LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl |
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OYSTER CREEK NUCLEAR GENERATING STATION imRgW (609)693-6000 P O BOX 388
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Mr. Boyce H. Grier, Director N
B Office of Inspection and Enforcment S-h Region I g U G 0 5 19a; u --
United States Nuclear Regulatory Ccmnission
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631 Park Avenue b
s King of Prussia, Pennsylvania 19406 i'O Th
Dear Mr. Grier:
SUBJECT: Oyster Creek Nuclear Generating Station Docket No. 50-219 Licensee Event Report Reportable Occurrence No. 50-219/81-24/3L This letter forwards three copies of a Licensee Event Report to report Reportable Occurrence No. 50-219/81-24/3L in cmpliance with paragraphs 6.9.2.b.2 and 6.9.2.b.3 of the Technical Specifications.
Very truly yours, an R. Finf Jr.
ice President - JCP&L Director - Oyster Creek IRF:dh Enclosures cc: Director (40 copies)
Office of Inspection and Enf'rcment United States Nuclear Regul a ry Ca mission Washington, D.C.
20555 Director (3)
Offi of Managmient Information
//f and Program Control United States Nuclear Regulatory Cmrtission Washington, D. C. 20555
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NBC Resident Inspector (1)
Oyster Creek Nuclear Generating Station Forked River, N. J.
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OYSTER CREEK NUCLEAR G m ERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/81-24/3L Report Date July 8, 1981 Occurrence Date June 8, 1981 Identification of Occurrence The plant was operating in a degraded mode as permitted by a limiting condition for operation as given in Tcchnical Specification paragraph 3.4.C.4, when two Emergency Service Water pumps were found to be inoperable, and the required operability check of the operable pumps was not performed in the time period specified.
This event is considercd to be a reportable occurrence as defined in the Technical Specifications, paragraphs 6.9.2.b.2 and 6.9.2.b.3.
Conditions Prior to Occurrence The plant was operating at steady state power.
Major Plant Parameters Power:
Reactor 1081 b5ft Generator 310 F54e 4
Flow:
Recirculation 12.0xlglb/hr p
3.5 x 10 Feedwater Description of Occurrence At approximately 12:35 A.M. on June 8, an operability check of the Emergency Service Water pumps was performcx1 due to grass clogging probleus at the intake structure. Pump 52B was found to have unacceptable motor current, and pump 52C was found to have unacceptable discharge pressure.
(Based on acceptance criteria given in the Containnent Spray and Emergency Service Water Pump Operability Test procedure, 607.4.001). The rcmaining pumps, 52A in Systan I and 52D in Systan II, met the acceptance criteria.
After discussion with the NBC Resident Inspector, at approximately 11:30 A.M.
on June 9, an operability check was again performed on the four ESW pumps (approximately 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br /> after the first operability check). Once again pumps 52B (Systan I) and 52C (Systen II) failed to meet acceptance criteria, and 52A and 52D were operable.
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Reportable Occurrence Page 2 Peport No. 50-219/81-24/3L On June 10, the four pumps were again tested, and in addition to measuring notor current and pump discharge pressure, the systan flow was measured using ultrasonic measuring equipnent. Based on the fact that each pump delivered nore than the acceptable flow r: te, the four ESW pumps were then considered operable. The test data for the three (3) days is as follows:
June 8 ESW Pump Disch. Pressure (psig)
Current (amps) i 52A 100 51 52B 100
- 95 51 52D 115 55 June 9 j
ESW Pump Disch. Pressure (psig)
Current (amps) 52A 100 51 52B
52C
- 97 51 52D 140 54 June 10 ESW Pump Disch. Pressure (psig)
Current (amps) Flow (ggn) 52A 100 50.5 3420 52B
- 95 51 3750 52D 115 53.5 4000 Acceptable Limits:
>100 psig pressure 53 + 3 amps current
> 3000 gpn flow (design flow)
- Denotes unacceptable values Apparent Cause of Occurrence i
Following the June 8 testing of the ESW pumps and after a managenent review of the test data, it was decidal to consider the pumps with questionable i
rmaings operable. This decision was based on past experience of poor correlation between I: ump flow and pressure / current readings. At the same time, engineers were assigned to evaluate the test data and conduct flow tests in order to verify the status of the pumps in question.
Subsequently, it was found that pump flows were well within acceptable limits and in fact the pumps were operable. Additionally, it was found that the amneter on the 'B' pump was faulty ard slight clogging of the pump suctions of 'B' and 'C' pump contributed to the low discharge pressure rmaings.
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Reportable u,Ct.irence Page 3 Report No. 50-219/81-24/3L Analysis of Occurrence The Containment Spray and Dnergency Service Water Systes are engineered safety systems designed to rmove fission product decay heat frm the primary containment in the event of a loss of coolant accident. There are two independent syst e s used to accmplish this, with each systs having redundant pumps, each capable of performing the safety function. The systes are designed so that a single Containment Spray pump and a single Dnergency Service Water pump can provide the necessary cooling.
In this case, the safety significance is minimized by the fact that the redundant punp in each systs was operable (52A in Systm I and 52D in Systm II). Based on this, the systs would have been aale to perform - designed function in the event of a IOCA. It should also be noted that the a,of June 10 shows that the punps are still capable of delivering rated flow even with the low current or pressure.
Corrective Action
Since the time of the occurrence, the faulty anneter has been replaced. Emergerg Service Water pumps 52B and 52C were rmoved and the suction bells were cleaned.
Testing perfonned after this maintenance yielded current and pressure readings which were all within acceptable limits.
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Currently, engineers have been assigned to provide flow instrumentation on this systs in order to provide positive indication of pump operability. In the interim, the pump testing procedure and pump acceptance criteria are being evaluated in order to determine possible changes to provide better irrlication of actual operability status.
In the future when a question on equipnent operability arises as a result of surveillance data or other conditions that can't be inenrhtely dispostioned, a conservative approach will be taken and the subject equignent declared inoperable and the appropriate surveillance performed as required by Technical Specification:
until resolved.
Failure Data l
Manufacturer - Byron Jackson Type -
Vertical-Centrifugal, 3000 gyn,1770 RPM
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| 05000219/LER-1981-001-03, /03L-0:on 810102,containment Spray Sys High Drywell Pressure Indicating Switch IP-15C Tripped Above Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset & Study Examining Causes of Repeatability Undertaken | /03L-0:on 810102,containment Spray Sys High Drywell Pressure Indicating Switch IP-15C Tripped Above Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset & Study Examining Causes of Repeatability Undertaken | | | 05000219/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000219/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000219/LER-1981-002-03, /03L-0:on 810102,gaseous Releases to Stack Found Not Continuously Monitored as Required by Tech Spec.Caused by Tripping of Stack Gas Sample Pump Due to Normal Wear.Pump Replaced W/Spare | /03L-0:on 810102,gaseous Releases to Stack Found Not Continuously Monitored as Required by Tech Spec.Caused by Tripping of Stack Gas Sample Pump Due to Normal Wear.Pump Replaced W/Spare | | | 05000219/LER-1981-003-03, /03L-0:on 810112,during Visual Insp of Fire Hydrants,Hydrant 2 Found to Contain Frozen Water in Barrel, Rendering Hydrant Inoperable.Caused by Water Leaking from Hydrant Valve & Freezing in Barrel.Hydrant Thawed | /03L-0:on 810112,during Visual Insp of Fire Hydrants,Hydrant 2 Found to Contain Frozen Water in Barrel, Rendering Hydrant Inoperable.Caused by Water Leaking from Hydrant Valve & Freezing in Barrel.Hydrant Thawed | | | 05000219/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000219/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000219/LER-1981-004-01, /01T-0:on 810116,studies Indicated That Emergency Diesel Generators May Exceed Load Rating During Accident Conditions.Caused by Using Different & More Conservative Methods to Calculate Load.Actions to Reduce Load Underway | /01T-0:on 810116,studies Indicated That Emergency Diesel Generators May Exceed Load Rating During Accident Conditions.Caused by Using Different & More Conservative Methods to Calculate Load.Actions to Reduce Load Underway | | | 05000219/LER-1981-005-03, /03L-0:on 810106,emergency Svc Water Pump 52B Current & Discharge Pressure Found Outside Tech Spec. Probably Caused by Clogged Pump Suction Strainer.Strainer Cleared | /03L-0:on 810106,emergency Svc Water Pump 52B Current & Discharge Pressure Found Outside Tech Spec. Probably Caused by Clogged Pump Suction Strainer.Strainer Cleared | | | 05000219/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000219/LER-1981-006-03, /03L-0:on 810115,during Surveillance Testing, Reactor Triple Low Water Level Indicator Switch RE-18B Tripped at Monometer Reading Higher than Allowed by Tech Spec Table 3.1.1.Caused by Instrument Drift.Switch Reset | /03L-0:on 810115,during Surveillance Testing, Reactor Triple Low Water Level Indicator Switch RE-18B Tripped at Monometer Reading Higher than Allowed by Tech Spec Table 3.1.1.Caused by Instrument Drift.Switch Reset | | | 05000219/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000219/LER-1981-007-03, /03L-0:on 810202,water-tight Door to Containment Spray Sys I Compartment Not Closed & Verification of Closed Door Not Performed.Caused by Personnel Error & Lack of Controls to Ensure Doors Are Closed After Passage | /03L-0:on 810202,water-tight Door to Containment Spray Sys I Compartment Not Closed & Verification of Closed Door Not Performed.Caused by Personnel Error & Lack of Controls to Ensure Doors Are Closed After Passage | | | 05000219/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000219/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000219/LER-1981-008-03, /03L-0:on 810210,water Seepage Observed Along West Wall of Nrw Bldg.Direct Survey Showed Detectable Ground Contamination Only within 6 Inches of Wall.Caused by High Levels in Tank Vaults.Herculite Secured & Sealed to Wall | /03L-0:on 810210,water Seepage Observed Along West Wall of Nrw Bldg.Direct Survey Showed Detectable Ground Contamination Only within 6 Inches of Wall.Caused by High Levels in Tank Vaults.Herculite Secured & Sealed to Wall | | | 05000219/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000219/LER-1981-009-03, /03L-0:on 810213,snubber 23/3 Found W/Very Low Oil Level & Oil Discovered on Floor at Base Connection During NRC walk-around Insp.Caused by Failure of Inner Shaft Seal Due to Deterioration.Snubber Replaced W/Operable Spare | /03L-0:on 810213,snubber 23/3 Found W/Very Low Oil Level & Oil Discovered on Floor at Base Connection During NRC walk-around Insp.Caused by Failure of Inner Shaft Seal Due to Deterioration.Snubber Replaced W/Operable Spare | | | 05000219/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000219/LER-1981-010-03, /03L-0:on 810202,during Routine Surveillance Testing,Main Steamline High Radiation Monitor RN-06B Tripped at Value Higher That Tech Spec Limits.Caused by Failure to Revise Trip Settings.Trip Settings Lowered | /03L-0:on 810202,during Routine Surveillance Testing,Main Steamline High Radiation Monitor RN-06B Tripped at Value Higher That Tech Spec Limits.Caused by Failure to Revise Trip Settings.Trip Settings Lowered | | | 05000219/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-011-03, /03L-0:on 810309,isolation Condenser Condensate Return Line Pipe Break Sensor IB11B2 Found to Trip at Value Greater than That Specified in Tech Specs.Caused by Instrument Repeatability.Replacement Recommended | /03L-0:on 810309,isolation Condenser Condensate Return Line Pipe Break Sensor IB11B2 Found to Trip at Value Greater than That Specified in Tech Specs.Caused by Instrument Repeatability.Replacement Recommended | | | 05000219/LER-1981-012-03, /03L-0:on 810313,electromatic Relief Valve High Pressure Actuation Switches 1A83C & 1A83E Tripped Higher than Limit Specified in Tech Spec.Caused by Instrument Repeatability.Pressure Sensors Reset to Trip within Limits | /03L-0:on 810313,electromatic Relief Valve High Pressure Actuation Switches 1A83C & 1A83E Tripped Higher than Limit Specified in Tech Spec.Caused by Instrument Repeatability.Pressure Sensors Reset to Trip within Limits | | | 05000219/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-013-03, /03L-0:on 810319,core Spray Hi Drywell Pressure Switch RV46B Tripped in Excess of 2 Psi Tech Spec.Caused by Sensor Repeatability.Sensor Recalibr.Replacement of Sensors Recommended by PORC | /03L-0:on 810319,core Spray Hi Drywell Pressure Switch RV46B Tripped in Excess of 2 Psi Tech Spec.Caused by Sensor Repeatability.Sensor Recalibr.Replacement of Sensors Recommended by PORC | | | 05000219/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-014, Forwards LER 81-014/01T-0.Detailed Event Analysis Encl | Forwards LER 81-014/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-014-01, /01T-0:on 810401,containment Oxygen Concentration Was Not Reduced to Less than 5% within 24-h After Placing Reactor Mode Switch in Run.Caused by Inerting at Significantly Reduced Rates | /01T-0:on 810401,containment Oxygen Concentration Was Not Reduced to Less than 5% within 24-h After Placing Reactor Mode Switch in Run.Caused by Inerting at Significantly Reduced Rates | | | 05000219/LER-1981-015-03, /03L-0:on 810324,main Steam Line High Flow Sensors Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability.Both Sensors Reset | /03L-0:on 810324,main Steam Line High Flow Sensors Tripped at Values Greater than Tech Specs Limit.Caused by Instrument Repeatability.Both Sensors Reset | | | 05000219/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-016-03, /03L-0:on 810421,approx 10,000 Gallons of Leakage from Condensate Transfer Pump Bldg Was Discovered on North & South Sides of Bldg.Caused by Loss of Valve Packing on V-2-88.Leakage Was Diked & Valve Repacked | /03L-0:on 810421,approx 10,000 Gallons of Leakage from Condensate Transfer Pump Bldg Was Discovered on North & South Sides of Bldg.Caused by Loss of Valve Packing on V-2-88.Leakage Was Diked & Valve Repacked | | | 05000219/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000219/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-017-03, /03L-0:on 810415,one Containment Spray Sys Loop Considered Inoperable During Normal Operation.Caused by Large Amount of Sea Lettuce in Intake Canal,Overwhelming Trash Removal Sys.Circulating Water Pump Stopped | /03L-0:on 810415,one Containment Spray Sys Loop Considered Inoperable During Normal Operation.Caused by Large Amount of Sea Lettuce in Intake Canal,Overwhelming Trash Removal Sys.Circulating Water Pump Stopped | | | 05000219/LER-1981-018, Forwards LER 81-018/01T-0.Detailed Event Analysis Encl | Forwards LER 81-018/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-018-01, /01T-0:on 810417,equipment Operator Found Valves Were Blocked from Fully Opening by Scaffolding Placed by Contractor Personnel.Caused by Personnel Error.Scaffolding Repositioned | /01T-0:on 810417,equipment Operator Found Valves Were Blocked from Fully Opening by Scaffolding Placed by Contractor Personnel.Caused by Personnel Error.Scaffolding Repositioned | | | 05000219/LER-1981-019-03, /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised | /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised | | | 05000219/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000219/LER-1981-020-03, /03L-0:on 810501,isolation Condenser Shell Level Instrument IGO6B Found Reading High During Annual Calibr. Caused by Evaporation of Instrument Ref Column.Column Backfilled W/Water to Normal Operating Level | /03L-0:on 810501,isolation Condenser Shell Level Instrument IGO6B Found Reading High During Annual Calibr. Caused by Evaporation of Instrument Ref Column.Column Backfilled W/Water to Normal Operating Level | | | 05000219/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-021-03, /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage | /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage | | | 05000219/LER-1981-022-01, /01T-0:on 810520,secondary Containment Integrity Not Maintained Due to Personnel Access Airlock Doors Ajar. Caused by Personnel Error & Loosened Striker Plate on Inside Door.Outside Door Closed & Striker Plate Repaired | /01T-0:on 810520,secondary Containment Integrity Not Maintained Due to Personnel Access Airlock Doors Ajar. Caused by Personnel Error & Loosened Striker Plate on Inside Door.Outside Door Closed & Striker Plate Repaired | | | 05000219/LER-1981-022, Forwards LER 81-022/01T-0 | Forwards LER 81-022/01T-0 | | | 05000219/LER-1981-023-03, /03L-0:on 810603,drywell Vented to Reduce Drywell Torus Differential Pressure.Caused by Moisture Buildup in Sensing Line Resulting in Erroneous Indication of Increased Oxygen Concentration.Procedures Will Be Reviewed | /03L-0:on 810603,drywell Vented to Reduce Drywell Torus Differential Pressure.Caused by Moisture Buildup in Sensing Line Resulting in Erroneous Indication of Increased Oxygen Concentration.Procedures Will Be Reviewed | | | 05000219/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-024-03, /03L-0:on 810608,while Operating in Degraded Mode, Two Emergency Water Pumps Found Inoperable.Caused by Faulty Ammeter,Clogged Pump Suction Bells & Inadequate Administrative Controls.Ammeter Replaced & Bells Cleaned | /03L-0:on 810608,while Operating in Degraded Mode, Two Emergency Water Pumps Found Inoperable.Caused by Faulty Ammeter,Clogged Pump Suction Bells & Inadequate Administrative Controls.Ammeter Replaced & Bells Cleaned | | | 05000219/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1981-025-01, /01T-0:on 810617,secondary Containment Was Broken When Both Reactor Bldg Railroad Airlock Doors Were Opened Together.Caused by Failure of Top Inner Door Latch & Operator Error.Operators Will Be Reinstructed | /01T-0:on 810617,secondary Containment Was Broken When Both Reactor Bldg Railroad Airlock Doors Were Opened Together.Caused by Failure of Top Inner Door Latch & Operator Error.Operators Will Be Reinstructed | | | 05000219/LER-1981-025, Forwards LER 81-025/01T-0.Detailed Event Analysis Encl | Forwards LER 81-025/01T-0.Detailed Event Analysis Encl | |
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