LER-1979-041, /01T-0 on 790525:certain Nylon Insulation Sleeve Portions of Compression Type Termination Lugs Did Not Meet Environ Qualification Tests.Each Drywell Termination Will Be Checked for Deterioration & Safety Assurance |
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| 3251979041R01 - NRC Website |
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LICENSEE EVENT REPORT toni n ot. o tOCK: l l
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RE POR T DAT E 80 EVENT DESCRIPTION AND PROBABt.E COT 5EQUENCES O'o IDuring the review of environmental qualification of electrical equipment for Unit Nos.
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l1 and 2 as required by IE Bulletin 79-01, it was found that certain nylon insulating g
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pleeve portions of the compression-type termination lugs, manufactured by AMP Special j
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The lug in question is ;
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LAMP Type PIDG for use with sizes 10 through 12 wiring.
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40 43 42 43 44 41 CAUSE DESCRIPTION AND CORRECTf W AcIlONS h l1 o lAn evaluation has been made of the possible problems which could result from the fail-l fure of the insulating sleeve.
It was assumed that a total _aeterioration of the sleeve I i
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[ problems can only occur if the lugs were free to rotate underneath the terminal (cont.)]
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d LER CONTINUATION -- RO# 1-79-41 Facility: BSEP Unit No. 1 Event Date: 5/25/79 screws far enough to cause contact between adjacent lugs, rotation is not expected in the seismically qualified terminations used at Brunswick.
As an interim measure, each of the drywell terminations using the AMP sleeve is being inspected for deterioration of the existing sleeve; this inspection will also ensure that the wire is properly aligned to the terminal block cnd that the termination screw is tight. These actions provide assurance for the nearterm that plant operation may continue without undo risk to the public health and safety.
At the next refueling outage for each unit, we will implement a permanent solution to the problem. There are several possible permanent insulation devices which will be evaluated in the interim.
During the refueling outage, one of these solutions, or a combination of them, will be used to ef fect a permanent, fully qualified solution.
2229 342
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| 05000324/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000324/LER-1979-001-03, /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | | | 05000325/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000325/LER-1979-001-03, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | | | 05000325/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000324/LER-1979-002-03, /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | | | 05000324/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000325/LER-1979-002-03, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | | | 05000324/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000324/LER-1979-003-03, /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | | | 05000325/LER-1979-003-03, /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | | | 05000325/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000325/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000325/LER-1979-004-03, /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | | | 05000324/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000324/LER-1979-004-03, /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | | | 05000325/LER-1979-005-03, /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | | | 05000325/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000324/LER-1979-005-03, /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | | | 05000324/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000325/LER-1979-006-03, /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | | | 05000324/LER-1979-006-03, /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | | | 05000325/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000324/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000325/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000325/LER-1979-007-03, /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | | | 05000324/LER-1979-007-01, /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | | | 05000324/LER-1979-007, Forwards LER 79-007/01T-0 | Forwards LER 79-007/01T-0 | | | 05000325/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000325/LER-1979-008-03, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | | | 05000324/LER-1979-009-03, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | | | 05000324/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000325/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000325/LER-1979-010-03, /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | | | 05000324/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000324/LER-1979-012-03, /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | | | 05000324/LER-1979-013-03, /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | | | 05000324/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000325/LER-1979-014-03, /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | | | 05000325/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000325/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000325/LER-1979-017-03, /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | | | 05000325/LER-1979-018, Forwards LER 79-018/03X-1 | Forwards LER 79-018/03X-1 | | | 05000325/LER-1979-018-03, /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | | | 05000325/LER-1979-019-03, /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | | | 05000325/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000324/LER-1979-021-03, /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | | | 05000324/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000325/LER-1979-022-03, /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | | | 05000325/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | |
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