05000325/LER-1981-021-03, /03L-0:on 810126,control Rod Scram Accumulators 46-15 & 30-07 Determined Inoperable Due to Inoperable Internal Leakage Detectors.Caused by Sticking Level Switch Floats in Detectors.Both Level Switches Replaced

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/03L-0:on 810126,control Rod Scram Accumulators 46-15 & 30-07 Determined Inoperable Due to Inoperable Internal Leakage Detectors.Caused by Sticking Level Switch Floats in Detectors.Both Level Switches Replaced
ML19341D008
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/19/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341D005 List:
References
LER-81-021-03L, LER-81-21-3L, NUDOCS 8103040693
Download: ML19341D008 (1)


LER-1981-021, /03L-0:on 810126,control Rod Scram Accumulators 46-15 & 30-07 Determined Inoperable Due to Inoperable Internal Leakage Detectors.Caused by Sticking Level Switch Floats in Detectors.Both Level Switches Replaced
Event date:
Report date:
3251981021R03 - NRC Website

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EVENT DESCnlPTIO'l AND PROU AOLE CONSEQUENCES h E l During the performance of control rod drive accumulator Icak detection instru g l calibration and functional tc3t, P.T.1.7.1PC, control rod scram accumula l

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1-12-81 The failure of the magnetic analy:cr sample cell was a result of corrosion in the analy:cr intake screen that was caused by excessive moisture in the analyzer sample lipe. Due to a history of similar problems involving this type of analyzer, a plant modification has been written to replace these monitors with those of a more reliable design during a future scheduled

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