ML19262D012
| ML19262D012 | |
| Person / Time | |
|---|---|
| Site: | Millstone |
| Issue date: | 04/08/1980 |
| From: | Howlett G NORTHEAST NUCLEAR ENERGY CO. |
| To: | |
| Shared Package | |
| ML19262D011 | List: |
| References | |
| NUDOCS 8004220413 | |
| Download: ML19262D012 (6) | |
Text
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OPERATING DATA REPORT DOCKET No. 50-336 DA rE ADril 8.1980 CO.\\lPLETED BY G.H. Howlett TELEPHONE 203 447~-1791 X364 OPERATING STATUS Millstone 2 Notes
- Items 21 & 22,
- 1. Unit N3me.
March 1980 Cummulative are computed
- 2. Reportin; Period:
- 3. Licen>cd Thermal Power $5tht): 2700 using a weighted average.
- 4. Nameplate Rating iGross \\lwe):
909
- 5. Desi;n Electrical Rating (Net SIWE):870
- 6. Stasimum Dependable Capacity (Gross 31Wep: 895
\\
864
- 7.. lasimum Dependable Capacity dNet stwe):
'i. If Chamges Occur :n Capacity Ratin;3 titems Nurnber 3 Through 7) since Last Report. Gise Reasonc None
- 9. Power Lese! To hhich Restricted. If Any INet.\\lhe):
None
- 10. Reasons For Restrictions. If Any:
None This.\\!onth Yr..to.Date Cumularise
- 11. Hours In Reporting Period 744 2,184 37,392
- 12. Number Of Hours Reactor has Critical 698.5 2,112.6 27,191.7
- 13. Reactor Re>ene Shutdown !!ours 0
0 q,0 %
l-1. Hours Generator On.Line 678.0 2.059.1 25,879.3
- 15. Unit Re<ene Shutdown Hours 0
0 3~35 7
- 16. Gros, Thermal Ener;> Generated (51%I1)
I,740,751
_5f25,544 63,124,172~~~~
l-Gros, E:e:tr:e.'l Energy Generated isti.Hi 567,033 1,778,469 20,363,114 li Net E'e trical Ener;> Generate!,3thH)
Sf4,23T- ~ ~
1,7TO 893 T9,T4T,151 It Unit Senice Faetor 91.1 94.3 69.2
- 20. Unit u.'iiabdity Factor 91.1 94.3 70.1
- i enit C;p av F2etar it,;n; \\iDC Neri 84.7 9.0.7 63.6
- cmr cy,,gc3 p,c.y,,esia; DER Net) 84.1 90.0 62.3
- .1 Unit Forced ouage Rate 8.9 5.7 22.6
- 4. Shatdowa, Seheduled Oser Nest o stonths tty pe. Dire. and Duration of Eachr Refueling (Cycle 4), July 1,1980,9 weeks.
NA
- - If Wr Dm n \\t End Of R eport P.. d. E-
>JDe af :
up.
h Units in Test Status iPrior to CommerJat Onr2 tion t Foreea,r Achiewd INITI AL CRITN A LtT'r N/A N/A INITIAL ELECTRIUTY N/A _
N/A C0\\isiERc! AL CPn iT!o',
N/A N/A "0TE: Correction to February Report Item 18.
Should read Month 528 95T -
Yr-To-Date 1,166,662, Cumulative 18.935,920.
Item 22 Year to Date sncuTd read 93.1 8004220g3
AVER AGE D All.Y UNIT POWER LEVEL 50-336 DOCKET NO.
Millstone 2 m.,7 DATE April 8,1980 CO\\!PLETED BY G.H. Howlett TELEPHONE (203)447-1791 X364 March 1980
,g.
DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL Dik,e-Net) anve. Net) 850 849 1
1,e 2
852 850 33 3
781 849 39 4
815 750 20 5
R14 21 289 6
820 536 22 7
850 13 73 8
851 484
,4 9
R51
,5 343 10 850 846 26 11 850 847 12 0
(-7)
,s 847 13 307 847
,9 847 84'/
34 3g 15 827 847 3
16 849 IN S TR UCTIC.N S On this Drm.n. i.c -'.: n se 6:h :..: p. e b d.., ' 9.'ie.N*c. r.; em 33 g, g, 9.g.- &c.yw
.e r e a en.i F. ': -- _, a :
I
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I PAGE 1 of 2 h
I T
llNII SilUIDOWNS AND POWER REDUCTIONS one 2 A E DATE April 9,1980 COMPLETED l!Y G.H. Howlett til RE PORT MONIll flarch 1980 203 447-1791 X364 l ELEPilONE 5
E
{g
'h
_$ E' ~;
t.icensee E r, h
Cause & Corrective
,t hic 3g j
jsy livent y?
gU3 Action to f-y jg
- Repo, u
mV Prevent Recurrence H
6 4
800312 F
29 A
3 ft/A
.;l VAL"vl (
Feedwater Regulating valve (2-fW-51B) locked-up (closed), resulting in a reactor trip on Low Steam generator level.
5 800320 F
0 A
4 N/A RB CRDRVE Dropped C.E.A. #7-1 due to failed Control Element Drive Mechanism power supply.
Reduced power to 65%.
6 800321 F
18.3 8/G 3
ft/A ZZ ZZZZZZ Instrumentation 'echnician removed flain feed pump suction pressure trans-mitter from service for calibration.
This lead to the camp tripping on low suction pressure and a subsequent reactor trip on Low Steam Generator level.
SilMMARY: The unit operated at or near 100% rated thermal power throughout the reporting period except for the following; 3/2-3/6 operations at 96% power in preparation of a Moderator Temperature Coefficient Test, 3/20 Dropped CEA and reactor trips on 3/21 and 3/23.
fl0TES:
Correction to February, Unit Shutdowns and Power Reductions; Item #1 Duration (Hours) should have read 23.5 not 24.5.
Item #2 Duration (llours) should have read 16.3 not 16.4.
i9///)
J l'AGI 2 of 2 50-336 U
UNil S!!U1 DOWNS AND POWl:R RE!)UC1 IONS
' MIIISl""" d U l P A 1E DATE April 9,1980 COMPI.ETLD liY G. ll. Howlett II REPolt'I MON fli March 1980 l tttpliONE 203 ^47-1791 X364 I
=
e 3g
'b J, Y l t.ite m ee
,E-r, L' n, cause & corrective p2 j
j5$
twn:
Lf '2
!i?
Attion to No.
Date H,
dE 3 ;y, S Rep.n: u eU UU Prevent Recurrence j
4 0
f C
l 7
800323 F
18.7 A
J N/A lill VALVEX Feedwater Re9ulatinq Valve (2-FW-51A) lill llTEXCil locked-up (closed) during a power reduction for a feedwater heater problem. The reactor tripped from 20% power on Low Steam Generator Level.
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Docket No. 50-336 P'8 9e I Of I
Date April 10, 1980 Unit Name ' Millstone 2 Completed By G. li. Ilowlett III Telephone (zu3J44/-i/91 x3b4 CORRECTIVE MAINTENANCE
SUMMARY
FOR SAFETY RELATED EQUIPMENT Report Month February 1980 DATE SYSTEM COMP 0NENT MAINTENANCE ACTION 2/4/80 Reactor Protection R.P.S. Ch. "B" Reactor Coolant Replaced and calibrated converter.
Pump Speed Sensing, Frequency to Voltage converter.
2/2//80 Safety injection 2-SI-466 Safety Inj Tk Fill Line Valve leaked through.
Rebuilt valve.
Relief Valve
Docket No.
50-336 Date:
April 11, 1980 Completed By G.H. Howlett III Telephone:
2037447-1971 X364 REFUELING IflFORMATION REQUEST 1.
Name of facility:
Millstone 2 2.
Scheduled date for next refueling shutdown: July 1, 1980 3.
Schedule date for restart following refueling: September 1, 1980 4.
Will refueling or resumption of operation thereaf ter require a technical specification change or other license amendment?
Technical Specification changes will be necessary as a result of the change in fuel and safety analysis supplier.
5.
Scheduled date(s) for submitting licensing action and supporting information:
The schedule for submitting license actica is as follows:
Basic Safety Report 3-6-80 ECCS Results 5-15-80 Reload Safety Evaluation 5-15-80 6.
Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significani changes in fuel design, new operating procedures:
Cycle 4 will be unique in that it will be the first where the fuel and safety analysis will be supplied by Westinghouse.
7.
The n mber of fuel assemblies (a) in the ccre and (b) in the sper.: tel c
storage pool:
(a)
In Core:
217 (b) 144 3.
The present licensed spent fuel pool storage capacity and *M size of any increase in licensed storage capacity that has been recuested or is planned, in number of fuel assemblies:
667 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
1985, Spent Fuel Pool, full core off load capability is reached.
1987, Core Full, Scent Pael Pool contains 648 bundles.
U l