05000325/LER-1979-059-03, /03L-0:on 790810,during Reactor Startup Discovered Number 7 Superimposed on Number 1 Digit for Position Indication on Rod 14-47.Caused by Problem in Drywell Prototypic Inlet Piping Probe

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/03L-0:on 790810,during Reactor Startup Discovered Number 7 Superimposed on Number 1 Digit for Position Indication on Rod 14-47.Caused by Problem in Drywell Prototypic Inlet Piping Probe
ML19208A036
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 09/07/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19208A027 List:
References
LER-79-059-03L-01, LER-79-59-3L-1, NUDOCS 7909120443
Download: ML19208A036 (1)


LER-1979-059, /03L-0:on 790810,during Reactor Startup Discovered Number 7 Superimposed on Number 1 Digit for Position Indication on Rod 14-47.Caused by Problem in Drywell Prototypic Inlet Piping Probe
Event date:
Report date:
3251979059R03 - NRC Website

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8 60 61 DOCKCT NUMBER 60 63 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 0

2 IDuring a normal reactor startuo. the operator noticed that a "7" was superimposed on 1

o a Ithe "ones" digit for positfon indication on rod 14-47 l

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o lAn investigation revealed that the problem was in the PIP orobe located in the drvwell.]

i i IThis oroblem will be corrected during the next outace of suf ficient length.

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NAME OF PREPARER PHONE: