LER-1979-006, /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys |
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| 3251979006R03 - NRC Website |
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2 l While leak-checkinn the tube sheet s on the_naln_Londemer durine a refun l i Tm oor ve I
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l The condensate system was running, and the condenser weis under a vacuna.
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CAU5E DESCRIPTION AND COnRECTIVF AC NO'. :
l On 3/16/ 79, condenser tube leaks allowed chlorides to enter the condenuate ssot 1
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LER CONTINUNfl0N -- R0it 1-79-o Facility' BSEP Unit el Event Date 3/16/79 nsed for hotwell level control. Chlorides were admitted to the vessel by the continuous feed of the CRD system. 1he RWCU system was under clearance to install a piping modi fic ation and thus was not available for chloride removal.
Condenser vacuum was broken, and CDD's and additional CFD's were placed on service to clean up the condensate system.
Condensate was circulated through the reactor vessel using the feedwater systcm for supply and the reactor cavity drain to the hotwell for return. A precaution has been added to 0.P 32.1 and 32.2 to maintain at least one (1) CFD and one (1) CDD on service with an effluent conductivity <0.8 mho/cm whenever condenser vacuum 27 in.
lig.
On 3/29/79, condenser tube leak, allowed chlorides to enter the condensate system with the CFD'-
and CDD's bypassed.
They were intentionally bypassed in order to determine if condenser tube leaks were present.
Chlorides entered the CST through the reject bypass valve, being used for hotwell level control. Chlorides were admitted to the vessel by the continuous feed of the CRD system and were not detected in time to prevent exceeding the Technical Specification limit of 0.2 ppm. The RWCU system was under clea rance for a piping modification and was not available for cleanup. Condenser vacuum was broken and CFD'-
and CDD's were placed on service to clean up the condensate system. The continuous feed of the CRD system and draining through the RHR system for level control were used to clean up the reactor vessel.
In order to prevent a recurrence of thi: type, a Special Test Procedure (79-23) was written and approved.
This procedure provides additional precautions and increased CST and reactor water sampling frequencies when CFD's and CDD's are bypassed while checking th: hotwells for chloride intrusion.
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| 05000324/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000324/LER-1979-001-03, /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | | | 05000325/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000325/LER-1979-001-03, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | | | 05000325/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000324/LER-1979-002-03, /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | | | 05000324/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000325/LER-1979-002-03, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | | | 05000324/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000324/LER-1979-003-03, /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | | | 05000325/LER-1979-003-03, /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | | | 05000325/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000325/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000325/LER-1979-004-03, /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | | | 05000324/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000324/LER-1979-004-03, /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | | | 05000325/LER-1979-005-03, /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | | | 05000325/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000324/LER-1979-005-03, /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | | | 05000324/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000325/LER-1979-006-03, /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | | | 05000324/LER-1979-006-03, /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | | | 05000325/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000324/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000325/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000325/LER-1979-007-03, /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | | | 05000324/LER-1979-007-01, /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | | | 05000324/LER-1979-007, Forwards LER 79-007/01T-0 | Forwards LER 79-007/01T-0 | | | 05000325/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000325/LER-1979-008-03, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | | | 05000324/LER-1979-009-03, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | | | 05000324/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000325/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000325/LER-1979-010-03, /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | | | 05000324/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000324/LER-1979-012-03, /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | | | 05000324/LER-1979-013-03, /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | | | 05000324/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000325/LER-1979-014-03, /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | | | 05000325/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000325/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000325/LER-1979-017-03, /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | | | 05000325/LER-1979-018, Forwards LER 79-018/03X-1 | Forwards LER 79-018/03X-1 | | | 05000325/LER-1979-018-03, /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | | | 05000325/LER-1979-019-03, /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | | | 05000325/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000324/LER-1979-021-03, /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | | | 05000324/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000325/LER-1979-022-03, /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | | | 05000325/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | |
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