.Sampling Valve Tagged | | | 05000298/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-009/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-010-03, /03L-0:on 820517,diesel Generator 1 & Output Breaker Tripped Shortly After Starting.Caused by Open Contact of Potential Transformer Disconnect Switch Interrupting Voltage to Overcurrent Relay Restraining Coil | /03L-0:on 820517,diesel Generator 1 & Output Breaker Tripped Shortly After Starting.Caused by Open Contact of Potential Transformer Disconnect Switch Interrupting Voltage to Overcurrent Relay Restraining Coil | | | 05000298/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-011-03, /03-0:on 820514,isolation Valve RR-740AV Failed to Close.Caused by Dirty Solenoid Slug.Solenoid Valve Replaced | /03-0:on 820514,isolation Valve RR-740AV Failed to Close.Caused by Dirty Solenoid Slug.Solenoid Valve Replaced | | | 05000298/LER-1982-011, Forwards LER 82-011/03-0.Detailed Event Analysis Submitted | Forwards LER 82-011/03-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-012-03, /03L-0:on 820522,during Reactor Vessel Head Removal for Refueling,Closure Stud Nuts Were Improperly Detensioned.Caused by Personnel Error.Personnel Informed of Mistake & Procedure Checklist Revised | /03L-0:on 820522,during Reactor Vessel Head Removal for Refueling,Closure Stud Nuts Were Improperly Detensioned.Caused by Personnel Error.Personnel Informed of Mistake & Procedure Checklist Revised | | | 05000298/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-013-03, /03L-0:on 820607,during Performance of Snubber Operability Test,Two Mechanical Shock Suppressors, RR-SNUB-SS7A1 & RR-SNUB-SS7B1,found Inoperable.Caused by Overload of Snubbers.Snubbers Replaced | /03L-0:on 820607,during Performance of Snubber Operability Test,Two Mechanical Shock Suppressors, RR-SNUB-SS7A1 & RR-SNUB-SS7B1,found Inoperable.Caused by Overload of Snubbers.Snubbers Replaced | | | 05000298/LER-1982-014-03, /03L-0:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-20,BJ-23,BJ-13 & BJ-15. Caused by Improper Fabrication Techniques During Original Const.Affected Piping & Fittings Replaced | /03L-0:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-20,BJ-23,BJ-13 & BJ-15. Caused by Improper Fabrication Techniques During Original Const.Affected Piping & Fittings Replaced | | | 05000298/LER-1982-015-03, /03L-0:on 820706,eleven Penetrations Leaked Excessively During Leak Rate Test.Cause Not Stated.Valve Repairs Performed on Anchor Gates,Globes & Checks.Anchor 6 Gate Valve Replaced.Final Leakage within Limit | /03L-0:on 820706,eleven Penetrations Leaked Excessively During Leak Rate Test.Cause Not Stated.Valve Repairs Performed on Anchor Gates,Globes & Checks.Anchor 6 Gate Valve Replaced.Final Leakage within Limit | | | 05000298/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-015/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-016-03, /03L-0:on 820712,diesel Generator Tripped W/No Alarms or Indications.Redundant Sys Operable.Caused by Drift in Holding Mechanism of Safety Trip Valve Overspeed Device. Valve & Section of Control Air Line Replaced | /03L-0:on 820712,diesel Generator Tripped W/No Alarms or Indications.Redundant Sys Operable.Caused by Drift in Holding Mechanism of Safety Trip Valve Overspeed Device. Valve & Section of Control Air Line Replaced | | | 05000298/LER-1982-016, Forwards LER 82-016/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-016/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-017/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-017-03, /03L-0:on 820713,at Completion of Overspeed Test on Diesel Generator 2,diesel Tripped Before Loading.Caused by Low Lube Oil Pressure Switch.Switch Replaced | /03L-0:on 820713,at Completion of Overspeed Test on Diesel Generator 2,diesel Tripped Before Loading.Caused by Low Lube Oil Pressure Switch.Switch Replaced | | | 05000298/LER-1982-018-03, /03L-0:on 820727,torus Water Temp Rose to 102 F, Exceeding Tech Spec Limit.Caused by Greater Bulk Temps During HPCI Test.More Sophisticated Torus Temp Monitoring Sys Will Be Installed by Jul 1983 | /03L-0:on 820727,torus Water Temp Rose to 102 F, Exceeding Tech Spec Limit.Caused by Greater Bulk Temps During HPCI Test.More Sophisticated Torus Temp Monitoring Sys Will Be Installed by Jul 1983 | | | 05000298/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-018/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-019-03, /03L-0:on 820726,drywell Equipment Sump 1G High Level Alarm W/Subsequent Automatic Pump Operation Observed. Caused by Blown Fuse in Power Supply 20-545A for Flow Recorder & Flow Integrator.Fuse Replaced | /03L-0:on 820726,drywell Equipment Sump 1G High Level Alarm W/Subsequent Automatic Pump Operation Observed. Caused by Blown Fuse in Power Supply 20-545A for Flow Recorder & Flow Integrator.Fuse Replaced | | | 05000298/LER-1982-020-03, /03L-0:on 821004,diesel Generator 2 Shutdown W/No Alarms or Indications.Water Found in Lube Oil Sys.Caused by Rupture of Left Cylinder Liner Expansion Seal on Diesel Engine.Seal Replaced & Part Returned to Vendor | /03L-0:on 821004,diesel Generator 2 Shutdown W/No Alarms or Indications.Water Found in Lube Oil Sys.Caused by Rupture of Left Cylinder Liner Expansion Seal on Diesel Engine.Seal Replaced & Part Returned to Vendor | | | 05000298/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-020/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-021, Forwards LER 82-021/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-021/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-021-03, /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement | /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement | | | 05000298/LER-1982-022, Forwards LER 82-022/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-022/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-022-03, /03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified | /03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified | | | 05000298/LER-1982-023-03, /03L-0:on 821128,while Snubber CS-57 Taken Out of Svc to Repair Oil Leak,Snubber Found Inverted.Caused by Loose Extension Tube Locknut Allowing Snubber to Rotate. Snubber Replaced | /03L-0:on 821128,while Snubber CS-57 Taken Out of Svc to Repair Oil Leak,Snubber Found Inverted.Caused by Loose Extension Tube Locknut Allowing Snubber to Rotate. Snubber Replaced | | | 05000298/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-023/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-024/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-024-03, /03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced | /03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced | | | 05000298/LER-1982-025-03, /03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified | /03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified | | | 05000298/LER-1982-025, Forwards LER 82-025/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-025/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-026/03L-0.Detailed Event Analysis Submitted | |
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