Letter Sequence Other |
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Results
Other: A01024, Forwards Info Re Five Addl TMI-2 Related Requirements Applying to Operating Reactors Per 800507 Request.Integrated Assessment of Collective Impact of All Requirements Should Be Conducted, A02589, Forwards Addl Info Re safety-related ECCS Tank Outages, Provided Verbally on 821220 in Response to NUREG-0737, Item II.K.3.17, A03501, Requests Addl Time to Provide Info Re 6-inch Containment Purge & Vent Valve Operability.Info Will Be Provided by 831026, ML19340E921, ML20004B640, ML20008E564, ML20008F134, ML20054E184, ML20076A987, ML20078N847
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MONTHYEARML20076A9871979-04-27027 April 1979 Forwards Proposed Revision to Tech Specs to Allow Unlimited Containment Purges.Revisions Deal W/Containment Isolation Valves Project stage: Other A01024, Forwards Info Re Five Addl TMI-2 Related Requirements Applying to Operating Reactors Per 800507 Request.Integrated Assessment of Collective Impact of All Requirements Should Be Conducted1980-06-10010 June 1980 Forwards Info Re Five Addl TMI-2 Related Requirements Applying to Operating Reactors Per 800507 Request.Integrated Assessment of Collective Impact of All Requirements Should Be Conducted Project stage: Other ML19340E9211980-12-31031 December 1980 Forwards Rept on post-TMI Requirements in Response to NUREG-0737 & NRC Project stage: Other ML20008E5641981-02-27027 February 1981 Provides Justification for Min Containment Pressure Used to Initiate Containment Isolation for Facility,Per NRC 801231 Request Re NUREG-0737.Present Containment Isolation Setpoint Is Adequate & No Reduction in Setpoint Is Warranted Project stage: Other ML20008F1341981-03-0404 March 1981 Forwards ECCS Outage Rept for Facilities for 1980,in Response to NUREG-0737,Item II.K.3.17.No Sys or Tech Spec Mods Are Required Project stage: Other ML20004B6401981-05-20020 May 1981 Advises That No Mods Will Be Made to TMI Action Plan Item II.E.4.2 Re Containment Isolation Dependability.Signals Used for Containment Isolation Are Redundant & Diverse & Adequate to Ensure Safe Operation Project stage: Other A01845, Forwards Info Re NRC Orders Confirming Licensee Commitments on post-TMI Related Issues.Issues Have Been Addressed.If NRC Does Not Allow Util to Reserve Request for Hearing,Ltr Should Be Treated as Hearing Request1981-08-10010 August 1981 Forwards Info Re NRC Orders Confirming Licensee Commitments on post-TMI Related Issues.Issues Have Been Addressed.If NRC Does Not Allow Util to Reserve Request for Hearing,Ltr Should Be Treated as Hearing Request Project stage: Request ML20054E1841982-04-16016 April 1982 Forwards Responses to Generic Ltr 82-05 Re post-TMI Requirements Implementation.Continued Safe Operation Assured W/Existing Implementation Status Project stage: Other A02589, Forwards Addl Info Re safety-related ECCS Tank Outages, Provided Verbally on 821220 in Response to NUREG-0737, Item II.K.3.171982-12-29029 December 1982 Forwards Addl Info Re safety-related ECCS Tank Outages, Provided Verbally on 821220 in Response to NUREG-0737, Item II.K.3.17 Project stage: Other A03035, Forwards Response to NRC Request for Addl Info Re Operability of 6-inch Butterfly Containment Purge & Vent Valves.Based on Analyses,Adequate Justification Does Not Exist to Warrant Mods to Equipment1983-03-28028 March 1983 Forwards Response to NRC Request for Addl Info Re Operability of 6-inch Butterfly Containment Purge & Vent Valves.Based on Analyses,Adequate Justification Does Not Exist to Warrant Mods to Equipment Project stage: Request A03501, Requests Addl Time to Provide Info Re 6-inch Containment Purge & Vent Valve Operability.Info Will Be Provided by 8310261983-10-12012 October 1983 Requests Addl Time to Provide Info Re 6-inch Containment Purge & Vent Valve Operability.Info Will Be Provided by 831026 Project stage: Other ML20078N8471983-10-27027 October 1983 Forwards Response to NRC 830902 Comments on Unresolved Items Re Containment Purge/Vent Review.No Addl Tech Specs or Equipment Mods Warranted.Operability Requirement Met W/Compliance W/Tmi Item II.E.4.2 Project stage: Other A03992, Requests Informal Appeal Meeting W/Nrc to Review Requested Mod of Hydrogen Purge Valves to Close on High Radiation Signal,Per Generic Ltr 84-08 & NUREG-0737,Item II.E.4.2.71984-05-15015 May 1984 Requests Informal Appeal Meeting W/Nrc to Review Requested Mod of Hydrogen Purge Valves to Close on High Radiation Signal,Per Generic Ltr 84-08 & NUREG-0737,Item II.E.4.2.7 Project stage: Meeting A04104, Forwards Overview Re Appeal for Requested Mod of Hydrogen Purge Sys Valves to Close on Radiation Signal,Per Generic Ltr 84-08 & NUREG-0737,Item II.E.4.2.7, Containment Venting at Power. Addl Info Re Leakage Testing Expected by 8407301984-07-11011 July 1984 Forwards Overview Re Appeal for Requested Mod of Hydrogen Purge Sys Valves to Close on Radiation Signal,Per Generic Ltr 84-08 & NUREG-0737,Item II.E.4.2.7, Containment Venting at Power. Addl Info Re Leakage Testing Expected by 840730 Project stage: Other B11269, Forwards Figure 3.1,per Re NUREG-0737,Item II.E.4.2.7, Containment Venting at Power, Providing Justification That Isolation Logic for Hydrogen Purge Valves Adequate1984-07-13013 July 1984 Forwards Figure 3.1,per Re NUREG-0737,Item II.E.4.2.7, Containment Venting at Power, Providing Justification That Isolation Logic for Hydrogen Purge Valves Adequate Project stage: Other ML20133E7071985-10-0303 October 1985 Forwards Structural & Geotechnical Engineering Branch Request for Addl Info to Complete Review of 850724 Application to Modify Tech Specs Re Spent Fuel Storage Capacity Expansion Project stage: RAI B11777, Forwards Response to Request for Addl Info Re 850724 Application to Revise Tech Specs on Spent Fuel Storage Capacity1985-10-17017 October 1985 Forwards Response to Request for Addl Info Re 850724 Application to Revise Tech Specs on Spent Fuel Storage Capacity Project stage: Request ML20134A5991985-10-29029 October 1985 Notice of Consideration of Issuance of Amend to License DPR-65 & Proposed NSHC Determination & Opportunity for Hearing.Amend Authorizes Licensee to Increase Spent Fuel Pool Storage Capacity from 667 to 1,112 Storage Locations Project stage: Other ML20134A5871985-10-29029 October 1985 Forwards Notice of Consideration of Issuance of Amend to License DPR-65 & Proposed NSHC Determination & Opportunity for Hearing Re 850724 Application to Expand Spent Fuel Pool Storage Capacity Project stage: Other B11766, Submits Isap Topic 1.11, Post-Accident Hydrogen Monitor Per 850517 Commitment.Installation of Redundant Containment Hydrogen Monitor Unnecessary.Addl Info Will Be Provided by 8601311985-11-25025 November 1985 Submits Isap Topic 1.11, Post-Accident Hydrogen Monitor Per 850517 Commitment.Installation of Redundant Containment Hydrogen Monitor Unnecessary.Addl Info Will Be Provided by 860131 Project stage: Request B11889, Forwards Confirmation of Resolution to Request for Addl Info Re Application for Increased Spent Fuel Storage Capacity Based on Series of Telcons1985-11-25025 November 1985 Forwards Confirmation of Resolution to Request for Addl Info Re Application for Increased Spent Fuel Storage Capacity Based on Series of Telcons Project stage: Request B11893, Forwards Review of Spent Fuel Storage Capacity Expansion Request,Containing Proposed Mod to Tech Spec Re Decay Time Requirement,In Response to NRC 850826 Request for Addl Info1985-11-27027 November 1985 Forwards Review of Spent Fuel Storage Capacity Expansion Request,Containing Proposed Mod to Tech Spec Re Decay Time Requirement,In Response to NRC 850826 Request for Addl Info Project stage: Request B11910, Responds to Request for Addl Info Re Spent Fuel Storage Capacity.Analysis Showing That Adjacent Modules Do Not Contact During Seismic Event Inadvertently Omitted from1985-12-0303 December 1985 Responds to Request for Addl Info Re Spent Fuel Storage Capacity.Analysis Showing That Adjacent Modules Do Not Contact During Seismic Event Inadvertently Omitted from Project stage: Request ML20137B4321985-12-16016 December 1985 Notice of Environ Assessment & Finding of No Significant Impact Re Issuance of Amend to License DPR-65,changing Tech Specs to Increase Storage Capacity of Spent Fuel Pool Project stage: Approval ML20137B4231985-12-16016 December 1985 Forwards Environ Assessment & Finding of No Significant Impact Re 850724 Request for Amend to License DPR-65 Concerning Spent Fuel Pool Expansion Project stage: Other ML20137B4421985-12-16016 December 1985 Environ Assessment & Finding of No Significant Impact Supporting Amend to License DPR-65,authorizing Increase of Spent Fuel Pool Storage Capacity Project stage: Other ML20137A4901985-12-31031 December 1985 Forwards Addl Info Demonstrating Compliance w/NUREG-0737, Item II.E.4.2.7 Re Containment Venting Through Hydrogen Purge Valves,Per 840425,0902 & 1211 Requests Project stage: Other 1983-03-28
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May 20, 1981 Docket Nos. 50-213 50-245 50-336 AOl379 Mr. Darrell G. Eisenhut, Director Division of Licensing Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D.C.
20555
References:
(1)
D. G. Eisenhut letter to All Operating Plants and Applicants for Operating Licensees and IIolders of Construction Permits, dated October 31, 1980, forwardir, NUREG-0737.
(2)
W. G. Counril letter to D. G. Eisenhut, dated December 13 1980.
(3)
W. G. Counsil letter to D. L. Ziemann, dated April 27, 1979.
Gentlemen:
lladdam Neck Plant Millstone Nuclear Power Station, Unit Nos. 1 and 2 TMI Action Plan Item II.E.4.2; Containment Isolation Dependability l
l Position (7) of Item II.E.4.2 of Reference (1) states that containment purge and vent isolation valves mus' close on a high radiation signal.
Connecticut Yankee Atomic Power Company (CYAPCO), on behalf of the IIaddam Neck Plant, and Northeast Nuclear Evergy Company (NNECO), on behalf of Millstone Unit Nos. 1 and 2, are docketing this supplement to l
Reference (2) prior to the required implemer.tation date given in Reference (1) in order to respond to the Staff's concern.
The fladdam Neck Plant uses a purge and vent system to reduce airborne activity prior to commencement of refueling or other shutdown operation.
Normal Operating Procedure NOP 2-13-5 requires that the 42-inch purge l
valves and the 8-inch purge bypass valves be closed before containment integrity can be established. These valves are not opened during any operational modes, as the IIaddam Neck plant Technical Specifications require that containment integrity be maintained during operational modes. There is a 3/4-inch line which may be used to vent the containment l
8105 290 p/5 f
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,i 'N during operation to prevent pressure increases inside containment from exceeding the Limiting Condition for Operation. Since the Haddam Neck Plant is a four-loop plant which is licensed for three-loop operation, there have been times when work has been performed on the isolated loop inside containment during operation. The use of the breathing air system increases the internal containment pressure, and the 3/4-inch vent line may be used to relieve this pressure. The flow rate for this line is about 10 SCFM.
This line automatically isolates on receipt of a High Containment Pressure signal. This vent line has been used on less than five occassions in over 12 years of operation.
Since both the 42-inch and 8-inch purge valves are closed during operation and since the 3/4-inch vent line is rarely used, the requirement to close these valves on receipt of a high radiation signal is unnecessary.
As such, no modification is planned.
At Millstone Unit No.1, the drywell and torus may be vented or purged through either of two lines. The 18-inch lines are used almost exclusively for inerting and de-inerting the containment. Technical Specification 3.7. A.6 requires that the containment atmosphere oxygen concentration be reduced to less than 5% by weight within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period subsequent to placing the reactor in the run mode. De-inerting may commence 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to a shutdown.
Therefore, since the 18-inch valves are only allowed to be open for these short durations and remain closed when containment integrity is required, there would be no appreciable increase in safety by requiring that these valves automatically close on a high radiation signal. These valves automatically isolate on high drywell pressure or low reactor water level. The offsite dose consequences which would result from failure to isolate the purge exhaust valve, if open at the time of the accident,.were submitted in Reference (3).
The two-inch lines are opened periodically.to maintain the 1.0 psid pressure differential between the drywell and the torus and to control drywell oxygen concentration. Procedures require that exhaust from these lines be directed to the Standby Gas Trcatment System. Effluent i
to the stack is continuously monitored so that if exhaust from the two-inch lines were inadvertantly directed to the stack, it would automatically be directed to the Standby Gas Treatnent System if high radiation were detected. Since vent exhaust is directed to Ctandby Gas Treatment System, these lines do not provide an opcn path from the containment to l
the atmosphere. As clarified in telephone conversations between NRC l
Staff and representatives of General Electric and the BWR Owners Group, i
the high radiation signal should close any line that provides an open path from the containment to the environment. Therefore, this requirement does not apply to the two-inch vent valves.
NNECO has concluded that the signals used for containment isolation are redundant and diverse and are adequate to ensure the safe operation of Millstone Unit No. 1.
As such, no modifications to the containment isolation signals are planned.
l
A V
Millstone Uni No. 2 has two systems for purging and venting of the containment. The 42-inch butterfly valves on the large purge lines are locked closed during operational modes, as required by Amendment 61 to DPR-65.
The 6-inch vent valves automatically isolate on higi: containment pressure or low pressurizer pressure. NNECO has determined that these diverse signals are adequate to ensure that the vent valves will isolate when required, and as such, no modifications are planned.
In the event of a loss of coolant accident, the high containment pressure and low pressurizer pressure signals would precede a high radiation signal and
' isolate the containment. Thus, the addition of a high radiation signal is neither desirable nor necessary to ensure safe operation of Millstone Unit No. 2.
For these reasons, no modifications to the containment isolation logic at the Haddam Neck Plant or at Millstone Unit Nos. 1 and 2 are planned.
We trust this information adequately addresses the Staff's concern.
Very truly yours, CONNECTICUT YANKEE ATOMIC POWER COMPANY NORTHEAST NUCLEAR ENERGY COMPANY
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rW I 71 rl4 W. G. Counsil
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Senior Vice President
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