05000298/LER-1981-003-03, /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter

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/03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter
ML20008F707
Person / Time
Site: Cooper Entergy icon.png
Issue date: 03/25/1981
From: Bednar L
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20008F704 List:
References
LER-81-003-03L, LER-81-3-3L, NUDOCS 8104210523
Download: ML20008F707 (1)


LER-1981-003, /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter
Event date:
Report date:
2981981003R03 - NRC Website

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.t***(FORM 366 ~

U.S. NUCLEAR REGULATORY COMMISSloN b

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60 61 DOCK ET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 burine S.P. 6.3.5.2. RHR-MO-26B motor acos increased and remained excessive 1v high I

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lared inoperable. No other significant occurrence took place. Re-l
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