05000325/LER-1979-002-03, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset

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/03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset
ML19269D115
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/21/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19269D104 List:
References
LER-79-002-03L-02, LER-79-2-3L-2, NUDOCS 7902270342
Download: ML19269D115 (1)


LER-1979-002, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset
Event date:
Report date:
3251979002R03 - NRC Website

text

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