05000325/LER-1979-001-03, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing

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/03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing
ML19269C606
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/02/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19269C605 List:
References
LER-79-001-03L, LER-79-1-3L, NUDOCS 7902060214
Download: ML19269C606 (1)


LER-1979-001, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing
Event date:
Report date:
3251979001R03 - NRC Website

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LICENSEE EVENT REPORT l

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7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 68 CON'T 3o[OR L l@l 0l 5 l 0 l - l 0 l 3 l 2 l 5 @l 0 l 110 l 4 l 7 I 9 @l 0 l 2 0]2l7 9 l@

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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE. CONSEQUENCES h o

2 l The HPCI system failed response time Periodic Test, P.T.45.3.4.

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Specification response time of 130.0 seconds is required, and on 1/4/79, a responsel o

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time of 30.2 seconds was attained.

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s I (Technical Specification 3.3.3) 1 0

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CODE SUSCO E COMPONENT CODE SUB ODE SUB E

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9 10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION LE EVENT YEAR REPORT NO.

CODE TYPE N O.

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HOURS 22 S8 FOR 8.

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Z 33 25 36 37 40 di 42 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h i

o l Troubleshooting work on the governor controls (EGM-EGR) was in progress when the l

unit was shut down on 1/13/79 for a refueling outage.

Response time testing will bel j3 ;i; i

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attempted again after reactor startup, when steam is available following the refuel-l 3

l ing outage. A revision to this report will be submitted describing event cause and l corrective actions after the response time test has been completed satisfactorily.

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% POWER OTHER STATUS IS O RY DISCOVERY DESCRIPTION NA l

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7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE D ESCRIPTION [0 l 0 l 0 l@l Z l@l NA l

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PERSONNEL INJU IES NUMRER

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8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE

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