05000325/LER-1979-102-03, /03L-0:on 791129,during Normal Operation, Containment Atmospheric Monitor Tripped & Could Not Be Restarted.Caused by Seized Pump Bearings.Pump Replaced & Preventative Maint Procedure Established

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/03L-0:on 791129,during Normal Operation, Containment Atmospheric Monitor Tripped & Could Not Be Restarted.Caused by Seized Pump Bearings.Pump Replaced & Preventative Maint Procedure Established
ML19256G126
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/20/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256G124 List:
References
LER-79-102-03L, LER-79-102-3L, NUDOCS 7912270490
Download: ML19256G126 (1)


LER-1979-102, /03L-0:on 791129,during Normal Operation, Containment Atmospheric Monitor Tripped & Could Not Be Restarted.Caused by Seized Pump Bearings.Pump Replaced & Preventative Maint Procedure Established
Event date:
Report date:
3251979102R03 - NRC Website

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LICENSEE EVENT REPORT

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60 61 COCK ET NLV8 ER (45 69 EVENT OATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PRO 8ABLE CONSEOUENCES h lol21 During normal operation, the operator noticed that the containment atmospheric monitor l lol3l l CAC-AT-1263 tripped and could not be restarted.

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