05000325/LER-1979-052, Supplementary LER 79-052 03X-1:on 790728,rod 26-15 Had No Position Indication at Notch 38 & Rod 18-23 Had No Position Indication at Notch 30.Caused by Defective Reed Switches. Switches Replaced.Problems May Be Generic

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Supplementary LER 79-052 03X-1:on 790728,rod 26-15 Had No Position Indication at Notch 38 & Rod 18-23 Had No Position Indication at Notch 30.Caused by Defective Reed Switches. Switches Replaced.Problems May Be Generic
ML19209B758
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 09/28/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B755 List:
References
LER-79-052-03X, LER-79-52-3X, NUDOCS 7910100404
Download: ML19209B758 (1)


LER-1979-052, Supplementary LER 79-052 03X-1:on 790728,rod 26-15 Had No Position Indication at Notch 38 & Rod 18-23 Had No Position Indication at Notch 30.Caused by Defective Reed Switches. Switches Replaced.Problems May Be Generic
Event date:
Report date:
3251979052R00 - NRC Website

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LICENSEE EVENT REPORT Previous Report Date:

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- EVENT DESCRIPTION AND PRO 8 ABLE CONSEQUENCES h O 21 lDuring a normal reactor startup. rod 26-15 had no positien indication at notch 38 and 1 o

a rod 18-23 had no position indication at notch 30.

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