05000287/LER-2005-001
Oconee Nuclear Station | |
Event date: | |
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Report date: | |
2872005001R00 - NRC Website | |
EVALUATION:
BACKGROUND
Technical Specification (TS) 3.5.3 requires two trains of Low Pressure Injection to be operable in Mode 1. Required Action A.1 of this specification states that a single inoperable train must be restored to operable status within 7 days. If operability is not restored within 7 days (Condition C), Required Actions C.1 and C.2, respectively, require the unit to be in Hot Standby (Mode 3) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Hot Shutdown (Mode 4) within 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />.
'TS 3.6.5 requires two trains of the Reactor Building Spray System to be operable in Mode 1. Required Action A.1 of ,this LCO allows 7 days to restore a single inoperable train. If operability is not restored within 7 days, Required Action D.1 requires that the unit be in Hot Standby (Mode 3) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Prior to this event Unit 3 was operating at 100% power with no safety systems or components out of service that would have contributed to this event.
This event is reportable per the criteria of 10CFR50.73 (a)(2)(1)(B) because the unit operated for approximately 27 days in a condition prohibited by TS.
EVENT DESCRIPTION
July 27, 2005:
Room 81 houses the B trains of the Unit 3 Low Pressure Injection [BP] Pumps [P] and Reactor Building Spray [BE] Pumps [P]. In preparation for lead and asbestos paint removal work in this room, Maintenance personnel began sealing off the stairwell above the room using 6 mil poly sheeting. The enclosure was installed to facilitate establishment of a negative pressure condition in Room 81 to allow lead and asbestos paint removal work to proceed with minimal risk to personnel outside of the room.
Room 81 has an open spiral staircase which opens at the top to an entry area. The "Auxiliary and Turbine Building Loss of Cooling/Ventilation Analysis" for Oconee Nuclear Station credits the stairwell to this room as a ventilation path necessary to ensure environmental qualification of the motors which drive these pumps.
August 3, 2005:
Maintenance completed installation of tent enclosure at stairwell above Room 81.
August 30, 2005:
System Engineers performing unrelated work in the Unit 3 Auxiliary Building discovered the tent enclosure had been installed.
Operations Shift Manager (OSM) is notified to declare 3B LPI Pump and 3B BS Pump inoperable. At the time of discovery, these pumps have been inoperable for 34 days (inoperability is assumed to begin at start of tent installation due to low operability margin).
August 30, 2005 at 1020 hrs:
OSM declares 3B LPI Pump and 3B BS Pump inoperable, enters applicable TS conditions.
August 30, 2005:
Further inspection finds filters installed on ventilation grilles on the air handling units for the room.
August 30, 2005 at 1525 hrs:
Tent enclosure removed and ventilation filters removed. OSM declares 3B LPI Pump and 3B BS Pump operable. Duration of inoperability is 34 days. Redundant train (A train) of LPI and BS remained operable and available throughout the period of B train inoperability. At no time was the system function lost.
September 6, 2005:
Request submitted to Operations to revise procedure for performing Primary rounds. Procedure change will require Nuclear Equipment Operator to verify ventilation flow path is not obstructed through the stairwell or ventilation ports (air handling unit intake grilles).
September 11, 2005:
Signs are posted outside of each LPI/BS Pump Room prohibiting blockage of stairway.
CAUSAL FACTORS
The personnel performing these maintenance activities, including those responsible for planning the work, were unaware of the requirement for maintaining a ventilation flow path in Room 81.
Two root causes have been identified.
The first cause was a failure of Engineering to capture critical design inputs and assumptions (such as the need for open air flow path through the LPI/BS Pump Rooms) in design deliverable documents. Had this requirement been reflected in System Design Basis Specifications through the site Engineering Change Process, other site groups would have had an opportunity to review the change and assess impact to their areas of work responsibility.
Engineering was aware of the need to capture critical inputs on design deliverable documents, since other key inputs such as initial room temperature were appropriately captured using the Engineering Change Process. However, the engineers involved incorrectly assumed that the physical characteristics of the room (as related to air flow path) would not change. Therefore, they did not realize the need for having controls to ensure no changes would occur.
The second cause was a lack of management guidance for managing and controlling design passive features.
CORRECTIVE ACTIONS
Immediate:
1) Removed tent enclosure from Room 81 stairwell.
2) Removed filter from ventilation grilles on air handling units in Room 81.
Subsequent:
1) Placed sign outside LPI/BS Pump Rooms on all units stating requirement to maintain air flow path through stairwell.
Planned:
1)Auxiliary and Turbine Building Loss of Cooling/Ventilation Analysis will be reviewed to ensure all critical design inputs are captured in design deliverable documents.
2)Operator rounds procedure will be revised to require verification of available flow path through stairwell and ventilation grilles.
3)A review of calculations related to passive and other features (in general) will be performed to identify post-accident conditions that have the potential to take credit for physical characteristics of the plant. The purpose of this review is to ensure that assumptions and inputs built into the associated models have been placed in appropriate licensing and design deliverable documents.
4)A review of nuclear system directives (NSDs) will be conducted to determine whether the installation of a tent enclosure over a stairwell should have been controlled by the Engineering Change Program (NSD-301) or Temporary Structures Program (NSD-315).
5)Guidance for managing and controlling design passive features shall be developed and incorporated into work management processes.
There are no NRC commitment items contained in this LER.
SAFETY ANALYSIS
This event did not include a Safety System Functional Failure. The installation of the tent enclosure at the stairwell of Room 81 would have prevented adequate ventilation for removal of heat from 3B LPI Pump, 3B BS Pump, and associated motors. This could have resulted in the overheating and subsequent failure of the pumps and/or motors and loss of the B train of each safety system. The A train of these systems, however, remained fully operable and available for the entire duration of the event. Therefore, the effect of the inoperability in the B train would have been a loss of redundancy and failure to satisfy design basis single failure criteria for a period of time. Nevertheless, these systems would have been fully capable of mitigating the consequences of all Design Basis Accidents for which they were designed. There would have been no loss of system function as a result of this event.
The Low Pressure Injection (LPI) System is required to mitigate consequences of design basis Loss Of Coolant Accidents by providing emergency core cooling functions including safety injection and long term cooling of the reactor core. This system also provides for containment heat removal by transferring heat from the pool of water in the reactor building basement to the Low Pressure Service Water System through the Low Pressure Injection Heat Exchangers.
These functions provide protection for two fission product barriers, the fuel and the containment building.
The Reactor Building Spray System is required to mitigate the consequences of Loss of Coolant Accidents as well as secondary side pipe breaks (feedwater and main steam). This system removes heat from the containment atmosphere in conjunction with the Reactor Building Cooling Units, provides long term pressure control in containment, and removes fission product nuclides from post- accident containment atmosphere for severe accidents. Thus, the system functions to protect one fission product barrier, the containment building.
Since no system functions were lost during the reported event, all system functions of the LPI and BS systems would have been performed by the unaffected safety system train as designed.
Therefore, there would be no adverse effect on fission product barriers as a result of this event, and no impact to the health and safety of the public.
The core damage significance of this event has been evaluated quantitatively using the Oconee PRA Model Revision 3a considering actual maintenance unavailability during the period and the degraded cooling capacity for the LPI pump room. The PRA model was also modified to credit normal ventilation cooling for accident sequences in which it would be available. Temperature analysis of the room determined that the normal auxiliary building fans can provide adequate cooling even with the staircase sealed.
The incremental conditional core damage probability (ICCDP) associated with this event is estimated to be 7.6E-07, and the incremental conditional large early release probability (ICLERP) is estimated to be 4.3E-09. These results indicate that this event is of low risk significance. The dominant accident sequences involve either a loss of off-site power or loss of 3TC bus (4kV) initiating event. These events are important because power to the normal ventilation system is lost. A loss of all emergency feedwater sources leads to HPI forced cooling which later requires alignment to the containment sump when the BLAST inventory is depleted.
Note: This analysis did not take credit for restoration of normal ventilation flow following a loss of power. Additional human reliability analysis of these recovery actions or further enhancement of the temperature analysis could be expected to further reduce the estimated risk impact of this event. Therefore, these risk results are considered to be conservative.
The failure of Reactor Building Spray (RBS) System does not play an important role in the large early release frequency (LERF) and is not modeled in the OR3 Simplified LERF model. The long-term nature of this failure mode for the 3B RBS pump also means that the containment temperature and pressure control functions should be able to perform as intended for most LOCA initiating events.
Further, the Reactor Building Cooling Units (RBCUs) were not affected by the ventilation problem. Therefore, the impact of the inoperability of the 3B RBS pump is not considered in the analysis of the ICCDP and ICLERP because it is not expected to have any measurable risk impact.
ADDITIONAL INFORMATION
There were no releases of radioactive materials, radiation exposures or personnel injuries associated with this event.
This event is not considered reportable under the Equipment Performance and Information Exchange (EPIX) program.