LER-1979-093, /03X-1:on 791021,during Normal Operation,Routine Computer Printout Indicated Core Max Fraction of Limiting Power Density Was 1.003 Over Tech Spec Limit.Power Reduced 2%.Control Rod Pattern Adjusted.Cause Not Reported |
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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333
_ ATTACHMENT TO LER 79-093/03X-1 Page 1 of 1 During normal operation, Operations personnel noted that a routine computer print out of the core performance log indicated that the Core Maximum Fraction of Limiting Power Density (CMFLPD) was 1.003 compared J
to a Tecimical Specification limit of equal to or less than i.000.
Reactor power was immediately reduced approximately 2% in accordance with the requirements of Technical Specifications, Appendix A, Paragraph
- 3. 5. I, This action restored CMFL.PD to within the limits of Technical Specifications within the time frame allowed and is considered to be equivalent to operation in a degraded mode.
Following the initial power reduction, the core performance log was again demanded from the plant's process computer and revealed that CMFLPD was within speci ficat ions.
Control rod pattern adjustments were made and approximately two hours later, power was restored to between 99 and 100%
of rated power. A core performance log demanded following the power increase revealed that CMFLPD was with speci fications.
Z.Z~.11 The event did not represent a significant hazard to the public health and safety.
NOTE:
LER 79-083 is a related event and Revision 1 of this LER is submitted to correct the Technical Specification Paragraph reference above.
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NAME OF PREPARER PHONE:
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0 Wisconsin Electnc mcoum 231 W. MICHIGAN. P.O. BOX 2046. MILWAUKEE, WI 53201 November 16, 1979 Mr. Harold R. Denton, Director Office of Nuclear Reactor Regulation U. S. NUCLEAR REGULATORY COMMISSION Washington, D. C.
20555 Attention : Mr. A. Schwencer, Chief Operating Reactors Branch #1 Gentlenen:
DOCKET NOS. 50-266 AND 50-301
- - LOSS OF 0FFSITE POWER EVENTS POINT BEACH NUCLEAR PLANT Your letter dated October 1,1979 requested that we provide you with information concerning the loss of offsite power which occurred at Point Beach on October 13, 1973 and any other loss of offsite power events. There have been a total of four loss of offsite power events at Point Beach. The following details are provided in response to your request for information:
A.
PARTIAL LOSSES OF 0FFSITE PGWER 1.
Date: April 13,1971 Event: Loss of normal offsite supply to bus lA05.
Cause
Wiring error on relay test switch prevented blocking of undervoltage trip while relay was being tested.
Results: Diesel generator 3D started and picked up bus lA05.
No other offsite power supplies were affected.
There were no voltage or frequency problems.
Normal power supply was restored a short time later. There was no effect on the unit since it was shut down at the time.
B.
TOTAL LOSSES OF 0FFSITE P0.WER 1.
Date: February 5,1971 Event: Loss of all offsite power and all transmission lines.
Cause
Major ice storm and improper relay operation.
Results: All transmission lines were lost and differential lockout relays on transformers 1X03,1X04 and 2X04 tripped. Both diesel generators started and picked f
up the safeguards loads on Unit I which was not on
]
9' D 144t 199 7911300 5/3
.M Mr. Harold R. Denton, Director November 16, 1979 B.
TOTAL LOSSES OF 0FFSITE POWER - continued 1.
Results: line at the time. One bus on Unit 2 was not picked up because a control power fuse had blown.
Unit 2 was not licensed yet and no fuel had been loaded. The restoration of offsite power to the plant was delayed by the need to evaluate gas saales from the transformers which had locked c.
The outage lasted for 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and 22 t.nutes. There were no voltage or frequency problems.
2.
Date: October 13, 1973 Event: Loss of all offsite power to safeguards buses.
Cause
A lightning mast failed and fell on transformer 2X03 while transformer 1X03 and the gas turbine generator wem temporarily out of service.
Results : The diesel generators started and supplied power to the safeguards buses of both units. Unit 1 was in hot shutdown and Unit 2 did not trip. The gas turbine generator was returned to service 55 minutes after the event and supplied offsite power to both units for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 30 minutes. At th 4t time transformer 1X03 was returned to service. There were no voltage or frequency problems.
3.
Date: April 27,1974 Event: Loss of all offsite power to Unit 1.
Cause
A wire lifted in the switchyard control house during a relay modification initiated a breaker failure scheme which isolated 345kV bus section 1.
Results: The isolation of B.S.1 removed the power supply to transfomer 1X03, the Unit 1 high voltage station auxiliary. A fast transfer took place on the 13.8kV bus which would have restored the offsite power to Unit 1, but the 4kV bus under-voltage relays operated before the transfer.
These undervoltage relays trip the connections to offsite power and start the diesel generators.
The buses which were now being supplied by the diesel generators were synchronized to the off-site power supply almost innediately by the operator and the system was returned to nomal.
There wem no unit trips, nor were there any voltage or frequency problems.
Very truly yours, C. W. Fay, Director Nuclear Power Department 1444 100
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| 05000333/LER-1979-001-03, /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | | | 05000333/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000333/LER-1979-002-03, /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | | | 05000333/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000333/LER-1979-003-03, /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | | | 05000333/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000333/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000333/LER-1979-004-03, /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | | | 05000333/LER-1979-005-04, /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | | | 05000333/LER-1979-005, Forwards LER 79-005/04L-0 | Forwards LER 79-005/04L-0 | | | 05000333/LER-1979-006, Forwards LER 79-006/03X-1 | Forwards LER 79-006/03X-1 | | | 05000333/LER-1979-006-03, /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | | | 05000333/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000333/LER-1979-007-03, /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | | | 05000333/LER-1979-008-03, /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | | | 05000333/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000333/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000333/LER-1979-009-03, /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | | | 05000333/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000333/LER-1979-010-03, /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | | | 05000333/LER-1979-011-03, /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | | | 05000333/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000333/LER-1979-014, Forwards LER 79-014/01T-0 | Forwards LER 79-014/01T-0 | | | 05000333/LER-1979-014-01, /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | | | 05000333/LER-1979-015, Forwards LER 79-015/03X-1 | Forwards LER 79-015/03X-1 | | | 05000333/LER-1979-015-03, /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | | | 05000333/LER-1979-020, Forwards Revised LER 79-020/03X-1 | Forwards Revised LER 79-020/03X-1 | | | 05000333/LER-1979-020-03, During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | | | 05000333/LER-1979-023-99, Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | | | 05000333/LER-1979-023, Forwards Revised LER 79-023/99X-1 | Forwards Revised LER 79-023/99X-1 | | | 05000333/LER-1979-024, Forwards Revised LER 79-024/03X-1 | Forwards Revised LER 79-024/03X-1 | | | 05000333/LER-1979-024-03, Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | | | 05000333/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000333/LER-1979-026-03, /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | | | 05000333/LER-1979-027-03, /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | | | 05000333/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000333/LER-1979-028-03, /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | | | 05000333/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000333/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000333/LER-1979-029-03, /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | | | 05000333/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000333/LER-1979-030-03, /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | | | 05000333/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000333/LER-1979-031-03, /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | | | 05000333/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000333/LER-1979-032-03, /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | | | 05000333/LER-1979-033-03, /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | | | 05000333/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000333/LER-1979-034-03, /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | | | 05000333/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | |
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