LER-1979-107, /01T-0:on 791212,while Performing Visual Insp of Inaccessible Snubbers,Several Snubbers Found on Safety Relief Valve F013H Tailpipe.Caused by Reactor Scram When Safety Relief Valves F013F,G & H Automatically Lifted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3251979107R01 - NRC Website |
|
text
"*'
LICENSEE EVENT REPORT CONTROL BLOCK: ]
]
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 6
[oTil I Nl Cl B l E l P l 1l@l 0 l 0 l -l 0 l 0 l 0 l 0 l 0 l - l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l l
l@
?
8 9 LICENSEE CODE 14 15 LICENSE NUMSER 25
- 6 LICENSE TYPE JO 57 CAT $8 E
1"RN lL l@l0]5l0l-l0l3l2l4l@l1]2l1l2l7l9l@l1l2l2l0l7l9l@
CON'T 7
8 50 61 DOCK ET NUMSER 68 69 EVENT OATE 14 75 REPORT QATE 40 EVENT OESCRIPTION ANO PRC8ABLE CONSEQUENCES h l While performing PT 19.6,0.1, Visual Inspection of Inaccessible Snubbers, the follow,J o
2
- 1) B21-34SS296,
.J g l ing snubbers were found on the safety relief valve F013H cailpipe:
i elongated hole in rodeye; 2) B21-34SS297, reservoir missing, broken shaf t, two bent J
o 4
l rodeyes, bent extension; 3) B21-34SS298, clamp moved; 4) 321-34SS299, broken chaft, j
o s
o 6 l bent rodeye, clamp moved; 5) B21-34SS300, cracked weld on I-beam, clamp _ moved: 6) B21-J l 34SS336, bent extension, clamp moved, valve body damaged, broken springs; 7) B21-l
~
gi,,7,j 0
8 i 34SS337, broken shaft, clamp rotated, extended end springs fammed into valve (cont.) 1 30 COMP.
VA LV E SYSTEV
CAUSE
CALSE COCE CCCE Sb8C00E COMPCNENT CODE SUSCOCE SLSCOCE l C l C l @ W@ l ", l @ lS IU lP l0 lR lT l @ l Dl @ [7d @
o 9
7 6
9 10 11 1:
f:
IS 19 20 SECUL NTI A L CCCURRENCE REPORT REVISION EVENT YE AR R E80 RT *dC.
COOE TYPE N o.
AE l7 l9 l l_l l 11 0l 7l j,.-l l 0l 1l lT[
l-l l 0l LER Ro Os
- 2
- 4 2.
- s
- 9 20 22 2:
( N 4
ON CNP. NT NCLAS 22 SS IT FOR 9.
SL PPLI E VA F
T AER IXl@lXl@
12l@
Iz l@
! 01 01 01 01 IY@
Y l@
lal@
l BI 2l 0l 9 33 34 35 36 31 40 41 42
.43 44 47 CAUSE CESCRIPTION AND COA AECTIVE ACTICNS h i
a ] It is believed that this damage occurred following a reactor scram on November 20,1979 jwhen safety relief valves F013F, G, and H automticallr lifted.
- i 7 l
- 1) All other safety relief valves and associated piping were checked for danace j
3 l with none found.
I gl
- 2) All damaged snubbers were rebuilt and functionally tested successfully.
(Cont.)]
7 8 9 STA
%PCWER OTHER STATUS iSCO RY DISCOVERY CESCRIPTION l G @ l0 l 0 l 0 l@l N/A l
Bl@l Periodic Test l
i s
Activity 0N ENT LCCATION OF RE LE ASE GELE ASE3 0F RELE ASE AVOUNT Cs ACTtvtTY l 2 l @ l Z l@l N/A l
N/A l
i c
44 45
/A 7
30 7
8 9
- 0 11 PERSONNEL f *PCSLAES Q ({
f NUYHEA TYPE O E SCRIPTICN -
N/A l
lOi010J@lzl@l 7
T;UU uU'.
^
.r.. a',N:Ji,u fi J.
i omP,,cN@
m...
N/A l010l01@l 7
d 3 11 1:
LO".S OF Ort D AV AGE To F ACILt Tv N/A y g222 8)tg C C.2 TYPE DE9CTiiPricN [FFq z l@l
.VV de 7
8 9 tu Npc gg[ QN(v PU H UCi t Y ISSU E D DE5CRIPTION N/A l
llllll{lll ll l 2
tia 63 i40 919 - 457-9521 A. C. Mison, Jr.
pggyg NAME OF PitEPAF4Ef4
\\
LER CONTINUATION - RO# 1-79-107 Facility: BSEP Unit #1 Event Date: 12-12-79 Event Descrip_ ton and Probable Consequences (cont.)
body; 8) B21-34SS338, valve body damaged by poppet spring; 9) B21-34SS339, rodeye bent, clamp moved; 10) B21-34SS340, bent rodeye, clamp moved.
Technical Specification 6.9.1.81 Cause Description and Corrective Actions (cont.)
- 3) All rodeyes, extensions, clamps, and I-beams were repaired or rebuilt, de-pending on the extent of damage.
- 4) All welde from the relief valve inlet to the relief line entry into the torus were cleaned and inspected by PT or MT and found satisfactory.
- 5) All relief line vacuum breakers were inspected and tested satisfactorily.
- 6) The testing and rebuild history of the snubbers on the F013H tailpipe were reviewed.
There were no significant findings.
7)
The F013H valve operating history was reviewed.
There were no significant findings.
3)
Special tests have been approved to:
a) Test F0137 and H at 250 psig and inspect for damage.
F013F and H share a co==on exhaust header in the torus.
b) Test F013F and H at normal pressure (900-1000 psig) to' approximate the opening sequence occurring on November 20, 1979. Perform a tailpipe in-spection.
9)
Until permanent resolution is determined, if any pair of valves lift which share the same exhaust header, the tailpipes will be inspected.
10)
The torus modifications scheduled for 1980 will rearrange the S/RV exhaust lines in the torus such that each will have a separate tee quencher.
11)
United Engineers and Constructors has analyzed this event with the following preliminary results:
a) A normal valve discharge cannot cause the observed damage.
b) A normal valve discharge with selected inoperable snubbers cannot cause the observed damage, c) A valve discharge with a water slug in the exhaust line is not likely to cause the observed damage.
d) A valve discharge with a water slug in the exhaust line and selected in-operable snubbers could produce the obcerved damage. The water slug was postulated to be ganerated by water being driven into the line as a result of SRV "F" discharge.
e) Conclusive proof of the cause has not been determined.
1642 028 e
3!
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000324/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000324/LER-1979-001-03, /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | | | 05000325/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000325/LER-1979-001-03, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | | | 05000325/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000324/LER-1979-002-03, /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | | | 05000324/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000325/LER-1979-002-03, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | | | 05000324/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000324/LER-1979-003-03, /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | | | 05000325/LER-1979-003-03, /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | | | 05000325/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000325/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000325/LER-1979-004-03, /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | | | 05000324/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000324/LER-1979-004-03, /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | | | 05000325/LER-1979-005-03, /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | | | 05000325/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000324/LER-1979-005-03, /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | | | 05000324/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000325/LER-1979-006-03, /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | | | 05000324/LER-1979-006-03, /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | | | 05000325/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000324/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000325/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000325/LER-1979-007-03, /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | | | 05000324/LER-1979-007-01, /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | | | 05000324/LER-1979-007, Forwards LER 79-007/01T-0 | Forwards LER 79-007/01T-0 | | | 05000325/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000325/LER-1979-008-03, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | | | 05000324/LER-1979-009-03, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | | | 05000324/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000325/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000325/LER-1979-010-03, /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | | | 05000324/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000324/LER-1979-012-03, /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | | | 05000324/LER-1979-013-03, /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | | | 05000324/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000325/LER-1979-014-03, /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | | | 05000325/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000325/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000325/LER-1979-017-03, /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | | | 05000325/LER-1979-018, Forwards LER 79-018/03X-1 | Forwards LER 79-018/03X-1 | | | 05000325/LER-1979-018-03, /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | | | 05000325/LER-1979-019-03, /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | | | 05000325/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000324/LER-1979-021-03, /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | | | 05000324/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000325/LER-1979-022-03, /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | | | 05000325/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | |
|