05000325/LER-1979-076-03, /03L-0:on 791002,valve E11-F068B Failed to Open. Caused by Contacts Sticking in Relay Ri in Position Modulator,Resulting in Constant Close Signal.Relay Freed & Replacement Ordered

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/03L-0:on 791002,valve E11-F068B Failed to Open. Caused by Contacts Sticking in Relay Ri in Position Modulator,Resulting in Constant Close Signal.Relay Freed & Replacement Ordered
ML19254E270
Person / Time
Site: Brunswick 
Issue date: 10/23/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19254E265 List:
References
LER-79-076-03L-01, LER-79-76-3L-1, NUDOCS 7910310402
Download: ML19254E270 (1)


LER-1979-076, /03L-0:on 791002,valve E11-F068B Failed to Open. Caused by Contacts Sticking in Relay Ri in Position Modulator,Resulting in Constant Close Signal.Relay Freed & Replacement Ordered
Event date:
Report date:
3251979076R03 - NRC Website

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