05000325/LER-1981-047-03, /03L-0:on 810422,during Testing of Type C Local Leak Rates,Primary Containment Isolation Valves 1-CAC-V7, V9,V15 & V17 Exceeded Leak Rate Limits.Caused by Corroded Valve Discs.Discs Will Be Replaced & Retested

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/03L-0:on 810422,during Testing of Type C Local Leak Rates,Primary Containment Isolation Valves 1-CAC-V7, V9,V15 & V17 Exceeded Leak Rate Limits.Caused by Corroded Valve Discs.Discs Will Be Replaced & Retested
ML20004B202
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 05/20/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004B194 List:
References
LER-81-047-03L-01, LER-81-47-3L-1, NUDOCS 8105270384
Download: ML20004B202 (1)


LER-1981-047, /03L-0:on 810422,during Testing of Type C Local Leak Rates,Primary Containment Isolation Valves 1-CAC-V7, V9,V15 & V17 Exceeded Leak Rate Limits.Caused by Corroded Valve Discs.Discs Will Be Replaced & Retested
Event date:
Report date:
3251981047R03 - NRC Website

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