05000325/LER-1979-093-03, /03L-0:on 791127,while Performing High Steamline Radiation Channel Alignment & Functional Test,Main Steamline Drawer B Was Out of Specs.Caused by Instrument Drift.Drawer Recalibr

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/03L-0:on 791127,while Performing High Steamline Radiation Channel Alignment & Functional Test,Main Steamline Drawer B Was Out of Specs.Caused by Instrument Drift.Drawer Recalibr
ML19256G162
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/19/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256G155 List:
References
LER-79-093-03L, LER-79-93-3L, NUDOCS 7912270541
Download: ML19256G162 (2)


LER-1979-093, /03L-0:on 791127,while Performing High Steamline Radiation Channel Alignment & Functional Test,Main Steamline Drawer B Was Out of Specs.Caused by Instrument Drift.Drawer Recalibr
Event date:
Report date:
3251979093R03 - NRC Website

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