05000325/LER-1979-050-03, /03L-0:on 790904,during Normal Operation,Drywell Oxygen/Hydrogen Monitor CAC-1263 Was Observed Making Step Increase.Cause Unknown.Instrument Recalibr & Returned to Svc Satisfactorily

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/03L-0:on 790904,during Normal Operation,Drywell Oxygen/Hydrogen Monitor CAC-1263 Was Observed Making Step Increase.Cause Unknown.Instrument Recalibr & Returned to Svc Satisfactorily
ML19209B243
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/01/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B237 List:
References
LER-79-050-03L-01, LER-79-50-3L-1, NUDOCS 7910090371
Download: ML19209B243 (1)


LER-1979-050, /03L-0:on 790904,during Normal Operation,Drywell Oxygen/Hydrogen Monitor CAC-1263 Was Observed Making Step Increase.Cause Unknown.Instrument Recalibr & Returned to Svc Satisfactorily
Event date:
Report date:
3251979050R03 - NRC Website

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LICENSEE EVENT REPORT

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8 60 61 DOCKdT NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEC UENCES h lDuring normal plant operation, the operator noticed that the drywell oxygen / hydrogen o

2 f5T31 Imonitor, CAC-1263, made a step increase for -

apparent reason. Drywell oxygen con-l ITITl I centration did not exceed 47..

l [TTTl Technical Specifications 3.6.6.4, 6.9.1.9b l

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42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h Li o l A calibration check _ found that the instrument "zero" had shifted approximately 407.

m l for no apparent reason, giving about a 27. shift in the monitor. The instrument was rqT) l recalibrated and returned to service satisfactorily. As this is the first time that ;

g l the instrument has been out of calibration since going to a biweekly calibration, j

I this is considered an isolated event and no further action is required.

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NAME OF PREPARER PHONE: