ML18153A888

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Insp Repts 50-280/94-02 & 50-281/94-02 on 940102-0205. Violations Noted.Major Areas Inspected:Plant Status,Review of Plant Minor Mod,Inservice Testing,Operational Safety Verification & Maint Insp
ML18153A888
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/07/1994
From: Belisle G, Branch M, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153A887 List:
References
50-280-94-02, 50-280-94-2, 50-281-94-02, 50-281-94-2, NUDOCS 9403150283
Download: ML18153A888 (21)


See also: IR 05000280/1994002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

Report Nos.:

50-280/94-02 and 50-281/94-02

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos. : - 50-280 and 50-281

License Nos~:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

January 2 through February 5, 1994

Inspectors:

Approved by:

Scope:

~LJ ~

fin__*

~W. Branc~or Resident

Inspector

,C(.J ~(*,~-, ~

W. Yo~Res1d~nt Inspector

S. G. Ting~n, Resident Inspector

G. A. Belisle, Sect)on Chief

Division-of Reactor Projects

SUMMARY

.1- ?- '!Y:

Date Signed

J-')- '?f

Date Signed

.s-?-<ff.

Date Signed

"3 - 7 -- ,(,./

Date Signed

This routine resident inspection was .conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, review of plant minor modifications, inservice testing, and

action on previous* inspection items. . While performing this inspection, the

resident inspectors conducted reviews of the licensee's backshifts, holiday or

weekend operations on January 6, 7, 21, 22, 23, 24, 25 and February 2 and 3,

1994.

9403150283 i;ggg~80

PDR

ADOCK

PDR

G

2

Results:

Plant Operations functional area:

Non-cited violation 50-280/94-02-01 was identified for failure to follow fire

seal inspection requirements contained in a surveillance procedure

(paragraph 3;b).

An .Unresolved Item was identified associated with reactor vessel level

indication problems that occurred while shutdown (paragra~h 3.i).

The magnitude qf the Unit 2 turbine runback on January 4 appeared to b~

excessive and challenged the operators. Their response to the event was good:

(paragraph 3.c).

-

The event assessment* of the Unit 2 runback was-thorough (paragraph 3.c).

The Unit 1 shutdown was well tontrolled and command and leadership were

evident (paragraph 3.e).

_The licensee demonstrated their ability to react to the icing conditions at

the low level intake structure that occurred on January 19.- However, the

licensee's cold weather protection program did not anticipate the icing

conditions that occurred during extreme cold weather (paragraph 3.f).

Several examples where personnel had to be prompted to initiate station

deviation reports for conditions adverse to quality were noted.

For the most

part~ operations has exhibited a very low threshold for station deviations and

this recent trend was not typical performance.

Operations management is

reviewing this is~ue with operation personnel (paragraphs 5.c and 7).

Operator response to two events indicated an apparent lack of understanding of

equipment operation.

The first involved a second Unit 2 turbine runbatk when

_load was increased above 70% first stage pressure with a runback signal

present (paragraph 3.c). The other example involved an unlicensed operator

improperly attempting to adjust -the #3 emergency diesel generator reactive

load.

This resulted in briefly operating equipment on the 1-H bus at

undervoltage conditions (paragraph 5.c)~

Maintenance functional area:

The service water- fl ow test to two Unit 1 reci rcul at ion spray heat exchangers

was well organized and conducted (paragraph 3.g).

An Unresolved Item was identified for activities involving a pressurizer

hydrogen burn (paragraph 3.j).

Rod control performance problems continue to occur.

The maintenance performed -

on the Unit 2 rod control system to troubleshoot and repair the step demand

counter indication was efficientlf accomplished and there was good

communications between operations and instrument and control personnel.

-

3

Unit l rod control improvements are being implemented and reliability centered

maintenance data is being utilized (paragraph 4).

A Unit 1 undervoltage and degraded voltige engineered safety feature actuation

surveillance was well coordinated and.controlled. A number of equipment

problems were noted during the 1-H bus test that required correction and

evaluation (paragraph 5.c).

The desigh chinge to waterproof the actuator for l-CW-MOV-106A was

accomplished without any deficiencies noted .. It was evident that the

mechanical and electrical maintenance personnel were prepared to implement

this design change (paragraph 6.a).

Engineering functional area:

The procedures developed by engineering support and utilized to accomplish the

Unit 1 shutdown worked well, in that, operators did not exhibit. significant

difficulties in understanding and performing the procedural steps

  • (paragraph 3.e).

The design change pack~ges for implementing minor modifications to .valves

l-CW-MOV-106A and 2-SI-MOV-28628 were good quality and were accomplished by

maintenance personnel without any significant difficulties encountered

(paragraphs 6.a and 6.b) .

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

  • J. Downs, Superintendent of Outage and Planning
  • D. Erickson, Superintendent, of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

B. Hayes, Supervisor, Quality Assurance

    1. M. Kansler, Station Manager
  • A. Keagy, Nuclear Materials

C. Luffman, Superintendent, Security

  • J. McCarthy, Superintendent of Operations
  • A. Price, Assistant Station Manager

R. Saunders, Assistant Vice President, Nuclear Operations

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • G. Woodzell, Nuclear Training

NRC Personnel

    1. M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector

J. York, Resident Inspector

  • Attended Exit Interview on February 8, 1994. *
  1. Attended Exit Interview on March 7, 1994.

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initial isms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in a power coast-down for refueling.

The unit was shutdown on January 22 for a planned 64-day refueling

outage .

Unit 2 operated at 100% power for most of the inspection period and at

the end of the period the unit had been on lirte for 68 days ..

On

January 4, the unit experienced a turbine runback due to testing on the

NI system (see paragraph 3.c). * On January-19, power was reduced to 92%

2

for a short period of time due to icing conditions at the low level

intake canal (see paragraph 3.f). *

3;

Operational Safety Verification (11707, 42700)

The inspectors conducted frequent tours of the control . room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended pl~nt status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices,. plant security programs and

housekeeping.

Deviation reports were reviewed ti assure that potential

safety concerns were properly addressed and reported.

ar

Licerisee 10 CFR 50.72 Reports

(1)

(2.)

On January 7, the licensee made a non-emergency four-hour

10 CFR 50.72 report due to an ERFCS failure that rendered

the SPDS unavailable.

The ERFCS failed at 12:20 a.m. and

was retur*ned to service at 1:45 a.m.

The ERFCs' failure

occurred when a disk drive malfunction rendered the on-line

  • data processor inoperable, and. the standby data processor

failed to automatically transfer to the data collection mode

of operation. *Wh~n this condition was identified, personnel

manually placed the standby data processor into operati.on.

This restored the ERFCS to an operable condition.* The disk

drive that had previously malfunctioned was replaced and t~e

data processor was returned to its normal bperating mode.

On February 4, the licensee made a non-emergency four-hour

10 CFR 50.72 report due to discovering a potential leakage

path from Unit 1 contain~eht. While inspecting the SW

piping inside containment, a small hole was found in the

piping downstream of recirculation spray heat exchanger

1-RS-E-18.

The unit was in cold shutdown when the hole was

identifiedi * Calculations performed by*the licensee

. indicated that the hole could have allowed leakage in excess

of that allowed by 10 CFR 50 Appendix J. The hole was

scheduled to be repaired prior to restarting the unit from

the current RFO.

The inspectors performed an initial assessment of the safety

significance of the hole in the SW pipe as it related to

containment integrity. The pipe with the through wall leak,

formed the membrane barrier between the inside containment

atmosphere and the ~ervice water.

In addition to the

  • . membrane barrier. the penetration in question was also

isolable and was in-fact isolated by closed containment

isolation val~es.

The SW dischafge piping is monitored by a

3

radiation monitor that would alert the operators to isolate

the RS heat exchanger if necessary.

With the one RS heat

exchange~ isolated, 100% ~ontainment heat removal capacity

would still be available.

At the end of the inspection

period the licensee was still evaluating the issue and an

LER is scheduled to be issued within the 30 day period.

The

inspectors continue to follow the licensee's assessment of

this item.

b.

Unit 1 Cable.Vault Fire Barrier Penetrati-0n Seals

During a routine walkdown of the Unit 1 cable vault upper section,

the inspectors noted that a metal duct was covering a wall area

that contained three HS system fire barrier penetration seals.

This wall was required to be a 3~hour fire resistance rated

barrier in accordance with the Appendix R program.

The inspectors

questioned if the duct or seals installed ar6und the piping

provided the required fire barrier.

The inspectors were informed

that the penetrations were sealed and that the metal duct was not

the design fire barrier.

Because the duct covered the three HS fire barrier penetration

seals, the seals were not able to be visually inspected unless the

duct was removed.

As a result of the inspectors questioning'the

existence of adequate fire seal~, the licensee attempted to

inspect the three penetrations without removing the duct.

The

licensee was unable to verify that the penetration fire seals were

installed. The fire barriers were declared inoperable and a fire

watch was posted in accordance with TS 3.21.B.7 .. The duct was

then removed, and it was concluded that no fire barrier seals

existed in these penetrations.

Fire barrier seals w~re

subsequently installed.

TS 4.18.G.l.a requires that fire barrier penetration seals be

visually inspected every 18 months.

Procedure O-LPT-FP-001, Fire

Barriers, implemented TS 4.JB.G.1.a ana was last performed in

September 1993.

The inspectors reviewed the procedure's

performance copy dated September 1993, and concluded that the

procedure was completed without properly inspecting the three HS

fire ba.rri.er penetration seals. The licensee indicated that

personnel performing the inspections did not properly interpret

the fire barrier inspection requirements contained in O-LPT-FP-001

for inaccessible seals and; therefore, failed to identify that the

seals were not installed.

In order to prevent recurr~nce, the licensee was rev1s1ng

O-LPT-FP-001 to clarify inspection requirements for inaccessible

seals and was planning to provide additional training to personnel

that inspect fire seals to*ensure that inaccessible seals are

properly inspected.

At the end of the inspection period, the

licensee was developing a program to inspect additional mechanical

4

system fire barrier penetration seals in order to determine if

. other seals have been properly inspected.

The licensee had

already implemented an extensive inspection program for electrical

penetration fire seals.

The licensee reviewed the Appendix R Report combustible loading

.analysis for the areas adjacent to the three penetrations and

concluded that there was not a significant operability concern.

The adjacent areas were classified as less than one minute fire

loading zones and therefore would not provide a sufficient

concentration of combustibles from any flames, smok~ or hot gases

generated from a fire. The inspectors' review of the information

provided resulted in similar conclusions.

The insp~ctor~ concluded that the failure to properly irite~pret

procedure O-LPT-FP-001 fire seal inspection requirements was a

violation of TS 6.4.D which requires that procedures be followed.*

This was identified as NCV 50-280/94-02-0l; Failure to Follow Fire

Seal Inspection Requirements. This *NRC identified violation is

not being cited because criteria specified in Section VII.B of the

NRC Enforcement Policy were satisfied.

c.

January 4 Unit 2 Turbine Runback

on January 4, Unit 2 experienced a turbine runback from 100% to.

appioximately 51% power.

The runback occurred during a special

test of power range NI channel N41.

This test is designed to

gather data to support the September 1994 RFO core reload *. The

NIS runback began immediately after the I&C technicians connected

the test equipment inside the NI drawer.

The plant's response to

the event was as expected, i.e., the steam dumps opened to control

steam pressure and inward rod motion controlled T avg.

However,

the turbine runback to 51 percent power was e~cessive and.

approximately 19 percent greater than designed.

The operators*

started an additional condensate pump and bypassed condensate

polishing to ensure adequate MFWP suction pressure. After plant

conditions were stable, the operatqr attempted to increase turbine

load to close the steam dump valves.

When turbine load increased

above 70% another runback to approximately 55% power occurred

because th_e NIS runback signal was still present. This' second

funback resulted from the operator's lack of understanding*of the

control logic.

The licensee performed Event Assessment 94-01 to identify the root -

causes and any corrective actions associated with the event~

The

inspectors reviewed the assessment which concluded that the NIS

runback was caused by a channel N41 failure. The channel failed

due to installing test equipment that was not grounded.

The

channel failed when the control power fuses blew immediately

following connecting the test device (recorder) to plant

equipment.

The assessment concluded that the test equipment was

not grounded because the test cart receptacle used to energize the

5

test equipment did not provide an adequate ground.

The inspectors

concluded that the assessment was thorough.

Corrective actions

included repl_acing the test cart receptacle and modifying the

_ method of checking test equipment prior to use.

Previously,

pieces of test equipment were checked individually prior to

installation. Under the new method, the test equipment will be

assembled and checked as a unit prior to connection to a plant

system. -

The assessment also concluded that the turbine ran back 19%

further than the design setpoint of 70% of full load. This was -

previously identified as a recurring probl~m and was attributed to

governor valve operating characteristics. A modification to

eliminated this automatic runback feature is scheduled for

implemeritatio~ during the Unit 2 1994 RFO and Unit 1 1995 RFO.-

d.

Unit 1 Containme_nt Integrity Verification

On January 22, the inspectors verified that containment integrity

was not compromised while bleeding steam for temperature and

pressure control when the plant was being maintained in hot

. shutdown.

Specifically, the inspector~ verifted that proper

admini~trative controls ~ere established and maintained while one

of the three MSIV bypass valves was unlocked and throttled open.

Th rot ti i ng of the bypass valve provided for fine temperatu*re

control by restricting the flow path used to bleed steam to the

condenser via the main steam dump valves.

I

The inspectors noted that adequate administrative controls wer~

implemented by procedures, and that an operator was stationed by

the valve with communication to the control room in the event that

the valve would have to be closed for containment integrity.

e.

Unit 1 Shutdown- for RFO

_ On January 21 and 22, the inspectors witnessed the shutdown of

Unit 1 in preparation for the RFO.

The unit ramp down rate was

150 MW/HR and the unit was at 53.5 % power when the shutdown was

initiated. Procedures involved included l-GOP-2.1, Unit Shutdown,

Power Decrease From Maximum Allowable Power to 25% to 30% Reactor

Power, revision 3; )-GOP-2.2, Unit Shutdown, 25% - 30% Reactor

Power to 2% Reactor Power, revision 4; and l-GOP-2~3, Unit

Shutdown, 2% Reactor Power to HSD, revision 3. - Th*e * inspectors*

concluded that the shutdown was well controlled and command and

control was evident. It was clear that the unit SRO was in charge

of the evolution, procedures were followed, and operators

continuously self~checked their actions.

The procedures, upgraded

by engineering support and utilized to accomplish the shutdown,

appeared to work well, in that, operators did not exhibit

significant difficulties in understanding and performing the

procedural steps.

. ***

6

The only time the operators were challenged during the shutdown

was when SG level control was transferred from automatic to

manual.

Although there were several swtngs in SG le~els while in

manual control, operators successfully controlled the level in

each SG within acceptable limits. This control prevented an

automatic reactor trip due to high or low SG level. The

inspectors discussed the manual control mode of maintaining SG

level with operators- and have witnessed similar occurrences during

startups and other shutdowns.

The inspectors concluded that the

feedwater control system's manual operation challenges operatofs.

f.

Problems at Low Level Due to Extreme Cold Weather

On several occasions throughout the inspection period ambient

. temperatures were significantly below normal.

On January 19, ice

buildup on the low level intake canal trash racks and rotating

screens restricted flow to the suction of the CW pumps.

This

condition degraded CW performance which made it difficult for

.

operators to maintain intake canal level.

As immediate corrective

actions, waterbox inlet MOVs were throttled to conserve intake

canal inventory and personnel were stationed at the low level

intake structure to remove the ice from the rotating screen

assemblies. Throttling water box inlet MOVs resulted irr the need

to reduce Unit 2 reactor power.

Intake canal level decreased to

26.2 feet before level was stabilized. Station management manned

the TSC in order to coordinate and implement the following actions

at the low level intake structure to improve CW performance:

The upper stop log was installed in -tne inlet bay to each CW

pump.

Every third basket was removed in each of the rota~ing

screen assemblies.

The upper rotating screen assemblies were covered with

herculite and heaters were placed in the area.

A tug boat was utilized to break ice at the entrance to the

low level intake structure.

Personnel were stationed at the low level intake structure

to monitor conditions.

There were no icing problems at the intake canal high level

structure; however, several actioris were implement~d to prevent

any problems from occurring. The upper stop log was installed in

each inlet bay and every other basket was removed in each of the

  • rotating screen assemblies. Herculite and heaters were also

installed at the rotating screen assembles.

The inspectors concluded that the licensee's response to the 1c1ng

conditions at the low level intake structure was effe~tive in

7

improving CW pump performance. This action allowed the units to

stay on line during a period when the electrical demands forced

rotating "black outs" in the ~ervice area.

The cold weather

protection program, implemented several months earlier, had not

anticipated the icing conditions th~t occurred at the low level

intake canal on January 19.

At the end of the inspection period,

the licensee was evaluating revisions to the cold weather

protection program to better anticipate extreme cold weather

,effects on the station.

g.

Service Water Flow To Recirculation Spray Heat Exchangers

On January 24, the inspectors observed portions of the SW flow

test conducted on the Unit 1 RSHXs 1-RS-E-lB and 1-RS-E-lC.

The

test was performed in accordance with special test procedure

  • 1-ST-0310, Recirculation Spray Heat Exchanger Service Water Flow,

dated January 21, 1~94. This test had. two purposes:

(1) to

collect data to verify that design basis accident service water

fl ow was adequate to reject design basis containment heat 1 oads,

and (2) to collect data on valves l-SW-MOV~l04B, RS HX B SW INLET

and 104C, RS HX C SW INLET, to support GL 8~-10 reviews.

This

test was performed at the same time the J-bus logic test procedure

l-OPT-ZZ-002 was performed.

The inspectors observed part of the test preparations, the pre-job

briefing, and reviewed the test procedure.

The test was monitored

from both the main control room and the Unit 1 safeguards area by

the inspectors.

Preliminary results identified that the SW flow

through both heat exchangers was good and very little, if any,

blockage exited. The actual calculations are currently being

performed by the engineering organization and will be reviewed by

the inspectors. The test was well organized and progressed

smoothly.

No discrepancies were identified.

h.

Contamination of Worker

While inspecting Unit l RFO activities, the inspectors reviewed a

worker contamination event that occurred on January 27.

When a

contract worker (welder/rigger), who had been handling deck

grating, attempted to exit the containment building, contamination

was detected on his hand by the PCM-1.

His hand was frisked

(8000 cpm) and several decontamination attempts by HP personnel

and by medical personnel were unsuccessful.

The licensee's doctor

placed ointment, bandages and a glove on the worker's hand prior

tri allowing him to leave the site. The worker was given

instruction by HP personnel which included returning to the site

for further decontamination efforts.

HP continued to monitor the

individual and on February 2 *the contamination was no longer

present.

The estimated external extremity dose from the

contamination was 703 mrem.

The estimated internal dose was less

than 0.1 mrem.

The inspectors discussed the worker contamination

event.with*Region II radiological protection personnel and they

8

determined that the licensee's actions were appropriate.

The

NRC's detailed review of this event is documented in NRC

Inspecti6n Report Nos. 50-280, 281/94-05.

i.

Unit 1 Reactor Vessel Level Indication

At approximately _10:40 a.m. on February 1, the level in the

reactor vessel standpipe decreased unexpectedly.

Level in the

standpipe was initially 18.0 feet and-decreased to 16.5 feet over

a ten minute period. Operators.isolated letdown and initiated

makeup to the reactor vessel from the RWST.

The*containment,

auxiliary building and safeguards valve pit were inspected for

leakage and no leakage was identified. A reactor vessel level of

16.5-feet is 1.2 feet above the level designated as reduced

inventory.

Approximately 15 minutes after the lev~l was noted to be

decreasing, Vent/Vent radiation monitors alarmed in the ~lert

range indicating that activity in the containment atmosphere had

incr~ased. Air samples obtained fro~ the containment refueling

floor indicated that the DAC was 1.3;

The DAC prior to this event

was O.

The Vent/Vent peak release rate was calculated to be 8~07%

of TS.

-

.

Level in the reactor vessel was returned to 18 feet and remained

stable. The containment was purged and activity in the

containment atmosphere returned to normal.

The inspectors monitored refilling of the vessel and reviewed the

controlling procedure to verify that level changes and volume

changes were as expected. Additionally, th~ inspectors performed

a walkdown of the standpipe assembly to determine if there were

any obvious eiplanations for the indicated level decreas~.

The

inspectors noted that there was a long torturous path from the

reactor head to where the v~nt piping penetrates the pressurizer.

The reactor vessel head vent was designed to ensure equal pressure

existed between the vented level stand pipe and the vessel. Most

of the head vent piping was disconnected at the time of the

indicated level drop to allow installation of the cavity seal.

However, the vent path described could result in trapping of

pockets of water in several a_reas of the system.

The inspectors

discussed their observations with the licensee to ensure that the

vent pa~h was reevaluated as part of the task teams efforts.

When the event occurred, the reactor vessel head was vented to the

containment via an open ended pipe.

Personnel in containment

noted that water sprayed from the head vent open ended pipe at

approximately the same time the reactor vessel level started to

decrease.

The reactor had been vented to the containment via the

open ended pipe for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> previously and reactor

vessel level indication was stable. Ther~ were no obvious

. **

j.

9

perturbations at the time of the event that could have resulted in

a decreasing reactor vessel level.* The licensee appointed a task

team to investigate this event. *The task team concluded *that the

most prtibable cause for the inaccurate ~tandpip~ level indication

was a restriction in the reactor head vent piping. Subsequent to

the inspection period, testing performed was unable to verify that

this conclusion wa~ correct.

During the last Unit l RFO, a similar decrease in reactor vessel

level occurred when the reactor head was d~tensioned.

Troubleshooting performed at that time did not identify any

blockages in the reactor vessel standpipe assembly. This event

and other reactor vessel-level indication problems were discussed

in NRC Inspection Report Nos. 50-280, 281/92~07.

The reactor vessel standpipe assembly is the sole reactor vessel

level indication utilized when the reactor vessel water level is

maintained below the reactor .head flange.

It should be noted

that there is another level monitor installed as discussed in

Generic Letter 88-17, Loss of Decay Heat Removal.

However, this.

monitor is only used during* mid~loop operations since it's range

  • is from the top of the loop piping to the bottom of the loop

piping. This second monitor would be off-scale high during

operations above mid-loop as was the case described above .

As indicated above; problems with the Unit l reactor vessel

standpipe assembly indication continue to occur.

Incorrect

standpipe level indications could result in an unplanned entry

into a ieduced inventory condition or a loss of shutdown cooling.

This contern was discussed with licensee management.

At the end

of the inspection period, the licensee was developi~g a strategy

to identify the cause of the reactor vessel level problems .. Until

the problem's root cause is identified and corrections actions are

taken, this item will b~ identified as URI 50-280/94-02-02, Review

Reactor Vessel Level Problem.

February 3 Unit l Pressurizer Hydrogen Ignition

On February 3, 1994, at approximately 2:38 a.m., spikes were

observed on the pressurizer level instruments.

At the same time,

a loud rumbling sound was heard in containment.

The containment

vent radiation alarm was feceived and containment was evacuated.

At the time of the event, the pressurizer was drained and vented

via open filtered pipes to the containment atmosphere.

Apparently

pressure fluctuations inside the pressurizer caused radioactive.

gases inside the pressurizer to be expelled into containment.

The

highest radiation monitor readings on the containment monitor was

3300 counts per minute and a reading of 8,500 microcurie per

second was noted on the Vent/Vent monitor.

This Vent/Vent level

was estimated to be approximately 30% of TS limits.

One worker

. .

10-

received an estimated 7 mrems *internal exposur*e and a total dose

of 16 mrems.

The cause of the pressurizer pressure increase was investigated by

both the licensee and the inspectors.

The inspectors interviewed

workers involved and conducted an independent inspection of the

_ pressurizer head area.

The inspectors noted that the FME screens

that were taped over the pressurizer side of thi piping where the

three safety valves were removed were discolored and appear~d

burned.

Discussions with the licensee indicated that they were

i~vestigating a possible cause that involved a hydrogen gas burn

in_side the pressurizer. A modification to eliminate the

pressurizer loop seals was in progress. Welding activities

associated with the modification may have ignit~d hydrogen gas

that had tome out of solution and accumulated inside the

pressurizer and associated piping.

The licensee initiated DR S-94-0263 to d_ocument this occurrence.

Additional controls for welding on the primary system were also

imposed.

These required measuring for explosive gases prior to

initiating an arc.

The licensee's initial investigation also

included determining if similar events had occurred at other

nuclear facilities.

On the afternoon of February 3, after

reviewing the preliminary information that was submitted, SNSOC

determined that a hydrogen burn had occurred. The SNSOC also

determined that the event was not reportable based on a review of

their emergency plan and 10 CFR 50.72 and 50.73.

However, a *

voluntary LER wil 1 be submitted to alert the industry of the

occurrence.

The inspectors cbntinue to follow the licensee's investigation and

root cause determination of this event. This item is identified

as URI 50-280/94-02-03, Evaluation of Pressurizer Hydrogen Burn.

Issues that need resolving included, determining the source of the

hydrogen since the RCS had been degassed to< 4 cubic

centimeters/Kilogram during the plant shutdown/cooldown

evolutions. Additionally, welding procedures were being reviewed

.to determine why there were no precautions to monitor for

explosive gases prior to welding on the RCS.

The licensee was

al so considering utilizing industry data to evaluate the

pressurizer stresses associated with this event.

Within the areas inspected, one non-cited violation was identified.

4.

Maintenance Inspections (62703, 42700)

During the reporting period, the inspectors _reviewed the following

maintenance activities to assure compliance with the appropriate

_ procedures.

11

Rod Control Activity

Unit 2 shutdown bank.B group 2 step demand counter was identified to be

malfunctioning while performing a routine control rod exercise.

surveillance test on January 26.

Operators noted that upon releasing

the rod motion lever, the step demand counter indicated that shutdown

bank B group 2 rods continued to move inward one extra step.

On that

same day the shutdown bank B group 1 and 2 step demand counter driver

card was replaced ard shutdown bank B rods were exercised. During the

exerctse, the group 2 rod step demand counter continued to indicate th~t

rods moved inward one additional step when the rod motion lever was

released.

In. addition, the group 1 rod step demand counter indication

malfunctioned during the exe~cise. The group 1 rods were inserted to

212 steps and then withdrawn.

The step demand counter indicated

properly during r*od insertion but remained at 212 steps when rods were

withdrawn.

The plant process comput~r, which provides redundant group 1

movement demand indication, and the IRPis indicated that rod motion

occurred as required.

Prior to performing corrective maintenance on January 28, the SNSOC

convened to approve the work instructions.

The inspectors attended the

SNSOC meeting.

Du~ing the meeting, thi maintenance department presented

detailed troubleshooting instructions that included installing test

equipment to monitor logic cabinet and step demand couriter performance

and replacing the shutdown bank B step demand driver card.* SNSOC did

not approve these troubleshooting instructions because a less intrusive

method of repair/troubleshooting was desired.

SNSOC concluded that

replacing the step demand driver card and group 2 step demand counter

was a more prudent course of action.

On January 28 the inspectors witnessed replacing the shutdown bank B

group 2 step demand count~r and shutdown bank B group 1 and 2 step

demand counter driver card. This maintenance was accomplished in

accordance with troubleshooting WO 281688 and procedure O-ICM-RD-CAB-

001, Rod Control System Power Cabinet and Logic Troubleshooting and

Maintenance, revision 0.

The inspectors noted that the maintenance_ was

efficiently accomplished and communications between operations and I&C

personnel were good.

An I&C supervisor, maintenance engineer and

training instructor assisted the I&C technicians performing this

  • maintenance.

Following replacement of the components,* all control rods were exercised

in accordance with 2-0PT-RX-005, Control Rod Assembly Partial Movement.

During this test, the shutdown bank B group 2 step demand counter

indicated correct rod movement.

However, the group 1 step demand

counter continued to indicate 212 steps when rods were withdrawn to 225

steps. At the end of the inspection period a vendor representative was

providing site support for the licensee's continued review and

corrective ,actions for this malfunction.

12

TS 3.12.E.1.a indirectly addresses the operational requirements for rod

step demand counters and states that above 50% power, the IRPI system

_ shall be operable and capable of determining the control rod positions

to within twelve steps of their respective group _step demand counter

indications. The inspectors noted that when the group step demand

counters did not provide proper indication or were deenergized for

.maintenance either process computer indication for group 1 rods was

utilized or control rods were rendered immovable but still trippable and

a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> Leo.was entered in accordance with TS 3.12.C.3.

Recurring rod control problems are being reviewed by the licensee as a

station level one priority. The inspectors attended a meeting where the

system engineer made proposals to station management to correct some of

~

the more frequent problems.

A plan for Unit 1 rod control improvements

was discussed which included RCM recommendations as well as component

replacement based on industry NPRDS failure hi story.

The inspectors observed I&C personnel performing Unit 1 rod control card

inspection and replacement.

The inspectors were shown several firing

cards that were replaced because of heat damage and loose soldered

components.

Based on the observed card conditions, their replacement .

was warranted.

When combined with other card inspections and component

replacements, rod control system reliability improvements were expected

by the licensee.

Within the.areas inspected, no violations Were identified. -

5.

Surveillance Inspections (61726, 42700)

Dtiring-the reporting period, the tnspectors reviewed surveill~nce

activities to assure compl ianc*e with the appropriate procedures and TS

requirements.

a.

Unit 1 Control Rod Test

On January 13, from the control room the inspectors witnessed -

operability test of the control rod assemblies' drive mechanisms

and control circuits. This test was performed biweekly using

procedure l-OPT-RX-005, Control Rod Assembly Partial Movement,

revision 1, dated January 12, 1994.

The inspectors observed the

reactor operators manually moving the rods 12 steps, recording the_*

position of the rods, and observing that the appropriate alarms

were activated.

At the termination of the test, a documentation

review was made.

No discrepancies we_re identified.

b.

Ch1lled Water Pump A 1ST

On January 14, the inspectors witnessed testing the A chilled

water pump in accordance with O-OPT-VS-001, Control Room Air

Conditioning System Pump and Valve Inservice Testing, revision 5.

The purpose of this test was to place the A chilled water pump

into service at a specified flow rate and measure pump vibration

. ***

13

and differential pressure.

The testing results indicated that the

pump operated satisfactorily. The inspectors monitored th.is

testing from MER 3, MER 5, and the control room.

The inspectors

verified that the instrumentation used to obtain test data was

calibrated and the procedure was followed. * No discrepancies were

identified .

. c.

Unit I J-Bus and H-Bus Logic Testing

On January 24, the inspectors witnessed portions of the Unit I

J-Bus logic testing as specified in procedure l-OPT-ZZ-002.

The

test consisted of two basic parts. The first was a simulated

high-high containment pressure initiated SI. This part was

.

followed by a simulated loss of off-site power.

During the LOOSP

~ortion of the test the r~nning EDG picked up the emergency bus

electrical loads and powered the bus while selective ESF loads

sequenced back ont~ the bus.

The test was well coordinated and

the pre-evolution briefing was extensive and well articulated.

The inspectors monitored the control room_portion of the test as

well as communications between the test director and the many data

gathering stations in other areas of the plant. Several equipment

problems were noted and documented on DRs including S-94-0136 for

the tripping of l-VS-F-58A which was not an expected action based

on system alignment for the test. -Additionally, the inspectors

noted that while the 1-J bus was being powered solely by the

  1. 3 EDG the unlicensed operator created a low voltage condition on

the bus while attempting to adjust VARs.

Step 6.4.8 of procedure

I~OPT-ZZ-002 required that a voltage between 4000 and 4400 Vac be

maintained by the EDG and* for the operator to adjust if necessary.

The operator attempted to adjust the VAR reading by lowering the

voltage regulator setting. With the EDG as the sole source of

power to the bus, this action did not regulate VAR loading;

however, it did result in a low voltage condition.

The licensed

operator in the area noted the condition and voltage was returned

within the specified values.

The inspectors expected a DR to be written on the above low

voltage condition but, after several days, one had not been

written. The inspectors informed the SNS supervisor responsible

for the DR system that per VPAP-1501, Station Deviatioh Reports,

the observed condition would meet the threshold for a DR to be

written.

On January 27, DR S-94-0169 was written to document the

occurrence and evaluate the impact of the undervoltage condition

on plant equipment that was energized from the 1-J bus. This was

identified to licensee management as an example of where

Operations threshold for documenting conditions adverse to quality

may need adjusting. Discussions with the SNS supervisor revealed

that their review of recent events had also identified the

possibility of a negative trend in DR identification. Operation

management held discussions with their personnel and the

inspectors will continue to monitor this area.

14

The 1-H bus testing was monitored on January 25 and during that*

test a number of equipment problems were noted and documented on

DRs.

Examples of the items identified include the following:

1) DR S-94-0148, Terminal 112 inside UPS 1A2 was glowing red; 2)

DR S-94-151, Containment isolation valve 1-DA-TV-lOOA did not

indicate fully closed; 3) DR S-94-152, Containment isolation valve

l-CC-TV-105A failed to close and would not close with push-button;

4) DR S-94-150, Breaker for Recirculation Spray pump l-RS-P-2A did -

not close when it was sequenced back on the bus following the

undervoltage test; and 5) DR S-94-153, Breaker for SW valve_

l-SW-MOV-102A tripped on thermal overload. These conditioris were

_ noted on the test procedure discrepancy list as well and will

require resolution prior to the satisfactory completion of the

surveillance test before unit restart.

Withih the areas inspected, no vi-0lations were identified.

6.

Review of Plant Minor Modifications (37828)

a.

Modification to Waterproof Unit 1 MOV Operator

The inspectors monitored portions of DCP 93-17, Modify CW_ -

Limitorque Motor Operators-Submersible/Surry/Units 1 and 2.

The

purpose of this design ch~nge was to modify the eight condenser CW

inlet MOV actuators to make them watertight. Watertight actuators

would enhance MOV operation if these actuators were to become

submersed in water during a turbine building flood.

The

inspectors witnessed the modifications implemented by the design

change and the testing. associated with l-CW-MOV-106A.

This design

change was accomplished by WO 266884, Protedure o~MCM-0305-01,

Limitorque Size SMB-0 Through SMB-4 Overhaul, revision 5 and DCP

93-17.

-

This modification involved replacing several actuator gaskets and

0-rings, installing RTV on the actuator's motor end bell joint and

fasteners, and installing electrical quick disconnect fasteners at*

the power leads to the actuator.

Following reassembly, an air

drop test was performed in accordance with O-NAT-M-004, Generic

Hydrostatic/Pneumatic Test Procedure, revision 1. The actuator

was pressurized to 4.5 psig and the acceptance criteria was that

pressure could drop no more than 0.5 psig within _one hour~

The

actuator failed the initial air test. Several minor leaks were

identified and r~paired.

Following these repairs the actuator was

satisfactorily tested. The MOV was also satisfactorily stroked

timed and diagnostically-tested.

The inspectors noted that this design change was accomplished on

l-CW-MOV-106A without any deficiencies noted. It was evident that

the mechanical and electrical maintenance personnel were prepared

to properly implement this design change.

I

15

b.

Modification to Increase Unit 2 MOV Operator Torque Output

The inspectors witnessed changing the motor and worm gear shaft*

gears on Unit 2 MOV 2-SI-MOV~2862B.

The licensee's GL 89-10

review identified that during a combination of high ambient

temperature and reduced voltage, the overall gear ratio of the

motor operator did not produce the desired torque.

Based on this

review, the motor operator gear set was replaced with gears that

produced a higher operator torque output. This modification also

  • resulted in a slower strok~ time.

This modification was accomplished in accordance with DCP 92-83~3,

Misc Limitorque Motor Operator MODS/Surry/1&2, revision 5;

Procedure O-MCM-0304-02, Limitorque SMB-00 Overhatil, revision 3;

O-ICM-15050-01, Limitorque SMB Operator Disconnect and Connect,

revision 1; and WO 280451.

The inspector attended the SNSOC

meeting that approved this design change and safety evaluation,

monitored portions of the motor operator gear set replacement and

witnessed portions of the post modification testing.

Prior to disassembling the actuator, a torque wrench was utilized

to operate the MOV in order to determine the torque required to

  • . operate 2-SI-MOV-2862B.

The testing re~ults ide~tified that it

took less than 25 ft-lbs of torque to operate the quarter turn

plug valve.

Vendor information on this valve stated that

approximately 40 ft-lbs of torque was required to operate the

valve.

The licensee concluded that 40 ft-lbs of torque applied to

a new valv~, and as it aged, less torque was required.

In

addition, 2-SI-MOV-2862B had been satisfactorily stroke tested on

a quarterly basis. The valve history indicated that there were no

operational problems associated with the valve.

The licensee-

concluded that 2-SI-MOV-2862B was operational prior to

implementing the design change.

The inspectors agreed with the

licensee's conclusion that the valve was operable .. The inspectors

concluded that the design change package adequately implemented

the modification to 2-SI-MOV-2862B.

Within the areas inspected no violations were identified.

7.

Unit 1 Inservice Testing

On January 22, the inspectors witnessed/reviewed portions of two 10-year .

ISi pressure tests.

ASME Code Section XI, requires that every 10 years

piping systems be hydrostatically tested to determine integrity. The

licensee substituted the pressure test for the hydrostatic test required

by the code by invoking ASME Code Case N-498.

The NRC endorsed this

Code Case through revision 9 of Regulatory Guide 1.147; Inservice

Inspection Code Case Acceptability, ASME Sect ion XI Division 1.

The first test-witnessed by the inspectors was a VT-2 visual inspection

of two sections of SI piping located in the Auxiliary Building between

valves l-SI-150 and 1-SI-174 and their respective containment

16

  • penetrati6ns.

The stated test pressure was 2135 psig with th~ normal

system operating pressure being 2235 psig. While performing the test,

the actual pressure obtained through throttling the manual valves was

approximately 2500 psig based on the.local gage. This was due to the

sensitivity of the manual valves.

Th~ inspectors questioned the

adequacy of the test pressure and concluded that it was satisfactory.*

The second test reviewed by the inspectors was a four-hour system

pressure test of the excess let-down heat exchanger.

The inspectors

noted through a review of the operator, logs that approximately 39.

minutes after the excess let-down heat exchanger was pressurized with

RCS fluid, radiation monitors l-CC-RM-105 and 106 went into an alert

alarm indicating a possible tube leak. This heat exchang~r had been

suspected as leaking in the past and was only used whenever the normal

let-down path was isolated.

The in~pectors questioned the licensee as

to whether this leak would cause the component to fail the system

pressure test. The inspectors reviewed the completed copy of the

pressure test procedure and found no mention of the indication of the

tube leakage.

The inspectors reviewed the applicable ASME Code Section XI requirement~

and determined that heat exchanger tube *leakage would be rejectable.

Note 6 of the licensee'sSection XI program stated that visually

inspecting the heat exchanger tubes was not required.

However, note 6

also state'd, "Good Engineering Practices will continue to be followed

when the need is recognized".

The inspectors recognize that the system

pressure test of the excess let-down heat exchanger was not structured

to identify tube leakage.

However, "good engineering practice" should

havi required th~t the noted RCS leakage into the CC system be evaluated

and corrected.

On January 27, five days after the occurrence and after

discussion with the inspectors, the licensee initiated DR s~94-0168 to

docum~nt the event. This was identified as another example of

operators' inappropriate threshold for problem identification and was

discussed with the Superintendent of Operations.

WO 262027 scope was

expanded to investigate and repair the tube leakage prior to unit

restart. *

8.

Action on Previous Inspection Items (92701)

(Closed) IFI 50-280, 281/92-17-01, Gas Void Long-Term Corrective Action.

In July 1992, the licensee identified gas voids in the LHSI piping.

Immediate corrective action involved venting the LHSI piping.

The

licensee replaced cold leg check valve 2-SI-85 during the 1993 Unit 2

spring RFO and modified procedure 2-PT-18.11, Cold Shutdown Test of SI

Check Valves to Hot and Cold Legs, to ensure that the SI system was

properly filled and vented.

The inspectors reviewed the 1993 results of

procedure 2-0SP-SI-001, Venting SI Piping, which was performed

quarterly. The review results indicated that gas had not been

identified in the Unit 2 SI piping since the 1993 Spring RFO.

Within the areas inspected, no violations were identified.

17

9.

Exit Interview

The inspection scope and findings were summarized on February 8 and

March 7, 1994, with those persons indicated in paragrap.h 1. the

inspectors described the areas inspected and discussed in detail the

inspection results addressed in the Summary section and those listed

below.

- Item Number

Status

Description

(Paragraph No.}

NCV 50-280/94-02-01

Closed

Failure To Follow Fire Seal

Inspection Requirements

(paragraph 3.b).

URI 50-280/94-02-02 *

Open

Review Reactor Vessel Level

Problem* (paragraph 3.i).

URI 50-280/94-02-03

Open

Evaluation of .Pressurizer

Hydrogen Burn (paragraph 3.j).

IF! 50-280, 281/92-17-01

Closed

Gas Void Long-Term Corrective

Action (paragraph 8).

Dissenting comments were not received from the liceDsee.

Proprietary

. information is not contained in this report.

10:

Index of Acronyms and Inttialisms

ASME

cc

CFR

CPM

cw

DAC

DCP

DR

ECCS .

EDG

ERFCS

ESF

FME

GL

HR

HP

HQ

HS

HSD

HX

I&C

IFI

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

COMPONENT COOLING

CODE OF FEDERAL REGULATIONS

COUNTS PER MINUTE

COOLING WATER

DERIVED AIR CONCENTRATION

DESIGN CHANGE PACKAGE

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

EMERGENCY RESPONSE FACILITY COMMUNICATION SYSTEM

ENGINEERED SAFETY FEATURE

FOREIGN MATERIAL EXCLUSION

GENERIC LETTER

HOUR

HEALTH PHYSICS

HEADQUARTERS

HEATING STEAM

HOT SHUTDOWN

HEAT EXCHANGER

INSTRUMENTATION AND CALIBRATION

INFORMATION FOLLOWUP ITEM

.\\.,

. .

.. . ,

!RPI

ISi

1ST

LCO

LER

LHSI

LOOSP

MER

MFWP

MOV .

MREM

MSIV

MW

NCV

NI

NIS

NPRDs*

NRC

PCM

PSIG

PT

RCS

RFO

RM

RS

RSHX

. RTV.

RWST

SG

SI

SNS

SNSOC

SPDS

SRO

SW

T AVG

TS

TSC

UPS

VAC

VAR

VPAP

WO 18

INDIVIDUAL ROD POSITION. INDICATION

INSERVICE INSPECTION

INSERVICE TESTING

LIMITING CONDITIONS OF OPERATION

LICENSEE EVENT REPORT

LOW HEAD SAFETY INJECTION

LOSS OF OFFSITE POWER.

MECHANICAL EQUIPMENT ROOM

MAIN FEEDWATER PUMP

MOTOR OPERATED VALVE

MILLI-ROENTGEN

MAIN STEAM ISOLATION VALVE

MEGAWATTS

NON-CITED VIOLATION

NUCLEAR INSTRUMENTATION

NUCLEAR INSTRUMENTATION SYSTEM

NUCLEAR PLANT RELIABILITY DATA SYSTEM

NUCLEAR REGULATORY COMMISSION

PERSONNEL CONTAMINATION MONITOR

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

RADIATION MONITOR

RECIRCULATION SPRAY

RECIRCULATION SPRAY HEAT EXCHANGER

ROOM TEMPERATURE VULCANIZER

REFUELING WATER STORAGE TANK

. STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SAFETY PARAMETER DISPLAY SYSTEM

SENIOR REACTOR 0-PERATOR

SERVICE WATER .

AVERAGE TEMPERATURE

TECHNICAL SPECIFICATION

TECHNICAL SUPPORT CENTER

UNINTERRUPTIBLE POWER SUPPLY

VOLTS - ALTERNATING CURRENT

VOLTS-AMPERE, REACTIVE

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER