05000395/LER-1982-024-03, /03L-0:on 821018,plant Went Into Mode 4 W/O Performing Surveillance Test Procedure 114.002, Operational Leak Test. Caused by Procedural Inadequacies.Procedure Revised to Comply W/Tech Spec Requirements

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/03L-0:on 821018,plant Went Into Mode 4 W/O Performing Surveillance Test Procedure 114.002, Operational Leak Test. Caused by Procedural Inadequacies.Procedure Revised to Comply W/Tech Spec Requirements
ML20028A878
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 11/16/1982
From: Fields H
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028A867 List:
References
LER-82-024-03L, LER-82-24-3L, NUDOCS 8211290164
Download: ML20028A878 (1)


LER-1982-024, /03L-0:on 821018,plant Went Into Mode 4 W/O Performing Surveillance Test Procedure 114.002, Operational Leak Test. Caused by Procedural Inadequacies.Procedure Revised to Comply W/Tech Spec Requirements
Event date:
Report date:
3951982024R03 - NRC Website

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o2 l On October 18. 1982. the Plant went into Mode 4 without performing Surveillance l l0l3ll Tert Procedure (STP) 114.002, " Operational Leak Test."

Technical Specification l 1014 l l 3.4.6.2 requires the STP to be performed prior to entering Mode 4.

There werel o5 I no adverse consecuences as the surveillance was performed short1v after Mode 4 1 0 0 I was entered.

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L. IJ CAUSE DE3CRIPTION AND CORRECTIVE ACTIONS h l_110 l I 'Ihe event was caused by procedural inadequacies. The STP required the Reactor l l 1 l 1 l l coolant System to be 2235 psig. At this pressure, the Plant is in Mode 4.

l l 1 l 2 I l STP-114.002 was revised to comniv with Technical Specification reautrements, l

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