05000325/LER-1978-081-03, LER 78- 081/03L-0 on 781028:main Steamline Drain Isolation Valve B21-F019 Failed to Operate Due to Faulty Brush Holder in Valve Motor.Motor Replaced & Valve Declared Operable

From kanterella
(Redirected from ML19294A509)
Jump to navigation Jump to search
LER 78- 081/03L-0 on 781028:main Steamline Drain Isolation Valve B21-F019 Failed to Operate Due to Faulty Brush Holder in Valve Motor.Motor Replaced & Valve Declared Operable
ML19294A509
Person / Time
Site: Brunswick 
Issue date: 11/28/1978
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML19294A507 List:
References
LER-78-081-03L, LER-78-81-3L, NUDOCS 7812070217
Download: ML19294A509 (1)


LER-1978-081, LER 78- 081/03L-0 on 781028:main Steamline Drain Isolation Valve B21-F019 Failed to Operate Due to Faulty Brush Holder in Valve Motor.Motor Replaced & Valve Declared Operable
Event date:
Report date:
3251978081R03 - NRC Website

text

(7 77)

LICENSEE EVENT REPORT

9....

CONTROL BLOCK:

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 iNIClBIEJ l1 l@l0 O ! -l 0 l 0 l 0 l 0 I 0 l - l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l l

l@

o i

1 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T S$RC L @ l 0l 5l0l-l0l3l2l5@l1 l0 12 18 l7 18 lgl1l1l2l8l7l8l@

o 7

8 60 61 DOCKET NUMBE R 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l A control operator discovered main steamline drain isolation valve B21-F019 failed toI O

2 o a l operate. Valve B21-F016, which is in series with B21-F019. was closed and deactivated, o 41 l This valve is located in the MSIV pit and required a unit shutdown to perform mai re-I o

s I nance.

(Technical Specification 3.6.3) 1 0

6 l

l 0

7 l

l 0

s I

l 80 7

8 9 C E CODE SUSCO E COMPONENT CODE SUB DE SU E

lC lD l@ lE l@ l Al@ l V l A l L l V l 0 l P lh lB l@ J @

O 9

7 8

9 to 11 12 13 18 19 20 SEQUE NTI AL OCCUR R E NCE REPORT REVISION LE A RO EVENT YE AR REPORT NO.

CODE TYPE N O.

b RE,P0RT l7 l8 l

[--]

l0 8 l 1l y

l 013 lL

(---J 0]

sv, (

_ 21 22 23 24 26 27 28 29 30 31 32 AKEN A ON ON PLANT M

HOURS 22 S8 i FOR 8.

SUPPLI R MANUFA URER l@

l Z l@

l Z l@

l0l0l0l0 lNl@

Yl@

lAl@

lLl2l0l0l@

l C lgl34 Z

3J 3b 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i

O l On 11/18/78 the unit e'xperienced a short scheduled shutdown.

The valve motor was I

,i i

l found inoperable due to a faulty brush holder.

The, motor was replaced and the valvo I i

7 l declared operable. This is considered an isolated incident and no further corrective i

3 l action is required.

l i

4 l

l 7

8 9 80 SA S

% POWER OTHER STATUS DISC RY DISCOVERY DE%CRIPTION i s lE @ l 0 l 9 l 9 l@l NA l

l B l@l Operator Observation l

A TlVITY CO TENT RELEASE @D OF RELE ASEl Z l@l AMOUNT OF ACTIVITY LOCATION OF RELEASE NA l

l NA l

1 6

7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

l 0l 0l 0l@l Zl@l NA l

1 7

PERSONNEL INJURIES NUMBER DESCR6PTION l0 l0 l0 l@l NA l

1 a

7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE

DESCRIPTION

(TITllZl@lNA 7

8 9 10 80 ISSUE D

L z18l ESCRIPTION NA l

lllllllllllll}

2 O

  • 5 7'8 '1 9. 0 7 0 ') q A. C. Tollison, Jr.

(919) 457-6701 PHONE:

NAME OF PREPARER