ML19242A879

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LER 79-042/03L-0 on 790706:support Beams for Snubber B RHR Heat Exchanger Steam Condensing Line Were Unable to Carry Loads Under Worst Case Seismic Conditions.Cause Unstated. Beams Reinforced Per Redesign & Plant Mod
ML19242A879
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/02/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19242A873 List:
References
LER-79-042-03L-01, LER-79-42-3L-1, NUDOCS 7908060545
Download: ML19242A879 (1)


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  • c ,nd h,ngarn nn c , f o r y.j o a Irelated lines, resulting from IE Bulletin 79-07. the sunoort beams for snubber o 4 11E11-49SS334 "B" RHR heat exchanger steam condensing line. were not canable of I o s lcarrying the calculated loeds under worst case seismic conditions. l 0 6 ITechnical Specification 3.7.5. 6.9.1.9b I cl7 l l d ti l l

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