05000325/LER-1979-008-03, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown

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/03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown
ML19274D556
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/09/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274D555 List:
References
LER-79-008-03L, LER-79-8-3L, NUDOCS 7902130101
Download: ML19274D556 (1)


LER-1979-008, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown
Event date:
Report date:
3251979008R03 - NRC Website

text

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LICENSEE EVENT REPORT tONTROL BLOCK: l l

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60 61 DOCKE T NUMBER tw 69 EVENT DATE 14 75 '

3EPORT DATE 80 EVENT DESCRIPT'ON AND PROBABLE CONSEQUENCES h The RHR Services Water System Component Test (P.T.8.2.4), for the IB pump, revealed g

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l unacceptable levels of pump differential pressure (psid) and vibration. An acceptable g o

3 l pump differential pressure range is 257 to 294 (test reading 228 psid). A vibration l

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I reading of 9.4 mils was also recorded of f the pump with an allowable vibration limit l

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o is Iof up to 2.3 mils.

(Technical Specification 3.7.7.1).

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