05000325/LER-1981-051-03, /03L-0:on 810422,investigation Revealed That 31- Day Surveillance Frequency for Verification of All Equipment Hatches Had Not Been Implemented.Caused by Oversight in Assessing Testing Requirements.Procedure Revised

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/03L-0:on 810422,investigation Revealed That 31- Day Surveillance Frequency for Verification of All Equipment Hatches Had Not Been Implemented.Caused by Oversight in Assessing Testing Requirements.Procedure Revised
ML20004B214
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 05/20/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004B207 List:
References
LER-81-051-03L, LER-81-51-3L, NUDOCS 8105270399
Download: ML20004B214 (1)


LER-1981-051, /03L-0:on 810422,investigation Revealed That 31- Day Surveillance Frequency for Verification of All Equipment Hatches Had Not Been Implemented.Caused by Oversight in Assessing Testing Requirements.Procedure Revised
Event date:
Report date:
3251981051R03 - NRC Website

text

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9 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h An investigation *to determine whether plant procedural controls adequately implement l

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