LER-1982-004, Forwards LER 82-004/03L-0.Detailed Event Analysis Submitted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2981982004R00 - NRC Website |
|
text
_ _. _ _
y n-COOPER NUCLE AR STATION Nebraska Public Power District
"~ ' " 9'a"" *"!?s Us""^T^
CNSS820110 March 5, 1982 g,
- - d g
Mr. John T. Collins, Regional Administrator f}gn,
'*d %
_g U.S. Nuclear Regulatory Commission y' OSJ g b88 Region IV 611 Ryan Plaza Drive h
gZ
\\.
. k, 3
Suite 1000 Arlington, Texas 76011 N
y
Dear Sir:
- c) m This report is submitted in accordance with Section 6.7.2.B.3 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occurrence that was discovered on February 3,1982.
A li-censee event report form is also enclosed.
Report No.:
50-298-82-04 Report Date:
March 5, 1982 Occurrence Date: January 9, 1982 Fac ility:
Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
An inadequacy was observed in the implementation of administrative and procedural controls developed to implement the requirements of Section 3.ll.C and 4.ll.C of the Technical Specifications.
Conditions Prior to Occurrence:
The reactor was operating at 39% of rated thermal power during a planned power reduction.
Description of Occurrence:
The " indicated" Minimum Critical Power Ratio (MCPR) was discovered to have been below the MCPR operating limit at 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br /> on Jan-uary 9, 1982 without the initiation of appropriate corrective actions as required by Section 3.ll.C of the Technical Specifications.
Designation of Apparent Cause of Occurrence:
The apparent cause of the occurrence was attributed to personnel error in that the surveillance requirements of Section 4.ll.C of the Technical Specifications were not met.
tI z
,...si
._____ h IY.5
\\\\
's lu
[
MF8 l982 L
t jv 8203170449 820305 J
PDR ADOCK 05000298 O
PDR
Mr. John T. Collins March 5, 1982 Page 2.
Analysis of Occurrence:
The operating limit MCPR's are designed to prevent the fuel clad-ding integrity safety limit MCPR of 1.07 from being violated during the course of any of the anticipated abnormal operational trans-ients analyzed in the most current CNS Reload Licensing submittal.
Section'4.11.C of the Technical Specifications require that MCPR be determined daily during reactor power operation at greater than 25%
rated thermal power and following any change in power level or distribution that would cause operation with a limiting control rod pattern. During this occurrence, power was reduced both by de-creasing core flow and inserting control rods. The power reduction was made to initiate a shutdown (if required) so personnel could enter the drywell to investigate an oil level alarm on "B" re-circulation pump motor.
From approximately 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> (start of power reduction) until 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br /> (time of occurrence), core thermal limits, including MCPR, dere evaluated as required. At 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br />, the core thermal limits were calculated by the process computer, however, it was not noted by the reactor engineer onsite or the control room operator that the calculated value of MCPR was below the Technical Specification limit. As a result, corrective action specified in Section 3.11.C of the Technical Specifications was not initiated.
Following the computer calculations, power was further reduced by inserting additional control rods; core flow, however, was not decreased further as "A" recirculation pump was at minimum speed. During this time, core flow Indication showed a flow of approximately 10 X 106 lb/hr (14%). At 2219 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.443295e-4 months <br /> (after both recirculation pumps were back on line), a computer calculation showed all thermal limits including MCPR, to be within the Technical Specification limits. However, the requirements of Section 4.11.C of the Tech-nical Specifications were not complied with for the power changes that occurred between 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br /> and 2219 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.443295e-4 months <br />.
Subsequent to the discovery of this event, a thorough analysis demonstrated that in actuality, the MCPR limit was not violated at 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br />. Thisanalysgsdeterminedthattheindicatedcoreflow of approximately 10 X 10 lb/hr was not correct because of the manner in which the core flow instrumentation functions during single recirculation loop operation. When the reactor is operating in the single loop mode, the core flow instrumentation responds by subtracting the indicated flow in the idle loop from the indicated flow in the active loop. This is because all flow through the idle loop is assumed to be backflow through the inactive jet pumps.
Mr. John T. Collins March 5, 1982 Page 3.
Based upon information from General Electric, it appears, however, that backflow is established in the idle loop only if the pump speed in the active loop is in a range greater than approximately 20 to 40%. The actual speed necessary to establish backflow would be dependent upon core thermal power and the particular hydraulic characteristics of the CNS reactor core. At a pump speed less than 1
i this 20 to 40% range, core flow assumes the characteristics of natural circulation flow.
In this condition, flow through the idle loop is forward flow as opposed to backflow. The core flow instru-mentation, however, in single loop operation will still subtract the flow in the idle loop from the active loop even though that i
flow is now forward flow. The resultant effect of this will be that core flow will indicate approximately 50% of what core flow actually is.
Based upon core stability analysis data provided to the NRC as part of the CNS Cycic 7 licensing submittal, the most restrictive conditions regarding core stability are operation with natural circulation and operation on the 105% rod line. This analysis assumes then that core flow cannot attain a value less than natural circulation flow. Therefore, it can be concluded that at 39% core thermal power, core flow could not be less than the 6
natural circulation value of 22 X 10 lb/hr (30%).
By utilizing a corethermallimitsevaluationmodelthatrunsoff-1gne, it was determined that with a core flow of at least 12 X 10 lb/hr, MCPR would have been within the Technical Specification limit.
If core flow is increased without varying the control rod pattern, MCPR will increase farther and farther from the Technical Specification limiting value. This effect is due to a flow biased multiplier that is applied to the MCPR limit at core flows less than rated core flow.
Conversely, if core thermal power is decreasing by fully (or almost fully) inserting control rods while holding core flow constant, MCPR will also increase due to the effect of the control rod insertions lowering the bundle power in the most limiting locations. Thus, it can be inferred with confidence, that during the interval from 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br /> until 2219 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.443295e-4 months <br />, MCPR was not more limiting than the MCPR calculated at 1459 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.551495e-4 months <br />.
This occurrence was attributed to personnel error. However, since the MCPR limit was not actually violated, this occurrence had no adverse effect on the public health and safety.
Because this event has a potential for repetition, actions as specified under cor-rective actions will be implemented to aid plant personnel in handling this problem in the future.
Mr. John T. Collins March 5, 1982 Page 4.
Corrective Action
After the discovery of this occurrence, a brief descripton of the event was routed to all licensed station personnel.
Additionally, the daily surveillance log will be revised to require the logging of the thermal limits by operations personnel each time they are evaluated by the process computer and the appropriate operations procedure will be revised to require the control room operator to input the natural circulation core flow value (for the appropriate core thermal power) into the process computer if required when operating with a single recirculation loop. These two procedures will be revised and in use by April 1, 1982. A copy of this LER will also be routed to all licensed personnel and the reactor engineers.
Sincerely,
^
L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:cg Attach.
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000298/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-001-03, /03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed | /03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed | | | 05000298/LER-1982-002-03, /03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced | /03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced | | | 05000298/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1982-003-03, /03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily | /03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily | | | 05000298/LER-1982-004, Forwards LER 82-004/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-004/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-004-03, /03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised | /03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised | | | 05000298/LER-1982-005, Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested | Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested | | | 05000298/LER-1982-005-03, /03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position | /03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position | | | 05000298/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-006/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-006-03, /03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established | /03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established | | | 05000298/LER-1982-007-03, /03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modif | /03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified | | | 05000298/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-008-03, /03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair | /03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair | | | 05000298/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-009-03, /03L-0:on 820428,suppression Chamber Level Instrument PC-LI-13 Failed full-scale.Caused by Personnel Error.Ref Water Leg Drained While Collecting Torus Water Sample.Level Transmitter Replaced.Sampling Valve Tagged | /03L-0:on 820428,suppression Chamber Level Instrument PC-LI-13 Failed full-scale.Caused by Personnel Error.Ref Water Leg Drained While Collecting Torus Water Sample.Level Transmitter Replaced.Sampling Valve Tagged | | | 05000298/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-009/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-010-03, /03L-0:on 820517,diesel Generator 1 & Output Breaker Tripped Shortly After Starting.Caused by Open Contact of Potential Transformer Disconnect Switch Interrupting Voltage to Overcurrent Relay Restraining Coil | /03L-0:on 820517,diesel Generator 1 & Output Breaker Tripped Shortly After Starting.Caused by Open Contact of Potential Transformer Disconnect Switch Interrupting Voltage to Overcurrent Relay Restraining Coil | | | 05000298/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-011-03, /03-0:on 820514,isolation Valve RR-740AV Failed to Close.Caused by Dirty Solenoid Slug.Solenoid Valve Replaced | /03-0:on 820514,isolation Valve RR-740AV Failed to Close.Caused by Dirty Solenoid Slug.Solenoid Valve Replaced | | | 05000298/LER-1982-011, Forwards LER 82-011/03-0.Detailed Event Analysis Submitted | Forwards LER 82-011/03-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-012-03, /03L-0:on 820522,during Reactor Vessel Head Removal for Refueling,Closure Stud Nuts Were Improperly Detensioned.Caused by Personnel Error.Personnel Informed of Mistake & Procedure Checklist Revised | /03L-0:on 820522,during Reactor Vessel Head Removal for Refueling,Closure Stud Nuts Were Improperly Detensioned.Caused by Personnel Error.Personnel Informed of Mistake & Procedure Checklist Revised | | | 05000298/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-012/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-013/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-013-03, /03L-0:on 820607,during Performance of Snubber Operability Test,Two Mechanical Shock Suppressors, RR-SNUB-SS7A1 & RR-SNUB-SS7B1,found Inoperable.Caused by Overload of Snubbers.Snubbers Replaced | /03L-0:on 820607,during Performance of Snubber Operability Test,Two Mechanical Shock Suppressors, RR-SNUB-SS7A1 & RR-SNUB-SS7B1,found Inoperable.Caused by Overload of Snubbers.Snubbers Replaced | | | 05000298/LER-1982-014-03, /03L-0:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-20,BJ-23,BJ-13 & BJ-15. Caused by Improper Fabrication Techniques During Original Const.Affected Piping & Fittings Replaced | /03L-0:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-20,BJ-23,BJ-13 & BJ-15. Caused by Improper Fabrication Techniques During Original Const.Affected Piping & Fittings Replaced | | | 05000298/LER-1982-015-03, /03L-0:on 820706,eleven Penetrations Leaked Excessively During Leak Rate Test.Cause Not Stated.Valve Repairs Performed on Anchor Gates,Globes & Checks.Anchor 6 Gate Valve Replaced.Final Leakage within Limit | /03L-0:on 820706,eleven Penetrations Leaked Excessively During Leak Rate Test.Cause Not Stated.Valve Repairs Performed on Anchor Gates,Globes & Checks.Anchor 6 Gate Valve Replaced.Final Leakage within Limit | | | 05000298/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-015/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-016-03, /03L-0:on 820712,diesel Generator Tripped W/No Alarms or Indications.Redundant Sys Operable.Caused by Drift in Holding Mechanism of Safety Trip Valve Overspeed Device. Valve & Section of Control Air Line Replaced | /03L-0:on 820712,diesel Generator Tripped W/No Alarms or Indications.Redundant Sys Operable.Caused by Drift in Holding Mechanism of Safety Trip Valve Overspeed Device. Valve & Section of Control Air Line Replaced | | | 05000298/LER-1982-016, Forwards LER 82-016/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-016/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-017/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-017-03, /03L-0:on 820713,at Completion of Overspeed Test on Diesel Generator 2,diesel Tripped Before Loading.Caused by Low Lube Oil Pressure Switch.Switch Replaced | /03L-0:on 820713,at Completion of Overspeed Test on Diesel Generator 2,diesel Tripped Before Loading.Caused by Low Lube Oil Pressure Switch.Switch Replaced | | | 05000298/LER-1982-018-03, /03L-0:on 820727,torus Water Temp Rose to 102 F, Exceeding Tech Spec Limit.Caused by Greater Bulk Temps During HPCI Test.More Sophisticated Torus Temp Monitoring Sys Will Be Installed by Jul 1983 | /03L-0:on 820727,torus Water Temp Rose to 102 F, Exceeding Tech Spec Limit.Caused by Greater Bulk Temps During HPCI Test.More Sophisticated Torus Temp Monitoring Sys Will Be Installed by Jul 1983 | | | 05000298/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-018/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-019, Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-019/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-019-03, /03L-0:on 820726,drywell Equipment Sump 1G High Level Alarm W/Subsequent Automatic Pump Operation Observed. Caused by Blown Fuse in Power Supply 20-545A for Flow Recorder & Flow Integrator.Fuse Replaced | /03L-0:on 820726,drywell Equipment Sump 1G High Level Alarm W/Subsequent Automatic Pump Operation Observed. Caused by Blown Fuse in Power Supply 20-545A for Flow Recorder & Flow Integrator.Fuse Replaced | | | 05000298/LER-1982-020-03, /03L-0:on 821004,diesel Generator 2 Shutdown W/No Alarms or Indications.Water Found in Lube Oil Sys.Caused by Rupture of Left Cylinder Liner Expansion Seal on Diesel Engine.Seal Replaced & Part Returned to Vendor | /03L-0:on 821004,diesel Generator 2 Shutdown W/No Alarms or Indications.Water Found in Lube Oil Sys.Caused by Rupture of Left Cylinder Liner Expansion Seal on Diesel Engine.Seal Replaced & Part Returned to Vendor | | | 05000298/LER-1982-020, Forwards LER 82-020/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-020/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-021, Forwards LER 82-021/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-021/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-021-03, /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement | /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement | | | 05000298/LER-1982-022, Forwards LER 82-022/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-022/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-022-03, /03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified | /03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified | | | 05000298/LER-1982-023-03, /03L-0:on 821128,while Snubber CS-57 Taken Out of Svc to Repair Oil Leak,Snubber Found Inverted.Caused by Loose Extension Tube Locknut Allowing Snubber to Rotate. Snubber Replaced | /03L-0:on 821128,while Snubber CS-57 Taken Out of Svc to Repair Oil Leak,Snubber Found Inverted.Caused by Loose Extension Tube Locknut Allowing Snubber to Rotate. Snubber Replaced | | | 05000298/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-023/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-024/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-024-03, /03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced | /03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced | | | 05000298/LER-1982-025-03, /03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified | /03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified | | | 05000298/LER-1982-025, Forwards LER 82-025/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-025/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1982-026, Forwards LER 82-026/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-026/03L-0.Detailed Event Analysis Submitted | |
|