05000325/LER-1979-062-01, /01T-0:on 790828,during Review of Core Load Videotapes,Bundle 29-10,Serial Ljo 197 Discovered Placed in Core 180 Degrees from Required Orientation.Cause Not Apparent from Review of Refuel Records.Procedure Revised

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/01T-0:on 790828,during Review of Core Load Videotapes,Bundle 29-10,Serial Ljo 197 Discovered Placed in Core 180 Degrees from Required Orientation.Cause Not Apparent from Review of Refuel Records.Procedure Revised
ML19208A276
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 09/11/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19208A272 List:
References
LER-79-062-01T, LER-79-62-1T, NUDOCS 7909130318
Download: ML19208A276 (2)


LER-1979-062, /01T-0:on 790828,during Review of Core Load Videotapes,Bundle 29-10,Serial Ljo 197 Discovered Placed in Core 180 Degrees from Required Orientation.Cause Not Apparent from Review of Refuel Records.Procedure Revised
Event date:
Report date:
3251979062R01 - NRC Website

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s 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h A lD arine a review of the Unit 1 core load videoenpos te uns discovered ehne bundin l

l"b5Tiil 129-10, Serial Number LJO 197 had been placed in the core 180 from the recuired I

o 4 l orientation. This was verified by channel fastener location and serial number alien- !

o s iment. Preliminary analysis by G.E. indicated that continued operation of the unit canl 0 6 the Supported with this condition.

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3*a 3ts 31 40 41 42 43 A4 47 CAUSE DESCRtPTION AND CORRECTIVE ACTIONS o i l A review of refueline records indicated that bundle LJO 197 was moved durine the 1979 I i

i i I refueline outace from position 33-02 to position 29-10 with no chance in orientation I

2 trequired. An evaluation of the fuel movement plan indicates no apparent cause for thel 3 Ibundle rotation. Core verification by a SRO, a Nuclear Engineer, and a Q.A. Techniciaft I failed to detect the rotated bundle.

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LER CONTINUATION - R04 1-79-062 Facility:

BSEP Unit No. 1 Evenc Date:

08-28-79 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS:

Conservative operating limits for bundle LJO 197, based on analyzed values given the BSEP Unit No. I supplemental reload licensing packagt submitted for cycle 2 (NEDO 24166), were determined and power was reduced to approximately 88% in order to e serve these limits. Tha daily core parameter limits was re-vised to include these special limits for bundle LJG 197.

It was verified that no other bundle was rotated in either Unit 1 or Unit 2.

Anslyses to determine the feasibility and desirability of continued operation were initiated by both CP&L and G.E. and the results of these analyses will be provided in a supple-mental report.

It was verified that the fuel loading error is analyzed for in the current cycle and results in no safety Ibnit violations. It was also verified that no transients upsets which have occurred this cycle could have caused a safety ifmit violation. It is General Electric's opinion that the single misoriented bundle does not compromise the current license basis.

The core verification proccdure will be revised to include:

1)

Initials for each bundle orientation requiring that at least 2 of 5 methods of verification be used, and those methcds used, identified.

2) Complete core verification of core loading and orientation, from the core load videotapes, by an independent verification team consisting of at least two of the following personnel:

a) Operating Supervisor b) Q A. Supervisor c) Engineering Supervisor d) Representative from CP&L Nuclear Fuels e) Reactor Project Engineer f) Other technically qualified personnel

3) Fuel movement sheets will be revised to add columns for channel fast-ener orientatien so that the refueling floor SRO can determine bundle orientati2n both before and after a move.

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