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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045G7881993-07-0101 July 1993 LER 93-004-00:on 930602,discovered Potential Torus Condition Outside Design Basis.Caused by Inadequate Design Info. Documentation Procedures Revised.Torus Calculations to Include Peak Pressure info.W/930701 Ltr ML20028H6911991-01-21021 January 1991 LER 90-016-00:on 901220,senior Reactor Operator Licensed Group Shift Supervisor Left Control Room W/O Replacement, Resulting in Lack of Operator in Control Room for 4 Minutes. Both Operators Returned to Control room.W/910121 Ltr ML20044B3831990-07-12012 July 1990 LER 90-007-00:on 900614,discovered That Numerous Fire Detection Instruments Exceeded Max Allowable Interval for 6-month Operability Test.Caused by Personnel Error. Procedures for Surveillance Tests changed.W/900712 Ltr ML20043G0931990-06-0808 June 1990 LER 90-006-00:on 900511,average Power Level Exceeded Licensed Limit by Approx 1.64 MW When Cleanup Sys Placed in Svc W/O 7.84 MW Loss Added Into Heat Balance Calculation. Caused by Personnel Error.Procedures changed.W/900608 Ltr ML20043B1181990-05-18018 May 1990 LER 89-023-01:on 891209,four of Six Low Vacuum Scram Setpoints Found Out of Spec Due to Drift of Sensing Element & Lack of Margin for Drift in as-left Setpoint in Calibr Procedure.Instrument Setpoint adjusted.W/900518 Ltr ML20043A4281990-05-15015 May 1990 LER 90-025-01:on 891216,operator Inadvertently Selected Incorrect Control Rod,Then Selected Correct Rod When Error Realized.Second Control Room Operator Will Be Used to Assure That No Signal Failure Will Move Two rods.W/900515 Ltr ML20012D9441990-03-21021 March 1990 LER 90-004-00:on 900220,operation of hand-held Radio Near Analog Trip Units Caused Sys to Actuate & Air Operated Valves Repositioned.Caused by Personnel Error.Use of Radios Must Be Approved by Supervisor of technicians.W/900321 Ltr ML20012D1601990-03-14014 March 1990 LER 90-003-00:on 900215,seven Control Rods Withdrawn During Reactor Startup While Rod Minimizer Was Bypassed.Caused by Personnel Error.Withdrawal Stopped & Keylock Switch Placed in Normal position.W/900314 Ltr ML20012D1581990-03-14014 March 1990 LER 89-017-01:on 890711,main Generator Tripped Due to Phase Differential Condition Caused by Fault in Operating Maint Output Transformer.Caused by Equipment Failure.Oil Boxes on Transformers repaired.W/900314 Ltr ML20012A1731990-02-27027 February 1990 LER-89-023-00:on 891209,four Out of Six Condenser Low Vacuum Setpoints Found at Values Less Conservative than Tech Spec Limit.Caused by Sensing Element Drift & Lack of Margin for Drift in Calibr Procedure.Setpoint changed.W/900227 Ltr ML20011F4401990-02-22022 February 1990 LER 90-001-00:on 900123,fire Alarm Received for Fire Zone in Cable Spreading Room,Resulting in Operability of Deluge Sys. Continuous Fire Watch Not Established.Caused by Inadequate Procedural Guidance.Detectors disabled.W/900222 Ltr ML19354D8341990-01-12012 January 1990 LER 89-021-01:on 890922,ref Leg of Level Instrument Vented to Test Equipment,Causing False High Reactor Pressure Vessel Signal.Caused by Trip of Turbine Generator Resulting in Scram.Excess Flow Check Valve depressurized.W/900112 Ltr ML19327C0661989-11-0606 November 1989 LER 89-022-00:on 891005,Tech Spec Violation Occurred When Licensed Group Shift Supervisor Left Control Room W/O Informing Operating Supervisor.Caused by Personnel Error. Individual Involved counseled.W/891106 Ltr ML19351A4161989-10-13013 October 1989 LER 89-020-00:on 890915,operator Trainee Identified That Knife Switch Used to Select Dc Control Power Source for 480 Volt Ac Unit Substation 1B2 Was Selected.Caused by Procedural Inadequacy.Lineup Sheet used.W/891013 Ltr ML19327A8081989-10-11011 October 1989 LER 89-019-00:on 890911,emergency Diesel Generator Became Inoperable.Caused by Dirt on Wiper of Motorized Potentiometer in Peaking Load Control Circuit & Latent Heat Expansion of Engine.Fuel Injectors replaced.W/891011 Ltr ML19327B4961989-09-23023 September 1989 LER 89-021-00:on 890922,false High Reactor Pressure Vessel Water Level Caused Turbine Generator Trip & Reactor Scram. Caused by Personnel Not Following Surveillance Procedure.All Involved Instruments Calibr checked.W/891023 Ltr ML20028G4431983-01-28028 January 1983 LER 82-063/03L-0:on 821227,operability of Control Rod Drive Pump a Not Demonstrated During 1-month Period.Caused by Breakdown in Administrative Controls for Surveillance Test Program.Surveillance Completed ML20028G2361983-01-28028 January 1983 LER 82-064/03L-0:on 821230,containment Spray Sys 1 Declared Inoperable Due to High Baffle Plate Differential Pressure Readings on 1-2 Hx.Caused by HX Fouling.Hx Inspected & Cleaned & Chlorination Sys for Emergency Svc Water Repaired ML20028E7741983-01-20020 January 1983 LER 82-061/03L-0:on 821216,offgas Isolation Valve Failed to Close Fully on Independent Closure Signal.Caused by Defective Pilot Solenoid Valves Due to Foreign Matter on Solenoid Valve Seat Prohibiting Termination of Air Supply ML20028C7991982-12-29029 December 1982 LER 82-058/03L-0:on 821128,main Steam Line Drain Valves V-1-106 & V-1-110 Failed to Close Fully.Cause Unknown. Investigation Will Continue During Next Outage ML20028C7541982-12-27027 December 1982 LER 82-059/03L-0:on 821124,reactor Circulation Pump a Taken Out of Svc.Caused by Indications of Leaking Seals.Seal Confirmed to Be Leaking During Subsequent Shutdown. Cartridge Assembly Replaced ML20027B9151982-09-16016 September 1982 LER 82-046/03L-0:on 820815,controls Keeping Main Line Drain Valves Deactivated in Isolation Position Were Defeated Prior to Temp Dropping Below 212 F.Caused by Personnel Error.Personnel Reinstructed ML20052E6541982-05-0303 May 1982 LER 82-021/01T-0:on 820416,containment Oxygen Concentration Not Reduced within 24-h After Run Mode & Drywell to Torus Differential Pressure Greater than 1 Psi.Caused by Loss of 6-h Inerting Time Due to Insufficient Nitrogen ML20052E2161982-04-28028 April 1982 LER 82-017/03L-0:on 820325,normal Auxiliary Power Bus 1C Relay Failed Totally & Svc Water Pump Trip Time Delay Relay SK8A Failed to Operate within Tech Spec Limits.Power Bus Failure Caused by Normal End of Life ML20052B0941982-04-16016 April 1982 LER 82-020/01T-0:on 820328,MSIV Leak Rate Testing Disclosed Deterioration of Valve Internals on NS03-A & Packing Leak on Outboard Valve NS04-A.Caused Not stated.NS03-A Disassembled & repaired.NS04-A Repacked ML20052G0011982-04-16016 April 1982 LER 82-021/01P:on 820416,primary Containment Atmosphere Not Reduced to Less than 5% Oxygen within 24-h After Reactor Mode Selector Switch Placed in Run Position.Caused by Insufficient Nitrogen & Blown Rupture Disc ML20050D9091982-03-29029 March 1982 LER 82-013/03L-0:on 820128,low Voltage Annunciator Relay Setting for Main Station Batteries B & C & Diesel Generator 2 Battery Relay & Setting Found Below Tech Specs Limit. Caused by Annunciation Setpoints Out of Spec ML20050A5051982-03-19019 March 1982 LER 82-008/03L-0:on 820210,monthly Channel Check of Secondary (Thermocouples) Safety & Relief Valve Position Monitoring Sys Not Performed as Required by Tech Spec. Caused by Lack of Administrative & Procedural Controls ML20042B2951982-03-15015 March 1982 LER 82-012/01P-0:on 820226,air Operated Vacuum Breaker V-26-18 Exceeded Allowable Leak Rate.Caused by Improper Alignment of Valve Shaft & Operator Due to Inadequate Maint Instructions.Valve Realigned & Procedures Will Be Revised ML20042B3141982-03-12012 March 1982 LER 82-009/03L-0:on 820210,overload Trip Occurred on Standby Gas Treatment Sys Exhaust Fan 1-8.Apparently Caused by Change in Breaker Trip Setpoint.Further Testing Underway ML20042A6281982-03-10010 March 1982 LER 82-011/03L-0:on 820208,three Hydraulic Snubbers Were Inoperable & Accelerated Surveillance of Tech Spec 4.5.0.3 Was Not Performed.Caused by Component Failure.Snubbers Replaced W/Certified Operable Snubbers ML20042A2941982-03-0505 March 1982 LER 81-071/01T-0:on 811231,radwaste Liquid Effluent Monitor Found Inoperable.Proper Surveillance Not Performed.Caused by Personnel Error & Lack of Administrative & Procedural Controls.Control Procedures Written & Parts Replaced ML20042A1131982-03-0404 March 1982 LER 82-010/01T-0:on 820218,deluge Sys for Reactor Bldg Elevation 51 Ft Actuated Due to Smoke from Overheated Bearing in Cleanup Sys Auxiliary Pump Motor.Caused by Inadequate Electrical Sealing Techniques ML20052G0281982-03-0101 March 1982 LER 82-012/01P:on 820226,reactor Bldg to Suppression Chamber Vacuum Breaker Valve V-26-18 Found Improperly Installed. Caused by Inadequate Procedure.Valve Shaft Realigned ML20041D8071982-02-26026 February 1982 LER 82-006/01T-0:on 811203,one Trip Sys in Automatic Depressurization Sys Rendered Inoperable by Removal of Dc Control Power Fuses.Caused by Nonrating of Microswitches Inside IA83-A Replacement.All EMRV Switches Replaced ML20041D8021982-02-25025 February 1982 LER 82-007/03L-0:on 820126,main Steam Line High Flow Sensor RE-22H Tripped at Greater Value than Given in Tech Specs. Caused by Instrument Repeatability & Drift.Sensor Reset & Setpoints Lowered ML20041D7821982-02-25025 February 1982 LER 82-005/03L-0:on 820125,during Load Surveillance Test, Diesel Generator 1-1 Tripped on Engine Fault.Caused by Reduction of Water Inventory in Cooling Sys as Result of Radiator Tube Leak.Leaky Tubes Plugged ML20041D4681982-02-22022 February 1982 LER 82-004/03L-0:on 820121,reactor Bldg Closed Cooling Water Drywell Isolation Valve V-5-167 Failed to Fully Close.Caused by Lack of Stem/Stem Nut Lubrication &/Or Packing Problem. Stem,Stem Nut & Bearing Lubricated & Valve Repacked ML20041D5801982-02-19019 February 1982 LER 82-002/03L-0:on 820118,installation of Mod Could Have Led to Possible Failure to Maintain Primary Containment Integrity.Change Defeated Automatic Withdrawal Function 3 & 4 TIP Detectors.Caused by Inadequate Safety Review ML20041D3791982-02-19019 February 1982 LER 82-003/03L-0:on 820122,containment Spray High Drywell Pressure Indicating Switch IP25B Found to Trip at Value Greater than Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset ML20041A2231982-02-0505 February 1982 LER 81-061/03L-0:on 811223,nine Snubbers on Core Spray, Containment Spray,Isolation Condenser & Shutdown Cooling Sys Determined Inoperable Due to Oil Leakage.Cause to Be Determined.Snubbers Replaced W/Operable Spares ML20040F5301982-02-0101 February 1982 LER 82-001/03L-0:on 820128,during Testing,Containment Spray High Drywell Pressure Indicating Switches IP15A,IP15B & IP15C Found to Trip at Values Greater than Tech Spec Limits. Caused by Instrument Repeatability.Switches Reset ML20040F4831982-01-28028 January 1982 LER 81-070/03L-0:on 811231,isolation Condenser Isolation Pipe Break Sensor IB11A1 Tripped Above Tech Spec Limit. Caused by Instrument Repeatability.Setpoint Lowered.Switches Will Be Replaced During Future Refueling Outage ML20040F5201982-01-28028 January 1982 LER 81-072/03L-0:on 811229,core Spray Sys I Parallel Isolation Valve V-20-15 Became Inoperable in Partially Open Position.Caused by High Motor Current Drawn When Valve Close Signal Inadvertently Intiated During Valve Stroking ML20040E4281982-01-26026 January 1982 LER 81-069/03L-0:on 811230,during Surveillance Testing,Core Spray High Drywell Pressure Switches RV-46A,RV-46B & RV-46D Tripped.Caused by Instrument Repeatability.Switches Reset. Setpoint Changed to Reflect Inherent Design Error ML20040D7551982-01-20020 January 1982 LER 81-067/03L-0:on 811220,during Maint Testing,Scram Pilot Solenoid Valve 118 (for Control Rod Drive 14-23) Failed When Rod Was Individually Scrammed.No Plausible Cause Could Be Postulated.All Scram Solenoids Will Be Verified Operable ML20040C6631982-01-18018 January 1982 LER 81-068/03L-0:on 811218,reactor Triple Low Water Level Indicator Switch RE18A Tripped at Monometer Reading Exceeding Tech Spec Limit.Caused by Instrument Drift.Switch Reset.Setpoint Sensors Will Be Replaced ML20040B1501981-12-31031 December 1981 LER 81-066/03L-0:on 811201,during Surveillance Testing,Main Steam Line High Flow Sensors RE22C,RE22E & RE22F Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability & Drift.Sensors Reset ML20039G0981981-12-23023 December 1981 LER 81-065/01T-0:on 811209,shutdown Commenced to Investigate a Isolation Condenser Isolation Valve V-14-30 811203 & 04 Failure to Operate Properly.Caused by Excessive Stress on Valve Backseat & Damage to Stem Nut ML20039G1891981-12-23023 December 1981 LER 81-062/03L-0:on 811125,core Spray Hi Drywell Pressure Switch RV46C Tripped in Excess of Tech Spec Limit.Caused by Sensor Repeatability.Sensor Recalibr 1993-07-01
[Table view] Category:RO)
MONTHYEARML20045G7881993-07-0101 July 1993 LER 93-004-00:on 930602,discovered Potential Torus Condition Outside Design Basis.Caused by Inadequate Design Info. Documentation Procedures Revised.Torus Calculations to Include Peak Pressure info.W/930701 Ltr ML20028H6911991-01-21021 January 1991 LER 90-016-00:on 901220,senior Reactor Operator Licensed Group Shift Supervisor Left Control Room W/O Replacement, Resulting in Lack of Operator in Control Room for 4 Minutes. Both Operators Returned to Control room.W/910121 Ltr ML20044B3831990-07-12012 July 1990 LER 90-007-00:on 900614,discovered That Numerous Fire Detection Instruments Exceeded Max Allowable Interval for 6-month Operability Test.Caused by Personnel Error. Procedures for Surveillance Tests changed.W/900712 Ltr ML20043G0931990-06-0808 June 1990 LER 90-006-00:on 900511,average Power Level Exceeded Licensed Limit by Approx 1.64 MW When Cleanup Sys Placed in Svc W/O 7.84 MW Loss Added Into Heat Balance Calculation. Caused by Personnel Error.Procedures changed.W/900608 Ltr ML20043B1181990-05-18018 May 1990 LER 89-023-01:on 891209,four of Six Low Vacuum Scram Setpoints Found Out of Spec Due to Drift of Sensing Element & Lack of Margin for Drift in as-left Setpoint in Calibr Procedure.Instrument Setpoint adjusted.W/900518 Ltr ML20043A4281990-05-15015 May 1990 LER 90-025-01:on 891216,operator Inadvertently Selected Incorrect Control Rod,Then Selected Correct Rod When Error Realized.Second Control Room Operator Will Be Used to Assure That No Signal Failure Will Move Two rods.W/900515 Ltr ML20012D9441990-03-21021 March 1990 LER 90-004-00:on 900220,operation of hand-held Radio Near Analog Trip Units Caused Sys to Actuate & Air Operated Valves Repositioned.Caused by Personnel Error.Use of Radios Must Be Approved by Supervisor of technicians.W/900321 Ltr ML20012D1601990-03-14014 March 1990 LER 90-003-00:on 900215,seven Control Rods Withdrawn During Reactor Startup While Rod Minimizer Was Bypassed.Caused by Personnel Error.Withdrawal Stopped & Keylock Switch Placed in Normal position.W/900314 Ltr ML20012D1581990-03-14014 March 1990 LER 89-017-01:on 890711,main Generator Tripped Due to Phase Differential Condition Caused by Fault in Operating Maint Output Transformer.Caused by Equipment Failure.Oil Boxes on Transformers repaired.W/900314 Ltr ML20012A1731990-02-27027 February 1990 LER-89-023-00:on 891209,four Out of Six Condenser Low Vacuum Setpoints Found at Values Less Conservative than Tech Spec Limit.Caused by Sensing Element Drift & Lack of Margin for Drift in Calibr Procedure.Setpoint changed.W/900227 Ltr ML20011F4401990-02-22022 February 1990 LER 90-001-00:on 900123,fire Alarm Received for Fire Zone in Cable Spreading Room,Resulting in Operability of Deluge Sys. Continuous Fire Watch Not Established.Caused by Inadequate Procedural Guidance.Detectors disabled.W/900222 Ltr ML19354D8341990-01-12012 January 1990 LER 89-021-01:on 890922,ref Leg of Level Instrument Vented to Test Equipment,Causing False High Reactor Pressure Vessel Signal.Caused by Trip of Turbine Generator Resulting in Scram.Excess Flow Check Valve depressurized.W/900112 Ltr ML19327C0661989-11-0606 November 1989 LER 89-022-00:on 891005,Tech Spec Violation Occurred When Licensed Group Shift Supervisor Left Control Room W/O Informing Operating Supervisor.Caused by Personnel Error. Individual Involved counseled.W/891106 Ltr ML19351A4161989-10-13013 October 1989 LER 89-020-00:on 890915,operator Trainee Identified That Knife Switch Used to Select Dc Control Power Source for 480 Volt Ac Unit Substation 1B2 Was Selected.Caused by Procedural Inadequacy.Lineup Sheet used.W/891013 Ltr ML19327A8081989-10-11011 October 1989 LER 89-019-00:on 890911,emergency Diesel Generator Became Inoperable.Caused by Dirt on Wiper of Motorized Potentiometer in Peaking Load Control Circuit & Latent Heat Expansion of Engine.Fuel Injectors replaced.W/891011 Ltr ML19327B4961989-09-23023 September 1989 LER 89-021-00:on 890922,false High Reactor Pressure Vessel Water Level Caused Turbine Generator Trip & Reactor Scram. Caused by Personnel Not Following Surveillance Procedure.All Involved Instruments Calibr checked.W/891023 Ltr ML20028G4431983-01-28028 January 1983 LER 82-063/03L-0:on 821227,operability of Control Rod Drive Pump a Not Demonstrated During 1-month Period.Caused by Breakdown in Administrative Controls for Surveillance Test Program.Surveillance Completed ML20028G2361983-01-28028 January 1983 LER 82-064/03L-0:on 821230,containment Spray Sys 1 Declared Inoperable Due to High Baffle Plate Differential Pressure Readings on 1-2 Hx.Caused by HX Fouling.Hx Inspected & Cleaned & Chlorination Sys for Emergency Svc Water Repaired ML20028E7741983-01-20020 January 1983 LER 82-061/03L-0:on 821216,offgas Isolation Valve Failed to Close Fully on Independent Closure Signal.Caused by Defective Pilot Solenoid Valves Due to Foreign Matter on Solenoid Valve Seat Prohibiting Termination of Air Supply ML20028C7991982-12-29029 December 1982 LER 82-058/03L-0:on 821128,main Steam Line Drain Valves V-1-106 & V-1-110 Failed to Close Fully.Cause Unknown. Investigation Will Continue During Next Outage ML20028C7541982-12-27027 December 1982 LER 82-059/03L-0:on 821124,reactor Circulation Pump a Taken Out of Svc.Caused by Indications of Leaking Seals.Seal Confirmed to Be Leaking During Subsequent Shutdown. Cartridge Assembly Replaced ML20027B9151982-09-16016 September 1982 LER 82-046/03L-0:on 820815,controls Keeping Main Line Drain Valves Deactivated in Isolation Position Were Defeated Prior to Temp Dropping Below 212 F.Caused by Personnel Error.Personnel Reinstructed ML20052E6541982-05-0303 May 1982 LER 82-021/01T-0:on 820416,containment Oxygen Concentration Not Reduced within 24-h After Run Mode & Drywell to Torus Differential Pressure Greater than 1 Psi.Caused by Loss of 6-h Inerting Time Due to Insufficient Nitrogen ML20052E2161982-04-28028 April 1982 LER 82-017/03L-0:on 820325,normal Auxiliary Power Bus 1C Relay Failed Totally & Svc Water Pump Trip Time Delay Relay SK8A Failed to Operate within Tech Spec Limits.Power Bus Failure Caused by Normal End of Life ML20052B0941982-04-16016 April 1982 LER 82-020/01T-0:on 820328,MSIV Leak Rate Testing Disclosed Deterioration of Valve Internals on NS03-A & Packing Leak on Outboard Valve NS04-A.Caused Not stated.NS03-A Disassembled & repaired.NS04-A Repacked ML20052G0011982-04-16016 April 1982 LER 82-021/01P:on 820416,primary Containment Atmosphere Not Reduced to Less than 5% Oxygen within 24-h After Reactor Mode Selector Switch Placed in Run Position.Caused by Insufficient Nitrogen & Blown Rupture Disc ML20050D9091982-03-29029 March 1982 LER 82-013/03L-0:on 820128,low Voltage Annunciator Relay Setting for Main Station Batteries B & C & Diesel Generator 2 Battery Relay & Setting Found Below Tech Specs Limit. Caused by Annunciation Setpoints Out of Spec ML20050A5051982-03-19019 March 1982 LER 82-008/03L-0:on 820210,monthly Channel Check of Secondary (Thermocouples) Safety & Relief Valve Position Monitoring Sys Not Performed as Required by Tech Spec. Caused by Lack of Administrative & Procedural Controls ML20042B2951982-03-15015 March 1982 LER 82-012/01P-0:on 820226,air Operated Vacuum Breaker V-26-18 Exceeded Allowable Leak Rate.Caused by Improper Alignment of Valve Shaft & Operator Due to Inadequate Maint Instructions.Valve Realigned & Procedures Will Be Revised ML20042B3141982-03-12012 March 1982 LER 82-009/03L-0:on 820210,overload Trip Occurred on Standby Gas Treatment Sys Exhaust Fan 1-8.Apparently Caused by Change in Breaker Trip Setpoint.Further Testing Underway ML20042A6281982-03-10010 March 1982 LER 82-011/03L-0:on 820208,three Hydraulic Snubbers Were Inoperable & Accelerated Surveillance of Tech Spec 4.5.0.3 Was Not Performed.Caused by Component Failure.Snubbers Replaced W/Certified Operable Snubbers ML20042A2941982-03-0505 March 1982 LER 81-071/01T-0:on 811231,radwaste Liquid Effluent Monitor Found Inoperable.Proper Surveillance Not Performed.Caused by Personnel Error & Lack of Administrative & Procedural Controls.Control Procedures Written & Parts Replaced ML20042A1131982-03-0404 March 1982 LER 82-010/01T-0:on 820218,deluge Sys for Reactor Bldg Elevation 51 Ft Actuated Due to Smoke from Overheated Bearing in Cleanup Sys Auxiliary Pump Motor.Caused by Inadequate Electrical Sealing Techniques ML20052G0281982-03-0101 March 1982 LER 82-012/01P:on 820226,reactor Bldg to Suppression Chamber Vacuum Breaker Valve V-26-18 Found Improperly Installed. Caused by Inadequate Procedure.Valve Shaft Realigned ML20041D8071982-02-26026 February 1982 LER 82-006/01T-0:on 811203,one Trip Sys in Automatic Depressurization Sys Rendered Inoperable by Removal of Dc Control Power Fuses.Caused by Nonrating of Microswitches Inside IA83-A Replacement.All EMRV Switches Replaced ML20041D8021982-02-25025 February 1982 LER 82-007/03L-0:on 820126,main Steam Line High Flow Sensor RE-22H Tripped at Greater Value than Given in Tech Specs. Caused by Instrument Repeatability & Drift.Sensor Reset & Setpoints Lowered ML20041D7821982-02-25025 February 1982 LER 82-005/03L-0:on 820125,during Load Surveillance Test, Diesel Generator 1-1 Tripped on Engine Fault.Caused by Reduction of Water Inventory in Cooling Sys as Result of Radiator Tube Leak.Leaky Tubes Plugged ML20041D4681982-02-22022 February 1982 LER 82-004/03L-0:on 820121,reactor Bldg Closed Cooling Water Drywell Isolation Valve V-5-167 Failed to Fully Close.Caused by Lack of Stem/Stem Nut Lubrication &/Or Packing Problem. Stem,Stem Nut & Bearing Lubricated & Valve Repacked ML20041D5801982-02-19019 February 1982 LER 82-002/03L-0:on 820118,installation of Mod Could Have Led to Possible Failure to Maintain Primary Containment Integrity.Change Defeated Automatic Withdrawal Function 3 & 4 TIP Detectors.Caused by Inadequate Safety Review ML20041D3791982-02-19019 February 1982 LER 82-003/03L-0:on 820122,containment Spray High Drywell Pressure Indicating Switch IP25B Found to Trip at Value Greater than Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset ML20041A2231982-02-0505 February 1982 LER 81-061/03L-0:on 811223,nine Snubbers on Core Spray, Containment Spray,Isolation Condenser & Shutdown Cooling Sys Determined Inoperable Due to Oil Leakage.Cause to Be Determined.Snubbers Replaced W/Operable Spares ML20040F5301982-02-0101 February 1982 LER 82-001/03L-0:on 820128,during Testing,Containment Spray High Drywell Pressure Indicating Switches IP15A,IP15B & IP15C Found to Trip at Values Greater than Tech Spec Limits. Caused by Instrument Repeatability.Switches Reset ML20040F4831982-01-28028 January 1982 LER 81-070/03L-0:on 811231,isolation Condenser Isolation Pipe Break Sensor IB11A1 Tripped Above Tech Spec Limit. Caused by Instrument Repeatability.Setpoint Lowered.Switches Will Be Replaced During Future Refueling Outage ML20040F5201982-01-28028 January 1982 LER 81-072/03L-0:on 811229,core Spray Sys I Parallel Isolation Valve V-20-15 Became Inoperable in Partially Open Position.Caused by High Motor Current Drawn When Valve Close Signal Inadvertently Intiated During Valve Stroking ML20040E4281982-01-26026 January 1982 LER 81-069/03L-0:on 811230,during Surveillance Testing,Core Spray High Drywell Pressure Switches RV-46A,RV-46B & RV-46D Tripped.Caused by Instrument Repeatability.Switches Reset. Setpoint Changed to Reflect Inherent Design Error ML20040D7551982-01-20020 January 1982 LER 81-067/03L-0:on 811220,during Maint Testing,Scram Pilot Solenoid Valve 118 (for Control Rod Drive 14-23) Failed When Rod Was Individually Scrammed.No Plausible Cause Could Be Postulated.All Scram Solenoids Will Be Verified Operable ML20040C6631982-01-18018 January 1982 LER 81-068/03L-0:on 811218,reactor Triple Low Water Level Indicator Switch RE18A Tripped at Monometer Reading Exceeding Tech Spec Limit.Caused by Instrument Drift.Switch Reset.Setpoint Sensors Will Be Replaced ML20040B1501981-12-31031 December 1981 LER 81-066/03L-0:on 811201,during Surveillance Testing,Main Steam Line High Flow Sensors RE22C,RE22E & RE22F Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability & Drift.Sensors Reset ML20039G0981981-12-23023 December 1981 LER 81-065/01T-0:on 811209,shutdown Commenced to Investigate a Isolation Condenser Isolation Valve V-14-30 811203 & 04 Failure to Operate Properly.Caused by Excessive Stress on Valve Backseat & Damage to Stem Nut ML20039G1891981-12-23023 December 1981 LER 81-062/03L-0:on 811125,core Spray Hi Drywell Pressure Switch RV46C Tripped in Excess of Tech Spec Limit.Caused by Sensor Repeatability.Sensor Recalibr 1993-07-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
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. OYSTER CREEK NUCIEAR GENERATING STATION Ebrked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/81-04/0lT Peport Date i
January 30, 1981 Occu m. Date i
i January 16, 1981 1
2 Identification of Occurrence i.
i Becent studies have indicated that the load on the Butu.yacy Diesel Generators,- I l during an actual Ioss of Coolant Accident (IDCA) with a loss of off-site power plus a single bus failure, oculd exceed the full load rating of 2500 KW.
i 'Ihis event is considered a reportable occurrence as defined in the Technical
{ Specifications, paragraph 6.9.2.a(9) .
Conditions Prior to Occurrence
)' Not applicable. r i
Description of Occurrence 3 Due to future anticipated load expansion at the Oyster Creek Station a study was l undertaken to document the present load profiles on all power buses throughout-1 the plant under several operating configurations. One aspect of this ' study
. performed for Jersey Central Power and Light included Maxinun Denand Safety Bus i loading during the IOCA and Ioss of Offsite pcwer scenario. Preliminary data pre-
- . sented to JCP&L indicated that a potE.ntial' exists for substantially overloading the diesel generator above its emergency rating of 2750 KW. 'Ihis result disagrees with measured inMing during annual testing and previously subnitted analysis to the NBC.
The primary differences are attributed to the use of nameplate data in addition to the inclusion of all non-safety connected load in the maximtrn demand study, therefore, resulting in highly ccnservative projections. Since the new calculational method introduces recognized conservatisms due to estimated or j nameplate load vs actual load conditions it was determined necessary to use i
demonstrated loss of power test results with aMM factors accounting for single failures and possible runout values. - The maxinun load experienced during any loss of power test at Oyster Creek was 2460 KW under postulated IOCA conditions,
< with loss of offsite power,. and one assuned diesel generator failure. To this L load an additional 219.4 KW was aMM to account for the aMM ' load resulting l- fran runout flows expected on Core Spray and Con + aim =nt Spray Systems for a t total of 2679.4 KW on Diesel Generator #2 (which is the most limiting case) .
This calculated total exceeds the continuous full load rating of 2500 KW for the a diesel generators.
Apparent Cause of Occurrence 1
3'
'Ihe cause of .this occurrence was attributed to differences in- the methods used to calculate the diesel generator loads,'during a IDCA with a loss of offsite power and 'a single bus failure, during a recent study as ccupared to _an analysis perfhmM during the Oyster Creek ECCS modification in 1975.
_ . . - . _ . _ , _ _..-... _ ,_ _ _ ,._ _. _ _. __,,._.a . ~ . , _ .. . _ . . _ _-
Reportable Occurrence Page 2 Report No. 50-219/81-04/0lT Analysis of Occurrence The nest limiting diesel generator load was found to be 2460 W on DG 2 which was detemined during loss of power testing. The procedure used to perform the loss of somr test is set up such that it reflects expected load conditions seen during a IDCA with a single failure. This single failure is a simulation of one faulted bus or diesel generator. However, certain pumps in the safety related systems muld be operating at " runout" ficw under accident conditions (approximated by using nameplate ratings) instead of rated systs flows which are those measured during the test. Assuming this occurs the difference between design pump load and nameplate load must be added to the actaal load of 2460 KW.
Another factor that must be included in the analysis is the load addal by smaller power panels in the distribution systs. Since these power panels will nomally transfer to other buses during the loss of pomr tests, these loads are not included in the expected value of 2460 KW. The total of these power panel loads was determined to be 80 KW. The suntrary of these calculations is as follows:
Actual Largest Diesel Ioad (with single failure) 2460 KW Transferable Power Panels 80 KW Two (2) Core Spray Booster Pumps (runout differential) 62.4 KW Two (2) Core Spray Main Pump (runout differential) 24.6 KW one (1) Containment Spray Pump (runout differential) 52.4 KW Total I. cad 2679.4 KW
'Ihis value compares satisfactorily with an allowable peak load rating of 2750 KW. Although the manufacturer will allow operation at 2750 KW for 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> per year (a virtual " continuous" rating as applied at Oyster Creek), aaaitional margin was provided by issuing a Standing Order requiring the cperators to trip the Peactor Building Closed Cooling Water Pumps and Service Water Pumps, follow-ing diesel generator. load sequencing, in the event of a IDCA with a loss of off-site power, since these loads are unnecessary in that scenario. The net effect of these actions would be to reduce the load on the diesel generator by 336 KW to a total of 2343.4 KW which is less than the continuous load rating of 2500 KW for the diesel generators.
Corrective Action i
A Standing Order has been issued which reqaires the operators to trip the Reactor Building Closed Cooling Water (RBOCW) and Service Water (SW) pumps after load sequencing following a TACA with a loss of offsite power. This action reduces the load on the most limiting Diesel Generator to less than the full load rating of 2500 KW (assuming one diesel generator fails) .
-her anticipated corrective actions include performing a study to install under voltage devices on non-essential loads and to install a modification which will prevent the RBCrW and SW pumps from starting during load sequencing under IDCA conditions.
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