LER-1980-010, /01T-0:on 800516,during Cold Pressure Test,Leakage Discovered at Gasket Joint Between Pump Casing & Pump Cover on Reactor Coolant Pumps RC-3A,3B & 3C.Closure Studs Corroded by Boric Acid.Leaks Caused by Deteriorated Gaskets |
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UCENSEE EVENT REPORT o-CONTROL BLOCK: l l
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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo !2I l A cold pressure test was being performed on the RCS prior to unit startup. Test l
4 I o 131 I pressure was approximately 180 psig.
Leakage was discovered at the gasketed joint l
lo i4 l l between the pump casing and the pump cover on reactor coolant pumps RC-3A, 38, and I !
IoIsl I 3C.
S ibsequent inspection revealed that significant corrosion damage had occurred l
1o le i I to a number of the closure studs on all three pumps.
No Technical Specification i
l o 17 I I LC0's were violated as a result of this condition.
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9 to 11 12 13 18 19 20 SEQU ENTI AL OCCURRENCE REPORT REVISION LE R RO EVENT YE AR RE80RT NO.
CODE TYPE NO.
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33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTICNS 11 101 L ! aakage fecm tho onmos was found to be caused bv detarioration of the Flexitallic I
li ll i l oaskets.
Damaca to the closure studs is believed to have been caused by boric acid 1 It i2II attack.
The affected cumos were disassenbled. the defective caskets reolaced, and I
l i 131 I new studs installed as recuired.
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% POWER OTHER STATUS 015 0 Y
DISCOVERY DESCRIPTION I1 45I[3]@ l0l0l0l@l NA l
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DESCRIPTION
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PERSONN E L INJLRt ES NUMBER DIESCRIPTION li la l l O l O l 2 l@l Minor ini:' ries occurred durino reoair of oumos l
7 8 9 11 12 80 LOSS CF OR OA '. *ME TO FACILITY
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LER 80-010 Omaha Public Fow::r District Fort Calhoun Station Unit No.1 Docket No. 05000285 ATTACHMENT NO. 1
Safety Analysis
It is probable that the corrosion damage to the reactor coolant pump closure studs did not occur over a short period of time and must have existed prior to the refueling shutdown.
However, even with the damaged studs discovered during this inspection, the 1 gpm reactor coolant system leak rate limit discussed in the Technical Specifica-tions was not exceeded during power operation.
The pump cover is secured to the pump casing by means of 16 closure studs.
The createst stud damage was observed on pump RC-3B; 3 of the studs were substantially corroded with a minimum diameter of 1 to 1-1/2" (original diameter of approximately 3-1/2") and a fourth stud exhibited significant corrdsion, although the stress area was not markedly decreased.
Durin'g disassembly of the pump, all but one of these studs were subjected to a stress of 23,500 psi without failure.
It is evident that, since normal operation of the reactor coolant pumps did not cause failure of any studs, the corroded studs were not overstressed even with the reduced stress area.
It is concluded that the gasket leakage and corrosion damage which occurred on the reactor coolant pumps did not create a con-dition which jeopardized the health and safety of the public or District personnel.
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LER 80-010 Omaha Public Power District Fort Calhoun Station Unit No. 1 Docket No. 05000285 ATTACHMENT NO. 2 Cause Description / Corrective Actions On the evening of May 15, 1980, plant operating personnel were performing a cold pressure test of the reactor coolant system prior to plant startup.
The primary system was pressurized to approxi-mately 180 psig using one low pressure safety injection pump.
A routine primary system leakage inspection by operations personnel revealed leakage coming from reactor coolant pump RC-3C.
At this time the low pressure safety injection pump was secured.
On the morning of May 16, 1980, the system was again pressurized using the low pressure safety injection pump.
An inspection by mainte-nance personnel revealed leakage from the shaft seal on pump RC-3C.
This seal was subsequently tightened which reduced but did not eliminate the leakage.
Further investigation revealed leakage emanating from the gasketed surface between the pump casing and the pump cover. At this time, technical assistance was requested from the pump manufacturer, Bryan Jackson.
On the afternoon of May 16, the other three reactor coolant pumps RC-3A, RC-3B, and RC-3D were inspected.
Leakage was found to be coming from RC-3A and RC-38.
In addition, it was noted that corrosion damage had occurred to a number of the closure studs on pumps RC-3A and RC-3B.
No stud damage was evident on RC-3D.
The corrosion had occurred on the exposed shank of the studs.
The pump cover and the pump casing for each reactor coolant pump are constructed of ASTM A-351, Grade CFSM stainless steel.
Sealing between the pump cover and the pump casing is accomplished by means of two concentric 304 stainless steel Flexitallic gaskets.
The cover is secured to the pump casing by 16 closure studs con-structed of ASTM A-193, Grade B7 carbon steel, chrome plated in the thread area, and phosphate coated in the shank area.
The studs are approximately 3-1/2" in diameter and approximately 29" in length.
During assembly the studs are hydraulically tensioned to approximately 23,500 psi.
The residual stress in the studs, when they are held by the nuts, is approximately 15,500 psi.
A leakoff line is included between the two Flexitallic gaskets; this line was originally blanked off with a pipe plug.
To aid in determining the source of the leakage, the leakoff line for each pump was unplugged ard the system was repressurized to approxi-mately 180 psig.
Pump RC-3A showed. slight leakage through the leakoff line.
Pumps RC-3B and RC-3C showed considerably more leakage.
No leakage was noted for RC-3D.
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The covers were removed from pumps RC-3A, RC-38, and RC-3C.
The Flexitallic geskets were inspected and it was determined that deterioration of the gaskets was apparent in some cases. Where deterioration was apparent, it was in the form of loss of asbestos filler, not catastrophic failure.
The gasketed surfaces for all three pumps were in good condition with no evidence of steam erosion. \\
LER 80-010 Omaha Public Power District i
Fort Calhoun Station Unit No. 1 Docket No. 05000285 ATTACHMENT NO. 2 (Continued)
Following removal, the 48 used studs were subjected to ultra-sonic, magnetic particle, and visual examinations.
A stud was considered to be acceptable for further service if the ASME Section XI acceptance criteria were met and if corrosion had not reduced the minimum diameter to less than 3.320" (the minimum acceptable diameter for new studs).
The following is the final status on the studs removed from service.
Number of Studs Reason for Rejection RC-3A RC-3B RC-3C Excessive corrcsion 4
8 6
Other unacceptable indications 2
2 0
E III T
It is emphasized that, of the studs rejected for excessive cor-rosion, only 3 studs on RC-3A and 4 studs on RC-3B were severely corroded (minimum diameter in the 1 to 1-1/2" range).
Full hydraulic tensioner pressure of 4500 psi (stud stress of 23,500 psi) was re-i quired for removal of 47 of the 48 studs; one stud on RC-3A fractured at a tensioner pressure of 3000 psi (stud stress of 15,500 psi).
The affected pumps were reassembled using new studs as required and new Flexitallic gaskets.
The nuts were visually inspected prior to reinstallation and one was replaced owing to excessive thread damage.
The closure studs for RC-3A and RC-3B were ultrasonically inspected during the 1980 refueling outage.
The studs were examined from the top surface using a straight beam longitudinal wave search unit at a nominal search frequency of 2.25 MHz.
No recordable indications were revealed. A visual examination of the shank of the studs was not performed since it was not known that the shank portions of the studs were accessible.
Following discovery of the corroded studs, the ultrasonic examination was repeated; once again, no recordable indications were revealed.
In order to preclude future stud damage and unidentified gasket failures, a number of preventive measures have been adopted.
- First, the leakoff lines between the primary and secondary gaskets have been connected to pressure transmitters so that leakage past the primary gaskets will be detected.
Second, the accessible portions of the pump closure studs will be visually inspected at least once per fuel cycle.
(The accessible portions were, in all cases, the portions susceptible to corrosion damage.)
The original insulation for the pumps has been replaced by insulation which will allow better inspection of the studs.
Third, further investigation will be con-ducted in an attempt to ascertain the precise mechanisms responsible for the stud damage.
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9 LER 80-010 Omaha Public Power District Fort Calhoun Station Unit No.1 Docket No. 05000385 ATTACHMENT NO. 2 (Continued)
In order to ensure that wetting of the old insulation did not create the possibility of chloride attack to the pump casing, samples of old insulation were analyzed for Cl, Na+, and SiO2 concentration.
In all instances, the analyses verified that the insuTat:en met the acceptance criteria in Regulatory Guide 1.36.
In addition, a sample area of pump casing was liquid penetrant inspected to confirm that no evidence of stress corrosion cracking had occurred.
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LER 80-010 Omaha Public Power District Fort Calhoun Station Unit No.1 Docket No. 05000285 ATTACHMENT N0. 3 Failure Data No problems had occurred previously with the reactor coolant pump gaskets or studs.
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| 05000285/LER-1980-001-03, /03L-0:800102,while Operating at Approx 98% Power, Breaker Feeding Containment Cooling Fan Motor VA-3B Tripped.Caused by Trip Units Out of Calibr.Units A&C Were Replaced,Calibr & Tested Satisfactorily | /03L-0:800102,while Operating at Approx 98% Power, Breaker Feeding Containment Cooling Fan Motor VA-3B Tripped.Caused by Trip Units Out of Calibr.Units A&C Were Replaced,Calibr & Tested Satisfactorily | | | 05000285/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000285/LER-1980-002-01, /01T-0:on 800117,while Performing Surveillance Test ST-SI/CS-1,containment Sump Safety Injection Recirculation Valve HCV-383-4 Failed to Close from Control Room Switch.Caused by Binding Auxiliary Interlock | /01T-0:on 800117,while Performing Surveillance Test ST-SI/CS-1,containment Sump Safety Injection Recirculation Valve HCV-383-4 Failed to Close from Control Room Switch.Caused by Binding Auxiliary Interlock | | | 05000285/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000285/LER-1980-003-03, /03L-0:on 800122,during Special 24-h Diesel Generator Test,While Attempting to Load Generator,Generator Field Went to Max Excitation.Caused by Faulty Zener Diode & Corresponding Draft in A-C Regulator Panel | /03L-0:on 800122,during Special 24-h Diesel Generator Test,While Attempting to Load Generator,Generator Field Went to Max Excitation.Caused by Faulty Zener Diode & Corresponding Draft in A-C Regulator Panel | | | 05000285/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000285/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000285/LER-1980-004-01, /01T-0:on 800126,while Fire Barrier Inside Empty Breaker Cubicle Was Degraded to Pull in New Cabling,Fire Watch Was Not Maintained Continuously.Caused by Fire Watch Not Receiving Accurate Info on Status of Barrier | /01T-0:on 800126,while Fire Barrier Inside Empty Breaker Cubicle Was Degraded to Pull in New Cabling,Fire Watch Was Not Maintained Continuously.Caused by Fire Watch Not Receiving Accurate Info on Status of Barrier | | | 05000285/LER-1980-005-03, /03L-0:on 800131,during Containment Integrated Leak Rate Test,Release to Atmosphere Occurred.Caused by Failure of Rupture Disk.Containment Pressure Monitored for Remainder of Test | /03L-0:on 800131,during Containment Integrated Leak Rate Test,Release to Atmosphere Occurred.Caused by Failure of Rupture Disk.Containment Pressure Monitored for Remainder of Test | | | 05000285/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000285/LER-1980-006-01, /01T-0:on 800415,as Required by IE Bulletin 79-01B,util Has Been Obtaining & Reviewing Test Data on Electrical Equipment.Samples Failed to Meet Acceptance Criteria.Caused by Steam & Moisture in Environ | /01T-0:on 800415,as Required by IE Bulletin 79-01B,util Has Been Obtaining & Reviewing Test Data on Electrical Equipment.Samples Failed to Meet Acceptance Criteria.Caused by Steam & Moisture in Environ | | | 05000285/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000285/LER-1980-007-01, /01T-0:on 800430,penetration Cable Splices for Containment Ventilation Fans Found to Lack Documentation for LOCA Qualification.Splices Will Be Coated w/LOCA-qualified Sealant | /01T-0:on 800430,penetration Cable Splices for Containment Ventilation Fans Found to Lack Documentation for LOCA Qualification.Splices Will Be Coated w/LOCA-qualified Sealant | | | 05000285/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000285/LER-1980-008-03, /03L-0:on 800515,during Check of Power Supply Trip Indicating lights,AB-1 Matrix Relay of Reactor Protective Sys Failed to Trip Clutch Power Supplies.Caused by Failure of Mercury Wetted Relay in Matrix Circuit | /03L-0:on 800515,during Check of Power Supply Trip Indicating lights,AB-1 Matrix Relay of Reactor Protective Sys Failed to Trip Clutch Power Supplies.Caused by Failure of Mercury Wetted Relay in Matrix Circuit | | | 05000285/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000285/LER-1980-009-99, /99T-0:on 800522,during Maint on Stack Iodine Process Monitor,New Sensitivity Calibr Was Required.Caused by Use of Wrong Calibr Procedure.Training Will Be Conducted to Ensure Familiarity W/Procedures | /99T-0:on 800522,during Maint on Stack Iodine Process Monitor,New Sensitivity Calibr Was Required.Caused by Use of Wrong Calibr Procedure.Training Will Be Conducted to Ensure Familiarity W/Procedures | | | 05000285/LER-1980-009, Forwards LER 80-009/99T-0 | Forwards LER 80-009/99T-0 | | | 05000285/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000285/LER-1980-010-01, /01T-0:on 800516,during Cold Pressure Test,Leakage Discovered at Gasket Joint Between Pump Casing & Pump Cover on Reactor Coolant Pumps RC-3A,3B & 3C.Closure Studs Corroded by Boric Acid.Leaks Caused by Deteriorated Gaskets | /01T-0:on 800516,during Cold Pressure Test,Leakage Discovered at Gasket Joint Between Pump Casing & Pump Cover on Reactor Coolant Pumps RC-3A,3B & 3C.Closure Studs Corroded by Boric Acid.Leaks Caused by Deteriorated Gaskets | | | 05000285/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000285/LER-1980-011-03, /03L-0:on 800528,during 1980 Refueling Outage Type B & C Containment Leak Rate Tests,Total Leakage Exceeded 0.6La Limit.Caused by Leaking Fuel Transfer Tube, Electrical,Mechanical Sleeve & Piping Penetrations | /03L-0:on 800528,during 1980 Refueling Outage Type B & C Containment Leak Rate Tests,Total Leakage Exceeded 0.6La Limit.Caused by Leaking Fuel Transfer Tube, Electrical,Mechanical Sleeve & Piping Penetrations | | | 05000285/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000285/LER-1980-012-03, /03L-0:on 800708,during Performance of ST-RPS-3, F.2,discovered That Trip Unit 3 Setpoints Had Drifted Out of Spec in Nonconservative Direction.Caused by Normal Setpoint Drift.Setpoints Adjusted | /03L-0:on 800708,during Performance of ST-RPS-3, F.2,discovered That Trip Unit 3 Setpoints Had Drifted Out of Spec in Nonconservative Direction.Caused by Normal Setpoint Drift.Setpoints Adjusted | | | 05000285/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000285/LER-1980-013-03, /03L-0:on 800707,during Normal Power Operation, Noted That Channel a Dc Sequencer SI-1 Had de-energized on-auto Light.Caused by Sequencer Circuitry Failure Due to Faulty Relay | /03L-0:on 800707,during Normal Power Operation, Noted That Channel a Dc Sequencer SI-1 Had de-energized on-auto Light.Caused by Sequencer Circuitry Failure Due to Faulty Relay | | | 05000285/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000285/LER-1980-014-03, /03L-0:on 800709,transformer T4 of Diesel Generator 1 Failed.Caused by Shorted Coil.Transformer Replaced | /03L-0:on 800709,transformer T4 of Diesel Generator 1 Failed.Caused by Shorted Coil.Transformer Replaced | | | 05000285/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000285/LER-1980-015-03, /03L-0:on 800710,during Insp,Noted That Trip Unit Setpoints on C Channel Had Become Positive Rather than Negative.Caused by Failure of 15-volt Power Supply for Trip Unit 4.Unit Calibr | /03L-0:on 800710,during Insp,Noted That Trip Unit Setpoints on C Channel Had Become Positive Rather than Negative.Caused by Failure of 15-volt Power Supply for Trip Unit 4.Unit Calibr | | | 05000285/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000285/LER-1980-016-03, /03L-0:on 800621,weld on Suction Side of Pump CH-1B in Demineralized Water Flush Line Cracked.Caused by Vibration of Piping in Svc.Crack Was Ground Out & Rewelded Using Certified Procedure & Line Tested | /03L-0:on 800621,weld on Suction Side of Pump CH-1B in Demineralized Water Flush Line Cracked.Caused by Vibration of Piping in Svc.Crack Was Ground Out & Rewelded Using Certified Procedure & Line Tested | | | 05000285/LER-1980-017-03, /03L-0:on 800804,during Normal Power Operation, Personnel Discovered Setpoint Selector Switches for RMO-61, Particulate Radiation Monitor,In Wrong Position.Caused by Personnel Error While Performing Test on Radiation Monitor | /03L-0:on 800804,during Normal Power Operation, Personnel Discovered Setpoint Selector Switches for RMO-61, Particulate Radiation Monitor,In Wrong Position.Caused by Personnel Error While Performing Test on Radiation Monitors | | | 05000285/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000285/LER-1980-018-03, /03L-0:on 800808,while Attempting to Monitor Gas Space on Vct,Inadvertent Release of Radioactive Matl to Auxiliary Bldg Environ Occurred.Caused by Deteriorated Surgical Tubing on Gas Analyzer.Tubing Replaced | /03L-0:on 800808,while Attempting to Monitor Gas Space on Vct,Inadvertent Release of Radioactive Matl to Auxiliary Bldg Environ Occurred.Caused by Deteriorated Surgical Tubing on Gas Analyzer.Tubing Replaced | | | 05000285/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000285/LER-1980-019, Forwards LER 80-019/03L-0 | Forwards LER 80-019/03L-0 | | | 05000285/LER-1980-019-03, /03L-0:on 800904,seismic Pipe Restraints SIS-62 & SIS-7 Were Inadvertently Made Inoperable at Same Time. Restraints Were Being Upgraded in Response to IE Bulletin 79-14.Restraint SIS-7 Was Immediately Made Operable | /03L-0:on 800904,seismic Pipe Restraints SIS-62 & SIS-7 Were Inadvertently Made Inoperable at Same Time. Restraints Were Being Upgraded in Response to IE Bulletin 79-14.Restraint SIS-7 Was Immediately Made Operable | | | 05000285/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000285/LER-1980-020-03, /03L-0:on 800905,axial Power Distribution Setpoints on D Channel Discovered Out of Tolerance in Nonconservative Direction.Caused by Dependent Setpoint Selection Switch Failure.Switch Cleaned & Returned to Svc | /03L-0:on 800905,axial Power Distribution Setpoints on D Channel Discovered Out of Tolerance in Nonconservative Direction.Caused by Dependent Setpoint Selection Switch Failure.Switch Cleaned & Returned to Svc | | | 05000285/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000285/LER-1980-021-03, /03L-0:on 800910,transformer T4 of DG-1 Failed. Transformer Feeds Diesel Oil Immersion Heater & Alarm Relays.Caused by Moveable Armature Located on Immersion Heater Contractor.Armature Repaired | /03L-0:on 800910,transformer T4 of DG-1 Failed. Transformer Feeds Diesel Oil Immersion Heater & Alarm Relays.Caused by Moveable Armature Located on Immersion Heater Contractor.Armature Repaired | | | 05000285/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000285/LER-1980-022-03, /03L-0:on 800911,during Safety Injection Actuation Signal Surveillance test,86B/VIAS Lockout Failed to Trip. Caused by Burned Coil.Coil Replaced W/Spare & Tested Satisfactorily for Proper Operation | /03L-0:on 800911,during Safety Injection Actuation Signal Surveillance test,86B/VIAS Lockout Failed to Trip. Caused by Burned Coil.Coil Replaced W/Spare & Tested Satisfactorily for Proper Operation | | | 05000285/LER-1980-023-03, /03L-0:on 800908,during Routine Operations,Power to Lockout Relay Coil 86A1/CPHS Was Interrupted.Caused by Electrically Opened Contacts.Contacts Cleaned & Burnished | /03L-0:on 800908,during Routine Operations,Power to Lockout Relay Coil 86A1/CPHS Was Interrupted.Caused by Electrically Opened Contacts.Contacts Cleaned & Burnished | | | 05000285/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000285/LER-1980-024-03, /03L-0:on 800926,while Completing Repairs on B Charging Pump,A Charging Pump Became Inoperable.Caused by Packing Cooling Pump Failure.Motor Replaced | /03L-0:on 800926,while Completing Repairs on B Charging Pump,A Charging Pump Became Inoperable.Caused by Packing Cooling Pump Failure.Motor Replaced | | | 05000285/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000285/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000285/LER-1980-025-03, /03L-0:on 801027,during Power Operation While Completing Repairs on C Charging Pump,A Charging Pump Became Inoperable.Caused by Leak in Weld Joining Sys to Flushing Line.Weld Repaired & Pump Returned to Svc | /03L-0:on 801027,during Power Operation While Completing Repairs on C Charging Pump,A Charging Pump Became Inoperable.Caused by Leak in Weld Joining Sys to Flushing Line.Weld Repaired & Pump Returned to Svc | |
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