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LER-1979-043, /01T-0 on 790522:auxiliary Feedwater Pumps Discharge Valves Demand Reduction to 0%.Caused by Deficient Surveillance Procedure.Immediate Change Initiated to Leave Demand Signal at Normal Value |
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| 2721979043R01 - NRC Website |
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text
Report Number:
79-43/0lT Report Date:
6/05/79 Occurrence Date:
5/22/79 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Auxiliary Feedwater Pumps Discharge Valves Closed during Surveillance Testing CONDITIONS PRIOR TO OCCURRENCE:
Refueling Mode 6 DESCRIPTION OF OCCURRENCE:
In reviewing the surveillance procedure which demonstrates the opera-bility of No. 13 (23) steam driven auxiliary feedwater pump during operational modes 1, 2, and 3 as required by Technical Specification 3.7.1.2, it was discovered the procedure called for the valve demand to be reduced to 0% for the motor driven feedwater pumps discharge control valves (AF-21's) in addition to the closure of the steam driven feedwater pump discharge control valves ( AF-ll's).
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was a deficiency in the surveillance pro-cedure.
The AF-21 and AF-ll valves were originally required to be shut to insure a single test flow path and to insure no auxiliary feedwater flow to the steam generator during the test evolution.
How-the AF-21's are normally closed and open to a preset valve
- ever, demand only when the associated motor driven pump develops the required discharge pressure.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.7.1.2 requires at least three independent steam generator auxiliary feedwater pumps and associated flow paths operable when in modes 1, 2 or 3, with two feedwater pumps capable of being powered from separate vital busses and one feedwater pump With capable of being powered from an operable Lteam supply system.
one feedwater pump inoperable, restore at least three auxiliary feed-water pumps to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
The average duration of the pump test has been 10 minutes after which normal auxiliary feedwater system lineup is verified.
The ECCS automatic start of the moc.or driven feedwater pumps is not disabled nor is remote control of the AF-21 valves taken from the control room reactor operator during the steam driven pump test.
2255 010 7906012,23/,
LER 79-43/0lT CORRECTIVE ACTION:
To insure full operability of the motor driven auxiliary feedwater pumps during the surveillance evolution, an on-the-spot change has been initiated to leave the demand signal for the AF-21 valves at the normal value.
Also, the AF-1, 3, 10, 20, 22, 23 and 86 manually operated valves normal position has been changed from open to locked open.
A further review of the surveillance procedures found no other pro-cedure deficiencies.
No further corrective action is required.
FAILURE DATA:
Not Applicable Prepared By A.
W.
Kapple
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Manager
' Sale 6 Generating Station SORC Meeting No.
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| 05000272/LER-1979-001-03, /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | | | 05000272/LER-1979-001, Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | | | 05000272/LER-1979-002-03, /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | | | 05000272/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000272/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000272/LER-1979-003-03, /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | | | 05000272/LER-1979-004, Forwards Updated LER 79-004/03X-1 | Forwards Updated LER 79-004/03X-1 | | | 05000272/LER-1979-004-03, /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | | | 05000272/LER-1979-005-03, /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | | | 05000272/LER-1979-005, Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | | | 05000272/LER-1979-006-03, /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | | | 05000272/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000272/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000272/LER-1979-007-03, /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | | | 05000272/LER-1979-008-03, /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | | | 05000272/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000272/LER-1979-009-03, /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | | | 05000272/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000272/LER-1979-011, Forwards LER 79-011/01X-2 | Forwards LER 79-011/01X-2 | | | 05000272/LER-1979-011-01, /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | | | 05000272/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000272/LER-1979-012-03, /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | | | 05000272/LER-1979-013-04, /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | | | 05000272/LER-1979-013, Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerat | Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerations | | | 05000272/LER-1979-014-03, /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | | | 05000272/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000272/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000272/LER-1979-015-03, /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | | | 05000272/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000272/LER-1979-016-03, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | | | 05000272/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000272/LER-1979-017-03, /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | | | 05000272/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000272/LER-1979-018-03, /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | | | 05000272/LER-1979-020-03, /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | | | 05000272/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000272/LER-1979-021-03, /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | | | 05000272/LER-1979-022-03, /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | | | 05000272/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000272/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000272/LER-1979-024-03, /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | | | 05000272/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000272/LER-1979-025-03, /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | | | 05000272/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000272/LER-1979-026-03, /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | | | 05000272/LER-1979-027-01, /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | | | 05000272/LER-1979-027, Forwards LER 79-027/01X-1 | Forwards LER 79-027/01X-1 | | | 05000272/LER-1979-028, Has Been Voided | Has Been Voided | | | 05000272/LER-1979-029-03, /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | | | 05000272/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | |
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